Rockwell Aero Commander 500
Safety Rating
9.8/10Total Incidents
93
Total Fatalities
165
Incident History
Private Dominican
Apparently following technical issues, the pilot was forced to attempt an emergency landing at Dabajuro Airport. The twin engine aircraft crash landed near the runway and struck two motorcyclists. One of them was killed while the second was injured. The airplane was damaged beyond repair and the pilot was uninjured.
Aerial Viewpoint
The airline transport pilot was conducting a cross-country repositioning flight. While en route to the destination airport, the pilot contacted air traffic control and stated that he was beginning to descend. No further radio transmissions were made by the pilot. Radar and GPS information showed, about the same time as the pilot's last transmission, the airplane's flightpath began descending in a westerly direction. The last recorded GPS point showed the airplane about 200 ft southwest of the initial impact point, 90 ft above ground level, and at a groundspeed of 66 knots. The airplane wreckage was located in an open field and impact signatures were consistent with a stall/spin, which had resulted in a near-vertical impact at a slow airspeed. The right propeller blades were found in the feathered position. Examination of the right engine found that the oil gauge housing extension was improperly secured to the oil gauge housing, which resulted in a loss of engine oil. Additionally, the examination revealed a hole in the right engine's crankcase, metal material in the oil sump, and signatures consistent with the lack of lubrication. Cockpit switches were positioned in accordance with the in-flight shutdown of the right engine. No anomalies were found with the left engine or airframe that would have precluded normal operation. Another pilot who had flown with the accident pilot reported that the pilot typically used the autopilot, and the autopilot system was found with the roll, heading, and pitch modes active. During the descent, no significant changes of heading were recorded, and the direction of travel before the stall was not optimal for the airplane to land before a fence line. It is likely that the autopilot was controlling the airplane's flightpath before the stall. Despite one operating engine, the pilot did not maintain adequate airspeed and exceeded the airplane's critical angle-of-attack (AOA), which resulted in an aerodynamic stall/spin. Correcting the last GPS recorded airspeed for prevailing wind, the airplane's indicated airspeed would have been about 72 knots, which is above the airplane's 0-bank stall speed, but an undetermined mount of bank would have been applied to maintain heading, which would have accelerated the stall speed. It could not be determined why the pilot did not maintain adequate airspeed or notify air traffic controller of an engine problem. Although a review of the pilot's medical records revealed that he had several historical medical conditions and the toxicology tests detected several sedating allergy medications in his system, it was inconclusive whether the medical conditions or medications impaired the pilot's ability to fly the airplane or if the pilot was incapacitated. It is also possible that the pilot was distracted by the loss of oil from the right engine and that this resulted in his failure to maintain adequate airspeed, his exceedance of the airplane's critical AOA, and a subsequent stall/spin; however, based on the available evidence, the investigation could not determine the reason for the pilot's lack of corrective actions.
Central Air Southwest
The commercial pilot was conducting an on-demand cargo charter flight. Shortly after takeoff, the pilot informed the tower controller that he wanted to "come back and land" because he was "having trouble with the left engine." The pilot chose to fly a left traffic pattern and return for landing. No further transmissions were received from the pilot. The accident site was located about 0.50 mile southeast of the runway's displaced threshold. GPS data revealed that, after takeoff, the airplane entered a left turn to a southeasterly course and reached a maximum GPS altitude of 959 ft (about 342 ft above ground level [agl]). The airplane then entered another left turn that appeared to continue until the final data point. The altitude associated with the final data point was 890 ft (about 273 ft agl). The final GPS data point was located about 135 ft northeast of the accident site. Based on GPS data and the prevailing surface winds, the airspeed was about 45 knots during the turn. According to the airplane flight manual, the stall speed in level flight with the wing flaps extended was 59 knots. Postaccident examination and testing of the airframe, engines, and related components did not reveal any preimpact mechanical failures or malfunctions that would have precluded normal operation; therefore, the nature of any issue related to the left engine could not be determined. Based on the evidence, the pilot failed to maintain adequate airspeed while turning the airplane back toward the airport, which resulted in an aerodynamic stall/spin.
