Cessna 441 Conquest
Safety Rating
9.8/10Total Incidents
42
Total Fatalities
99
Incident History
BCD Aviation
On February 7, 2021, about 1648 central standard time, a Cessna 441, N44776, was destroyed when it was involved in an accident near Belvidere, Tennessee. The airline transport pilot and a commercial pilot-rated passenger were fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight. According to preliminary radar and communications information obtained from the Federal Aviation Administration, the pilot took off from Thomasville Regional Airport (TVI), Thomasville, Georgia about 1527 with a destination of Winchester Municipal Airport (BGF), Winchester, Tennessee. As the airplane was descending to 4,000 ft mean sea level (msl), the pilot established contact with the Bowling Green, Kentucky radar controller. The flight was then cleared for the RNAV runway 36 approach. As the airplane descended through 2,300 ft, the radar target disappeared, which was normal due to the radar coverage in the area. About 3 minutes later, the controller attempted to contact the pilot with no response. There was no further communication with the pilot. Later that evening, the wreckage was found about 6 miles south of BGF. The wreckage path was about 500 ft in length, and oriented on a northerly heading. A large portion of the fuselage and both wings were consumed by a postimpact fire.
Bismarck Air Medical
The pilot and two medical crewmembers were repositioning the airplane to pick up a patient for aeromedical transport. Dark night instrument meteorological conditions prevailed for the flight. Radar data showed the airplane climb to 14,000 ft mean sea level after departure and proceed direct toward the destination airport before beginning a right descending turn. The airplane subsequently broke up inflight and impacted terrain. No distress calls were received from the pilot before the accident. Although weather conditions were conducive for inflight icing, no evidence of structural icing was identified at the scene. The debris field was 2,500 ft long and the disbursement of the wreckage confirmed that both wings, the horizontal stabilizer, both elevators, and both engines separated from the airplane before impacting the ground. Examination of the wreckage revealed that the initiating failure was the failure of the wing where it passed through the center of the airplane. The three wing spars exhibited S-bending deformation, indicative of positive overload producing compressive buckling and fracture. Further, impact signatures as black paint transfers and gouged aluminum, were consistent with the left outboard wing separating when it was struck by the right engine after the wing spars failed. There was no evidence of any pre-exiting conditions that would have degraded the strength of the airplane structure at the fracture locations. Flight control continuity was confirmed. An examination of the engines, propellers, and available systems showed no mechanical malfunctions or failure that could have contributed to the accident. The descending right turn was inconsistent with the intended flight track and ATC-provided clearance. However, there was insufficient information to determine how it was initiated and when the pilot became aware of the airplane's state in the dark night IMC conditions. Yet, the absence of a distress call or communication with ATC about the airplane's deviation suggests that the pilot was not initially aware of the change in state. The structural failure signatures on the airplane were indicative of the wings failing in positive overload, which was consistent with the pilot initiating a pullup maneuver that exceeded the airplane spars' structural integrity during an attempted recovery from the spiral dive.
Ponderosa Aviation
The airline transport pilot and two passengers departed in the twin-engine, pressurized airplane on a business flight in night instrument meteorological conditions. Shortly after takeoff, the airplane began to deviate from its assigned altitude and course. The controller queried the pilot, who responded that the airplane was "… a little out of control." After regaining control of the airplane, the pilot reported that he had experienced a "trim issue." The airplane continued on course and, about 13 minutes later, the pilot again reported a trim malfunction and said that he was having difficulty controlling the airplane. The flight's heading and altitude began to deviate from the course for the last 8 minutes of radar data and became more erratic for the last 2 minutes of radar data; radar and radio communication were subsequently lost at an altitude of about 18,300 ft in the vicinity of the accident site. Several witnesses reported hearing the airplane flying overhead. They all described the airplane as being very loud and that the engine sound was continuous up until they heard the impact. The airplane impacted a field in a relatively level attitude at high speed. The wreckage was significantly fragmented and the wreckage path extended about 1/4 mile over several fields. Examination of the available airframe and engine components revealed no anomalies that would have precluded normal operation of the airplane. The accident airplane was equipped with elevator, rudder, and aileron trim systems; however, not all components of the trim system and avionics were located or in a condition allowing examination. Although the airplane was equipped with an electric elevator trim and autopilot that could both be turned off in an emergency, the investigation could not determine which trim system the pilot was reportedly experiencing difficulties with. It is likely that the pilot was unable to maintain control of the airplane as he attempted to address the trim issues that he reported to air traffic control.
