Wrangell – Everett

The aircraft had an in-flight breakup when the left wing and tail section separated. Post accident inspection revealed a right engine main fuel supply line progressive rupture, only trace amounts of fuel in the fuel lines, and no rotational damage to the right engine. Pre accident, long term, fuel leak evidence surrounded the ruptured line. The right propeller was not feathered. The left wing D-tube rib at station 127 exhibited compressive buckling. Left wing fractures were upward, and horizontal stabilizer deformation was downward. During an actual loss of engine power in the airplane 17 months before this accident, the pilot had feathered the incorrect propeller. Both a mechanic, and an FAA safety counselor, who were familiar with the pilot, described him as able to be disoriented, and reliant on GPS for navigation. He had stated five months before the accident that he did not feel his instrument flying skills were proficient, and desired training. On the day of the accident, weather was visual meteorological conditions, with layered clouds above 2,200 feet mean sea level. The pilot stated to the FAA weather briefer that he wanted to make the flight under visual conditions. The flight route and altitude was unknown.

Flight / Schedule

Wrangell – Everett

Registration

N543AN

MSN

500-908-17

Year of Manufacture

1960

Date

September 6, 1997 at 01:00 PM

Type

CRASH

Flight Type

Private

Flight Phase

Flight

Crash Site

Plain, Valley

Crash Location

Ketchikan Alaska

Region

North America • United States of America

Coordinates

55.3431°, -131.6467°

Crash Cause

Human factor

Narrative Report

On September 6, 1997 at 01:00 PM, Wrangell – Everett experienced a crash involving Rockwell Aero Commander 500, operated by Robert Kirke Dent, with the event recorded near Ketchikan Alaska.

The flight was categorized as private and the reported phase was flight at a plain, valley crash site.

2 people were known to be on board, 2 fatalities were recorded, 0 survivors were identified or estimated. This corresponds to an estimated fatality rate of 100.0%.

Crew on board: 1, crew fatalities: 1, passengers on board: 1, passenger fatalities: 1, other fatalities: 0.

The listed crash cause is human factor. The aircraft had an in-flight breakup when the left wing and tail section separated. Post accident inspection revealed a right engine main fuel supply line progressive rupture, only trace amounts of fuel in the fuel lines, and no rotational damage to the right engine. Pre accident, long term, fuel leak evidence surrounded the ruptured line. The right propeller was not feathered. The left wing D-tube rib at station 127 exhibited compressive buckling. Left wing fractures were upward, and horizontal stabilizer deformation was downward. During an actual loss of engine power in the airplane 17 months before this accident, the pilot had feathered the incorrect propeller. Both a mechanic, and an FAA safety counselor, who were familiar with the pilot, described him as able to be disoriented, and reliant on GPS for navigation. He had stated five months before the accident that he did not feel his instrument flying skills were proficient, and desired training. On the day of the accident, weather was visual meteorological conditions, with layered clouds above 2,200 feet mean sea level. The pilot stated to the FAA weather briefer that he wanted to make the flight under visual conditions. The flight route and altitude was unknown.

Aircraft reference details include registration N543AN, MSN 500-908-17, year of manufacture 1960.

Geospatial coordinates for this crash are approximately 55.3431°, -131.6467°.

Fatalities

Total

2

Crew

1

Passengers

1

Other

0

Crash Summary

The aircraft had an in-flight breakup when the left wing and tail section separated. Post accident inspection revealed a right engine main fuel supply line progressive rupture, only trace amounts of fuel in the fuel lines, and no rotational damage to the right engine. Pre accident, long term, fuel leak evidence surrounded the ruptured line. The right propeller was not feathered. The left wing D-tube rib at station 127 exhibited compressive buckling. Left wing fractures were upward, and horizontal stabilizer deformation was downward. During an actual loss of engine power in the airplane 17 months before this accident, the pilot had feathered the incorrect propeller. Both a mechanic, and an FAA safety counselor, who were familiar with the pilot, described him as able to be disoriented, and reliant on GPS for navigation. He had stated five months before the accident that he did not feel his instrument flying skills were proficient, and desired training. On the day of the accident, weather was visual meteorological conditions, with layered clouds above 2,200 feet mean sea level. The pilot stated to the FAA weather briefer that he wanted to make the flight under visual conditions. The flight route and altitude was unknown.

Cause: Human factor

Occupants & Outcome

Crew On Board

1

Passengers On Board

1

Estimated Survivors

0

Fatality Rate

100.0%

Known people on board: 2

Operational Details

Schedule / Flight

Wrangell – Everett

Flight Type

Private

Flight Phase

Flight

Crash Site

Plain, Valley

Region / Country

North America • United States of America

Aircraft Details

Registration

N543AN

MSN

500-908-17

Year of Manufacture

1960