Houston Air
The pilot stated that, during the preflight inspection of the airplane, he checked the fuel gauge, and it indicated 65 gallons. Due to the design of the fuel system, it is not possible to visually check the fuel level to confirm that the fuel gauge indication is accurate. During takeoff and as he reduced power for enroute climb, the left engine began to surge and lose power. He immediately turned left back toward the airport and contacted the control tower to advise that he was making a single-engine, straight-in approach to land. When he lowered the landing gear, the right engine began to surge and lose power. Subsequently, the pilot declared an emergency, and, realizing he had insufficient engine power and altitude to return to the airport, he retracted the landing gear and made a no-flap, gear-up landing on a nearby golf course. Postaccident application of battery power to the airplane confirmed that the fuel gauge indicated 65 gallons; however, when the airplane's fuel system was drained, only about 1/2 gallon of fuel was recovered. Thus, the engines lost power due to fuel exhaustion.
Central Air Southwest
The pilot was en route on a positioning flight when the airplane’s right engine surged and experienced a partial loss of power. He adjusted the power and fuel mixture controls; however, a few seconds later, the engine surged again. The pilot noted that the fuel flow gauge was below 90 pounds, so he turned the right fuel pump on. The pilot then felt a surge on the left engine, so he performed the same actions he as did for the right engine. He believed that he had some sort of fuel starvation problem. The pilot then turned to an alternate airport, at which time both engines lost total power. The airplane impacted trees and terrain about 1.5 miles from the airport. The left side fuel tank was breached during the accident; however, there was no indication of a fuel leak, and about a gallon of fuel was recovered from the airplane during the wreckage retrieval. The company’s route coordinator reported that prior to the accident flight, the pilot checked the fuel gauge and said the airplane had 120 gallons of fuel. A review of the airplane’s flight history revealed that, following the flight immediately before the accident flight, the airplane was left with approximately 50 gallons of fuel on board; there was no record of the airplane having been refueled after that flight. Another company pilot reported the airplane fuel gauge had a unique trait in that, after the airplane’s electrical power has been turned off, the gauge will rise 40 to 60 gallons before returning to zero. When the master switch was turned to the battery position during an examination of another airplane belonging to the operator, the fuel gauge indicated approximately 100 gallons of fuel; however, when the master switch was turned to the off position, the fuel quantity on the gauge rose to 120 gallons, before dropping off scale, past empty. Additionally, the fuel cap was removed and fuel could be seen in the tank, but there was no way to visually verify the quantity of fuel in the tank.
Central Air Southwest
Prior to the flight, the pilot preflighted the airplane and recalled observing the fuel gauge indicating full; however, he did not visually check the fuel tanks. The airplane departed and the en route portion of the flight was uneventful. During the downwind leg of the circling approach, the engines began to surge and the pilot added full power and turned on the fuel boost pumps. While abeam the approach end of the runway on the downwind leg, the engines again started to surge and subsequently lost power. He executed a forced landing and the airplane impacted terrain short of the runway. A postaccident examination by Federal Aviation Administration inspectors revealed the fuselage was buckled in several areas, and the left wing was crushed and bent upward. The fuel tanks were intact and approximately one cup of fuel was drained from the single fuel sump. Fueling records indicated the airplane was fueled 3 days prior to the accident with 135 gallons of fuel or approximately 4 hours of operational time. Flight records indicated the airplane had flown approximately 4 hours since refueling when the engines lost power.
Rolando Velasco
The twin engine aircraft departed San Juan-Isla Grande Airport on a private flight to Santo Domingo with two passengers and two pilots on board. On final approach to Santo Domingo-Las Américas-Dr. José Francisco Peña Gómez Airport, at an altitude of 2,000 feet and at a distance of 8 km from the airport, both engines failed simultaneously. As the crew realized he was unable to reach the airport, he attempted an emergency landing when the aircraft crashed in a dense wooded area located about one km southeast of runway 35 threshold. All four occupants escaped uninjured and the aircraft was damaged beyond repair.