Rossair Charter
On 30 May 2017, a Cessna 441 Conquest II (Cessna 441), registered VH-XMJ (XMJ) and operated by AE Charter, trading as Rossair, departed Adelaide Airport, South Australia for a return flight via Renmark Airport, South Australia. On board the aircraft were: • an inductee pilot undergoing a proficiency check, flying from the front left control seat • the chief pilot conducting the proficiency check, and under assessment for the company training and checking role for Cessna 441 aircraft, seated in the front right control seat • a Civil Aviation Safety Authority flying operations inspector (FOI), observing and assessing the flight from the first passenger seat directly behind the left hand pilot seat. Each pilot was qualified to operate the aircraft. There were two purposes for the flight. The primary purpose was for the FOI to observe the chief pilot conducting an operational proficiency check (OPC), for the purposes of issuing him with a check pilot approval on the company’s Cessna 441 aircraft. The second purpose was for the inductee pilot, who had worked for Rossair previously, to complete an OPC as part of his return to line operations for the company. The three pilots reportedly started their pre-flight briefing at around 1300 Central Standard Time. There were two parts of the briefing – the FOI’s briefing to the chief pilot, and the chief pilot’s briefing to the inductee pilot. As the FOI was not occupying a control seat, he was monitoring and assessing the performance of the chief pilot in the conduct of the OPC. There were two distinct exercises listed for the flight (see the section titled Check flight sequences). Flight exercise 1 detailed that the inductee pilot was to conduct an instrument departure from Adelaide Airport, holding pattern and single engine RNAV2 approach, go around and landing at Renmark Airport. Flight exercise 2 included a normal take-off from Renmark Airport, simulated engine failure after take-off, and a two engine instrument approach on return to Adelaide. The aircraft departed from Adelaide at 1524, climbed to an altitude about 17,000 ft above mean sea level, and was cleared by air traffic control (ATC) to track to waypoint RENWB, which was the commencement of the Renmark runway 073 RNAV-Z GNSS approach. The pilot of XMJ was then cleared to descend, and notified ATC that they intended to carry out airwork in the Renmark area. The pilot further advised that they would call ATC again on the completion of the airwork, or at the latest by 1615. No further transmissions from XMJ were recorded on the area frequency and the aircraft left surveillance coverage as it descended towards waypoint RENWB. The common traffic advisory frequency used for air-to-air communications in the vicinity of Renmark Airport recorded several further transmissions from XMJ as the crew conducted practice holding patterns, and a practice runway 07 RNAV GNSS approach. Voice analysis confirmed that the inductee pilot made the radio transmissions, as expected for the check flight. At the completion of the approach, the aircraft circled for the opposite runway and landed on runway 25, before backtracking and lining up for departure. That sequence varied from the planned exercise in that no single-engine go-around was conducted prior to landing at Renmark. At 1614, the common traffic advisory frequency recorded a transmission from the pilot of XMJ stating that they would shortly depart Renmark using runway 25 to conduct further airwork in the circuit area of the runway. A witness at the airport reported that, prior to the take-off roll, the aircraft was briefly held stationary in the lined-up position with the engines operating at significant power. The take-off roll was described as normal however, and the witness looked away before the aircraft became airborne. The aircraft maintained the runway heading until reaching a height of between 300-400 ft above the ground (see the section titled Recorded flight data). At that point the aircraft began veering to the right of the extended runway centreline (Figures 1 and 15). The aircraft continued to climb to about 600 ft above the ground (700 ft altitude), and held this height for about 30 seconds, followed by a descent to about 500 ft (Figures 2 and 13). The information ceased 5 seconds later, which was about 60 seconds after take-off. A distress beacon broadcast was received by the Joint Rescue Coordination Centre and passed on to ATC at 1625. Following an air and ground search the aircraft was located by a ground party at 1856 about 4 km west of Renmark Airport. All on board were fatally injured and the aircraft was destroyed.