Frank N. Vessels
The evening prior to the accident, the pilot acquired a computer generated text weather briefing. On the day of the accident, the pilot acquired another computer generated text weather briefing, and then contacted the Flight Service Station (FSS) for an interactive telephonic weather briefing. The information provided in all three briefings indicated that a flight on a direct route between the pilot's point of departure and his planned destination would take him through an area of forecast rain showers, thunderstorms, and cloud tops significantly higher than his intended en route altitude. Although the FSS briefer recommended an alternate route, for which he provided weather information, after departure the pilot flew directly toward his destination airport. While en route, the pilot, who was not instrument rated, encountered instrument meteorological conditions, within which there was an 80 percent probability of icing. After entering the area of instrument meteorological conditions, the airplane was seen exiting the bottom of an overcast cloud layer with a significant portion of its left wing missing. It then made a high velocity steep descent into the terrain. A postaccident inspection of the airplane's structure did not find any evidence of an anomaly that would contribute to the separation of the wing structure, and it is most likely that the wing section separated as a result of the airplane exceeding its structural limitations after the pilot lost control in the instrument meteorological conditions.
Private Botswana
Upon landing at Gaborone-Seretse Khama Airport, the twin engine aircraft went out of control, flipped over and crashed, coming to rest upside down on the runway edge. All five occupants were injured and the aircraft was destroyed. The aircraft type is not confirmed.
Central Air Southwest
The commercial pilot departed on a night instrument flight rules flight in actual instrument meteorological in-flight conditions. Less than 2 minutes after the airplane departed the airport, the controller observed the airplane in a right turn and instructed the pilot to report his altitude. The pilot responded he thought he was at 3,500 feet and he thought he had lost the gyros. The pilot said he was trying to level out, and when the controller informed the pilot he observed the airplane on radar making a 360-degree right turn , the pilot said "roger." Three minutes and 23 seconds after departure the pilot said "yeah, I'm having some trouble right now" and there were no further radio communications from the flight. The on scene investigation disclosed that both wings and the tail section had separated from the airframe. All fractures of the wing and wing skin were typical of ductile overload with no evidence of preexisting failures such as fatigue or stress-corrosion. The deformation of the wings indicated an upward failure due to positive loading. No anomalies were noted with the gyro instruments, engine assembly or accessories
Hicks %26 Lawrence
The aircraft departed from Dryden, Ontario, en route to Geraldton, Ontario. The flight was conducted under visual flight rules at 5500 feet above sea level with ambient temperatures aloft of -33°C. Approximately 40 minutes into the flight, the crew observed an abnormal right engine fuel flow indication. While troubleshooting the right engine, the engine rpm and fuel flow began to decrease and the crew diverted toward Armstrong, Ontario. A short time later, the left engine rpm and fuel flow began to decrease and the crew could no longer maintain level flight. At 0917 central standard time, the crew made a forced landing 20 nautical miles southwest of Armstrong, into a marshy wooded area. The captain sustained serious injuries and the co-pilot and passenger sustained minor injuries. The aircraft was substantially damaged. The crew and passenger were stabilized and transported to Thunder Bay, Ontario, for medical assistance.
Central Air Southwest
The airplane was operated as an on-demand cargo flight that impacted trees and terrain about one mile from the destination airport during a non-precision approach. Night instrument meteorological conditions prevailed at the time of the accident. The airplane was equipped with an "icing protection system" and a report by another airplane that flew the approach and landed without incident indicated that light rime icing was encountered during the approach. Radar data shows that the accident airplane flew the localizer course inbound and began a descent past the final approach fix. No mechanical anomalies that would have precluded normal operation were noted with the airplane.
Joseph L. Ciabattoni
The airplane did not gain altitude after takeoff and collided with trees and terrain off the departure end of the runway. Prior to takeoff the pilot received a computerized weather briefing that showed generally good conditions. The tower controller cleared the pilot to taxi to the active runway (runway 21) and issued winds, which were 300 degrees at 10 knots, a direct crosswind. During the initial climb after liftoff, the pilot saw that the airplane had stopped climbing and he asked for and received the wind information again. With the airplane not climbing and headed directly for some trees, the pilot maneuvered the airplane towards a clearing but the left wing hit a tree and the airplane descended into the ground. The pilot reported no mechanical problems with the airframe and engines. The density altitude was calculated to be 9,481 feet. The aircraft's gross weight at the time of takeoff was 6,000 pounds. Review of the Airplane Flight Manual climb performance charts for that aircraft weight at the pressure altitude and reported outside air temperature discloses that the airplane should have had a positive rate of climb of about 1,100 feet per minute. The airport was equipped with a wind information recording system, which had four sensors. Three sensors recorded wind information at ground level only. They were placed, one each, at the approach, middle, and departure ends of the runway. Wind data was recorded every 10 seconds. The system does not have the capability to predict or warn of wind shear events. During the aircraft's departure, the approach end sensor recorded winds at 068 degrees at 1 knot; the middle sensor recorded winds at 293 degrees at 5 knots; and the departure sensor recorded winds at 302 degrees at 2 knots. At the next data sampling (10 seconds later), the departure end sensor recorded a wind increase of 10 knots, and the approach end recorded a wind shift from a headwind to a tailwind at 10 knots. A full analysis of the weather conditions indicated that due to developing convection over the runway the airplane likely encountered a wind shear (increasing tailwind) event that seriously degraded the takeoff and climb performance.
Robin Williams
The twin-engine airplane was observed at a low altitude of approximately 1,000 feet agl performing power off stall maneuvers. The witness described the first stall maneuver initiation and recovery as "good." During the second stall maneuver, the nose rose higher than it did during the first maneuver, the right wing dropped, followed by a steep nose down attitude. The airplane rotated about one and one half revolutions before disappearing behind trees. Prior to ground impact, the witness heard the engines rev up. The purpose of the flight was to demonstrate the airplane to a prospective buyer. A radar and aircraft performance study indicated that the accident airplane departed the airport and began a series of heading, speed and altitude changes ultimately crashing 14.6 nautical miles east of the departure airport. During several time periods, calculations of the calibrated airspeed indicated a trend towards and below published stall speeds of 63 knots flaps extended and 71 knots flaps retracted. No structural or mechanical anomalies were observed during an examination of the airplane and engine.
Bevins Air Service
On May 31, 2002, about 1315 Atlantic standard time, an Aero Commander 500-B, N78336, registered to Bevins Air Service Inc., operating as a 14 CFR Part 135 air-taxi passenger/cargo flight ditched into the Atlantic Ocean, near Roseau, Dominica. Visual meteorological conditions prevailed and a VFR flight plan was filed. The airplane has not been located and is presumed to be destroyed. The commercial pilot has not been located and is presumed to be fatally injured. The deceased passenger was recovered from the Atlantic Ocean on June 4, 2002. The flight originated from Melville Hall Airport, Roseau, Dominica, at 1240. According to Organization of East Caribbean States (OECS) the pilot informed Guadeloupe Air Traffic Control that the airplane was experiencing engine problems and that he was returning to Dominica. The airplane was last observed on radar about six miles north of Dominica.
Rafael Perez
While descending to Puerto Plata Airport, the crew encountered poor weather conditions and limited visibility due to low clouds and fog. The twin engine aircraft struck the slope of Mt Loma del Toro located few km from Puerto Plata and was destroyed. All seven occupants were killed. The crew started the approach prematurely and descended too low in poor visibility.
Thomas H. Hoffman
The non instrument-rated pilot attempted VFR flight into known instrument flight conditions after being briefed by an FAA Automated Flight Service Station that VFR flight was not recommended. The pilot encountered instrument flight conditions while maneuvering on initial takeoff climb, experienced an in-flight loss of control (stall/spin) due to failure to maintain airspeed, and subsequent in-flight collision with trees and terrain.
EEC Investments
The flight was on approach, and the pilot was in radio contact with approach control. For unknown reasons the pilot performed a 360-degree turn, without permission from the controller, and was then vectored to a different runway. After acknowledging the clearance to the new runway, the controller lost all contact with the flight. None of the radio communications indicated that the pilot was having mechanical or medical problems. A search was initiated by air and a debris field was located. Five yellow life jackets, 1 six man life raft, several unidentified pieces of white and gold airframe were recovered. The pilot and the wreckage were never recovered from the water. At the time of the accident the pilot's license had been suspended by the FAA.
Thomas M. Fisher
Prior to departure the pilot believed that his airplane contained between 30 and 40 gallons of fuel, adequate for a 15-minute-long flight to another airport where he could purchase additional fuel. The pilot reported the fuel gauge registered 40 gallons, so he departed. During initial climb upon reaching an altitude of about 400 feet above the ocean, both engines simultaneously lost power. The pilot rocked the airplane's wings and experienced a 'short surge of power.' However, it lasted only a brief moment and all engine power was again totally lost. The pilot turned toward the shoreline, reduced airspeed, and ditched about 0.25 miles off shore. The overnight tide/wave action subsequently beached most of the airplane. In the pilot's report, he did not indicate having experienced any mechanical malfunctions. The Federal Aviation Administration (FAA) coordinator examined recovered portions of the airframe and engines. In pertinent part, the FAA reported finding no physical evidence of any mechanical malfunction with the examined components. However, because of the airframe damage sustained during immersion in the salt water and the subsequent destruction to components, the Safety Board was unable to document the integrity of the fuel quantity indicator system.
MGS Corporation
After departing on an IFR flight in VFR conditions, the flight had been cleared to climb from 3,000 to 4,000 feet, when the right engine lost power. The pilots diverted toward an uncontrolled airport, secured the right engine, & cancelled their IFR clearance. They made an approach to land on runway 15, then attempted a single engine go-around. During the go-around, the airplane yawed/rolled to the right in what the passenger believed was a VMC roll. It then struck power lines & crashed in a right wing low attitude. Investigation revealed that both pilots held multi-engine ratings. The owner said the pilot (PIC) had flown the airplane for a short time on 12/21/98; however, no other record was found to verify that either the pilot or copilot had flight experience in this make/model of airplane. Examination of the wreckage revealed evidence that the flaps were retracted, the landing gear was in transit, the left propeller was operating with power, & the right propeller was feathered. The airplane had a history of fuel flow fluctuations in the right engine. The diaphragm (P/N 364446) in the right engine distributor valve assembly was found ruptured. It was an old style diaphragm, which was colored black. Bendix Service Bulletin RS-76, issued 11/15/80, called for replacement of the black diaphragm with a red fluorosilicone diaphragm (P/N 245088) at overhaul. The engine was overhauled in June 1992. During maintenance in December 1997, both fuel system injectors & nozzles were tested; however, the distributor valve assembles were not tested. Calculations showed the airplane was loaded 116.3 lbs over the maximum allowable gross weight & 1.3 inches forward of the allowable CG range.
Robert Kirke Dent
The aircraft had an in-flight breakup when the left wing and tail section separated. Post accident inspection revealed a right engine main fuel supply line progressive rupture, only trace amounts of fuel in the fuel lines, and no rotational damage to the right engine. Pre accident, long term, fuel leak evidence surrounded the ruptured line. The right propeller was not feathered. The left wing D-tube rib at station 127 exhibited compressive buckling. Left wing fractures were upward, and horizontal stabilizer deformation was downward. During an actual loss of engine power in the airplane 17 months before this accident, the pilot had feathered the incorrect propeller. Both a mechanic, and an FAA safety counselor, who were familiar with the pilot, described him as able to be disoriented, and reliant on GPS for navigation. He had stated five months before the accident that he did not feel his instrument flying skills were proficient, and desired training. On the day of the accident, weather was visual meteorological conditions, with layered clouds above 2,200 feet mean sea level. The pilot stated to the FAA weather briefer that he wanted to make the flight under visual conditions. The flight route and altitude was unknown.
Domtrav Airways
The pilot departed on a VFR flight behind another company airplane. About 5 minutes after takeoff, the pilot informed the pilot in the lead airplane that he was having a generator problem, and that he would monitor them. The lead airplane landed at a different airport, and waited for the other pilot to join him after dropping off his passengers at another airport. The pilot did not arrive at either airport. All shipping vessels along the airplane's expected course were requested to report any sightings. No contact was reported and the search was terminated. Aircraft damage and injuries are presumed.
Palm Beach Aviation
On July 10, 1995, about 1430 eastern daylight time, an Aero Commander 500, N89M, registered to Candy Yellow Apple, Inc., leased to and operated by Palm Beach Aviation, experienced separation of a propeller blade during the ground roll to takeoff from the Treasure Cay Airport, Treasure Cay, Bahamas. The nonscheduled, international, passenger flight was operating under 14 CFR Part 135. Visual meteorological conditions prevailed at the time and a VFR flight plan was filed for the flight. The airplane was substantially damaged and the airline transport- rated pilot and five passengers were not injured. One passenger was fatally injured. The flight was originating at the time of the accident.
Rent-a-Plane
Shortly after takeoff, while in initial climb, the twin engine aircraft went out of control and crashed in a field located 2 km from the airport. Both pilots were killed. The aircraft was engaged in a cargo flight and was carrying a load of newspapers.
Michelle M. Mellor
The aircraft had not flown for 2 years. Before flight, a mechanic saw evidence of fuel leaking at drain holes in the left wing root, just aft of the main cabin door. He brought this to the attention of the pilotrated passenger, who shortly thereafter, departed in the aircraft with the pilot (pic), the aircraft owner and a passenger/mechanic. About 14 minutes after takeoff, radar data showed the aircraft transitioning from a climb to a descent, while in a 180°turn. Also, witnesses saw smoke/flames trailing from the aircraft. Subsequently, the aircraft impacted trees and power lines, then it crashed in a small flat field in hilly terrain. Post-crash examination revealed melted aluminum spatters on the leading edge and underside of the left horizontal stabilizer. Also, 'focalized' fire damage was noted on the cabin behind the drain holes in the left wing root. Tetrahydrocannabinol carboxylic acid (marijuana) was detected in the pilot-rated passenger's blood (0.004 ug/ml) and urine (0.010 ug/ml).
Raff Aviation
The airplane was observed by witnesses in a rolling maneuver, followed by the separation of the left wing and collision with trees. Witnesses stated that the pilot had performed acrobatics in this airplane on other occasions. The airplane flight manual prohibits intentional acrobatics. No evidence of corrosion or fatigue in the wing spar or support structures was observed.
Palm Beach Aviation
While in level flight the pilot reported both engines failed and all attempts to restart them were unsuccessful. The pilot then ditched the airplane in the ocean, and it sank and was not recovered. The pilot and three passengers were rescued 2 days later. According to fuel consumption estimates there should have been adequate fuel for the entire flight and a reserve.
Central Air Southwest
Both aircraft departed Wichita on IFR flight plan in VFR weather conditions. They flew northwest toward their respective destinations, and cancelled IFR about 20 minutes before the accident. ATC observed the airplanes on radar, and stated they were 'dogfighting back and forth' prior to the collision. One pilot's roommate reported the two pilots, who were close friends as well as co-workers, often cancelled IFR and flew in formation if the weather was VFR. He reported the pilots often videotaped each other, and he had watched some of the tapes. He stated 'it was hard to tell from the videotape how close they were because they could use the zoom feature, etc. You could read the N numbers.' Investigation revealed brown paint transfer on the bottom of the right wing of the blue and white airplane, which had separated and was located 1.5 miles from the main wreckage. There were light colored scuff marks on the top of the left engine nacelle of the brown and white airplane. Both aircraft and both pilots were killed.
Central Air Southwest
Both aircraft departed Wichita on IFR flight plan in VFR weather conditions. They flew northwest toward their respective destinations, and cancelled IFR about 20 minutes before the accident. ATC observed the airplanes on radar, and stated they were 'dogfighting back and forth' prior to the collision. One pilot's roommate reported the two pilots, who were close friends as well as co-workers, often cancelled IFR and flew in formation if the weather was VFR. He reported the pilots often videotaped each other, and he had watched some of the tapes. He stated 'it was hard to tell from the videotape how close they were because they could use the zoom feature, etc. You could read the N numbers.' Investigation revealed brown paint transfer on the bottom of the right wing of the blue and white airplane, which had separated and was located 1.5 miles from the main wreckage. There were light colored scuff marks on the top of the left engine nacelle of the brown and white airplane. Both aircraft and both pilots were killed.
Central Air Charter
The aircraft departed Garden City under extremely poor weather conditions. More than half way to Dodge City, the pilot reported engine problems to Kansas City (ARTCC). Vectors were provided to the Dodge City Airport, but the pilot did not maintain assigned headings. The aircraft headed back towards Garden City to attempt an instrument approach. Radar vectors were provided for the localizer approach. Radar indicated that the aircraft did not become stabilized on the approach. There was a significant loss of ground speed as the pilot was attempting to get established on the localizer. Radar contact was lost about 2 miles from the airport at a speed approaching stall speed for this aircraft. The aircraft crashed about 2 miles short and to the right of course. The aircraft impacted in a vertical nose down attitude on heading which indicated a turn away from the airport. The left prop was found in the feather position. No mechanical problem was discovered. The right engine appeared to be producing full power at impact. The pilot, sole on board, was killed.
Miller Flying Service
The airplane was in a normal appearing climb after takeoff when it pitched up to a 70° to 80° attitude, stalled, dropped the right wing, then leveled the wings and hit the ground in a near-flat attitude. The weight and cg were within limits. No preimpact problems were found that could cause an inadvertent pitchup. Pilot's only memory is that he couldn't get the control column far enough forward to stop the pitchup. The pilot's seat was found in the full forward position with the right locking pin in the locking hole and the left pin 1/4th of an inch forward of the front locking hole. There were no visible marks on either of the locking pins. Deep scratches were found on the sides of the rail where the seat attachments normally slide back and forth when the seat is adjusted. Exam of the outboard side recessed surface near the aft end disclosed what appeared to be a fresh scratch. The pilot, sole on board, was seriously injured.
Fairburn Aviation Services
The aircraft was being used to transport equipment for members of an Aero Club, who were to carry out training at Goulburn. As the pilot was undergoing formation flying training, it was decided that he would lead a formation of two aircraft for the flight. A briefing on the procedures to be followed was carried out. During the flight the pilot of the second aircraft began to suspect the accuracy of his aircraft's airspeed indicator and requested that it be checked against that of the lead aircraft as the aircraft joined the circuit. The pilot of the lead aircraft extended the landing gear and flew the initial leg of the circuit at an indicated airspeed of 96 knots. At the end of this leg the pilot turned the aircraft steeply to the left, the nose dropped slightly and the aircraft flicked into a steep right turn. The aircraft then assumed a steep nose down attitude, however, the pilot was able to level the wings and raise the nose to the level attitude before impact. The impact occurred at a very high rate of sink. The pilot had not previously practiced steep turns at relatively slow airspeed and was not aware of the stalling speed in the given configuration and attitude. The pilot was subsequently unable to recall the reason for attempting a steeper than normal turn. When the aircraft stalled the pilot was unable to effect a full recovery in the height available before impact with the ground.
Hawk Aviation
En route from The Bahamas to Florida, the twin engine airplane crashed in unknown circumstances into the sea about 17 km off Rat Cay Island. The pilot, sole on board, was killed. Contraband was found on board. Illegal flight.
Combs FreightAir
The pilot said that when he called on the radio prior to the approach for an altimeter setting the reply was '30.11 or 30.12, something like that.' The aircraft altimeter was found after the accident set at 30.22 inches of mercury. The visibility was described as 1 and 1/2 miles in snow showers. He continued the approach 'because minimums are one mile.' He descended outbound to 4,500 feet. Minimum procedure turn alt is 4,700 feet msl. The pilot then descended to 3,700 feet msl as he approached the VOR. Power was reduced to 17-18 inches of manifold pressure and airspeed reduced to 120 knots. As the VOR was crossed he glanced at the altimeter and 'the hands were in the two o'clock position.' Landing gear was extended and approach flaps set. The pilot said all seemed normal. He looked out the window and saw 'wispy clouds going by rapidly. Then there were the sounds of impact.' The next thing remembered was the sound of dripping gasoline. The pilot said he crawled out of the cockpit window and wandered 'for a couple hours trying to chase down the searchlights.'
Walley Construction Company
Before departing Youngstown, OH, the pilot filed two IFR flight plans, one for a flight to Plattsburgh, NY, the other for a return flight from Plattsburgh back to Youngstown. After a 2 hour and 10 minutes flight to Plattsburgh, 70 gallons of fuel was added, but the person who serviced the aircraft indicated the tanks were not full after servicing. The plane then made a 10 minutes flight to Burlington, VT, but no fuel was added at Burlington. The pilot then took off on a return flight to Youngstown. During the descent phase to Youngstown, the pilot requested vectors to the closest airport. He was provide vectors to the Chess Lamberton Airport and advised it was 6 miles away. A short time later, the pilot said the aircraft had lost power. Subsequently, it crashed in rolling, wooded terrain. During an exam, no fuel was found in the aircraft. No other evidence of a malfunction or failure was found. With the passenger and cargo load, a maximum of about 104 gallons of fuel could have been used without exceeding the certificated gross weight of the aircraft. At 45 to 55% power, the aircraft burned 17 to 22 gallons per hour. Wind gusts 30 knots. All six occupants were killed.
Líder Taxi Aéreo
Crashed under unknown circumstances near Anapuera (exact location unknown).
A. W. Hirshberg
While flying at low height by night, the twin engine airplane struck trees and crashed near Flagler Beach, bursting into flames. The passenger was killed in the accident while the pilot was not found. Injury is presumed. The aircraft was destroyed. A load of marijuana was found in the wreckage.
Jarlin Aviation
The twin engine airplane was completing a flight from Johannesburg-Rand Airport to Riversdale, carrying four members of the South African Air Defence School. En route, the airplane struck the north face of Mt Fouriesberg located in the region of Oudtshoorn, about 10 km west of Robinson Pass. All four occupants were killed.
James B. Urban
After takeoff from Buffalo Airport in blowing snow, the twin engine airplane encountered difficulties to maintain a positive rate of climb. It collided with ground and subsequently crashed. All four occupants were killed.
Commander 6206
On approach to Santa Maria, the pilot encountered poor weather conditions with low ceiling and a limited visibility due to fog. He initiated a go-around manoeuvre and started a second ILS approach few minutes later. In a visibility limited to two miles or less, he failed to realize his altitude was too low when the airplane struck a mountain slope located about six miles from the airport. The aircraft was destroyed and both occupants were killed.
Hansa Luftbild
The aircraft and its crew took part to an airshow that day at Münster-Telgte Airport. At the end of the afternoon, the crew departed Telgte Airport to return to his base at Münster-Osnabrück Airport. About two minutes after takeoff, the twin engine airplane lost height and crashed onto a farm located about 3,5 km from the airfield. The aircraft was destroyed and all three occupants were killed.
United States Forest Service - USFS
The pilot and the passenger were engaged in a survey flight from Salmon to McCall. While flying at low height, the twin engine airplane struck trees and crashed in a dense wooded area. While the passenger was seriously injured, the pilot was killed.
Combs FreightAir
While flying in marginal weather conditions, the pilot failed to realize his altitude was insufficient when the twin engine airplane struck trees and crashed in a mountain shrouded in clouds. The pilot, sole on board, was killed.
Iron Bird
While in cruising flight between Andros Town and West Palm Beach, the pilot encountered poor weather conditions when the airplane crashed in unknown circumstances in the Florida Strait. SAR operations were initiated but no trace of the aircraft nor the pilot was found. The wreckage was not recovered.
Palm Beach Aviation
During initial climb at Treasure Cay Airport, one of the engine failed. Unable to maintain a positive rate of climb, the airplane struck trees and lost height. The pilot decided to ditch the airplane into the sea, less than two km northeast of the airfield. The pilot was slightly injured and the airplane was lost.
Connie E. Bowman
While approaching Laredo area by night, the pilot encountered marginal weather conditions with low ceiling and limited visibility. He completed several turns when the airplane entered a dive and crashed. The airplane was totally destroyed upon impact and all seven occupants were killed.
Combs FreightAir
The pilot, sole on board, was completing a night cargo flight from Helena to Great Falls. On approach, he encountered poor weather conditions when the airplane struck the ground and crashed few miles short of runway threshold. The aircraft was destroyed and the pilot was killed. At the time of the accident, weather conditions were below minimums.
Private Bolivian
On final approach to La Paz-El Alto Airport, the twin engine airplane struck the ground about one km short of runway threshold. It slid in a field and came to rest against a stone wall. All occupants escaped uninjured while the aircraft was damaged beyond repair.
Safety Profile
Reliability
Reliable
This rating is based on historical incident data and may not reflect current operational safety.