Legal Airways
The purpose of the flight was for the commercial pilot/owner to pick up passengers at the destination airport and return to the departure airport. The airplane was 33 miles from its destination in cruise flight at 3,300 ft mean sea level (msl) and above a solid cloud layer when the pilot declared to air traffic control (ATC) that he had the destination airport "in sight" and cancelled his instrument flight rules (IFR) clearance. During the 13 minutes after cancellation of the IFR clearance, the airplane's radar track made an erratic sequence of left, right, and 360° turns that moved the airplane away from the destination airport in a westerly direction. The altitudes varied between about 4,000 and 900 ft msl. Later, the pilot reestablished communication with ATC, reported he had lost visual contact with the airport, and requested an instrument approach to the destination airport. The controller then provided a sequence of heading and altitude assignments to vector the airplane onto the approach, but the pilot did not maintain these assignments, and the controller provided several corrections. The pilot expressed his inability to identify the initial approach fix (IAF) and asked the controller for the correct spelling. The radar target then climbed and subsequently entered a descending right turn at 2,500 ft msl and 180 knots ground speed near the IAF, before radar contact with the airplane was lost. Although a review of airplane maintenance records revealed that the airplane was overdue for several required inspections, examination of the wreckage revealed signatures consistent with both engines being at high power at impact, and no evidence of any preimpact mechanical anomalies were found that would have precluded normal operation. Examination of the airplane's panel-mounted GPS, which the pilot was using to navigate the flight, revealed that the navigation and obstruction databases were expired. During a weather briefing before the flight, the pilot was warned of low ceilings and visibility. The weather conditions reported near the destination airport about the time of the accident also included low ceilings and visibilities. The restricted visibility conditions and the high likelihood of inadvertent entry into instrument meteorological conditions were conducive to the development of spatial disorientation. The flight's erratic track, which included altitude and directional changes inconsistent with progress toward the airport, were likely the result of spatial disorientation. After reestablishing contact with ATC and being cleared to conduct an instrument approach to the destination, the airplane's flight track indicated that the pilot was not adequately prepared to execute the controller's instructions. The pilot's subsequent loss of control was likely the result of spatial disorientation due to his increased workload and operational distractions associated with his attempts to configure his navigation radios or reference charts. Postaccident toxicological testing of samples obtained from the pilot revealed the presence of ethanol; however, it could not be determined what percentage was ingested or produced postmortem. The testing also revealed the presence of amphetamine, an opioid painkiller, two sedating antihistamines, and marijuana. Although blood level quantification of these medications and drugs could not be made from the samples provided, their combined effects would have directly impacted the pilot's decision-making and ability to fly the airplane, even if each individual substance was only present in small amounts. Based in the reported weather conditions at the time the pilot reported the airport in sight and canceled his IFR clearance, he likely was not in a position to have seen the destination airport even though he may have been flying between cloud layers or may have momentarily observed the ground. His decision to cancel his IFR clearance so far from the destination, in an area characterized by widespread low ceilings and reduced visibility, increased the pilot's exposure to the hazards those conditions posed to the successful completion of his flight. The pilot showed other lapses in judgment associated with conducting this flight at the operational, aircraft, and the personal level. For example, 1) the pilot did not appear to recognize the significance of widespread low ceilings and visibility along his route of flight and at his destination (nor did he file an alternate airport even though conditions warranted); 2) the accident airplane was being operated beyond mandatory inspection intervals; and 3) toxicological testing showed the pilot had taken a combination of multiple medications and drugs that would have likely been impairing and contraindicated for the safe operation of an airplane. The pilot's decision-making was likely affected by the medications and drugs.
E-Med Rescue 24
On 15 August 2015 at 2351Z a Cessna 441 aeroplane, with two crew and a paramedic on board took off from Eros Airport (FYWE) on a medical evacuation flight with their intended final destination Cape Town International Airport (FACT). The aircraft landed at Oranjemund (FYOG) to pick up a male patient and his daughter. At 0206Z the aircraft departed from FYOG on a mercy flight to FACT. At 0343Z the aircraft made the first contact with FACT area and the aircraft was put under radar control. At 0355Z, area control advised the crew that there was a complete radar failure. The aircraft was on a descent to 6500 ft when approach advised them to prepare for a VOR approach for runway 19. At 0429Z, while on approach for landing at FACT, all contact was lost with the aircraft. At approximately 0556Z the aircraft’s wreckage was located approximately 8 nm to the north of FACT. All five occupants on board were fatally injured and the aircraft was destroyed by impact and post impact fire. The investigation revealed the aircraft collided with terrain during instrument meteorological condition (IMC) conditions while on the VOR approach for Runway 19 at FACT. At the time the ILS was working, however the approach controller offered a VOR approach for separation with an outbound aircraft as the radar was unserviceable.
Private Mexican
Crashed in unknown circumstances near Cañaote, State of Cojedes. The wreckage was found the following morning. The aircraft was destroyed, all three occupants were killed and a load of 999 kilos of cocaine was found among the debris.
Del Air Enterprises II
The instrument-rated commercial pilot was approaching the destination airport after a cross country flight in night instrument meteorological conditions. According to radar track data and air traffic control communications, while receiving radar vectors to the final approach course, the pilot did not always immediately comply with assigned headings and, on several occasions, allowed the airplane to descend below assigned altitudes. According to airplane performance calculations based on radar track and GPS data, the pilot made an engine power reduction about 2.5 minutes before the accident as he maneuvered toward the final approach fix. Following the engine power reduction, the airplane's airspeed decreased from 162 to 75 knots calibrated airspeed, and the angle of attack increased from 2.7° to 14°. About 4 miles from the final approach fix, the airplane descended below the specified minimum altitude for that segment of the instrument approach. The tower controller subsequently alerted the pilot of the airplane's low altitude, and the pilot replied that he would climb. At the time of the altitude alert, the airplane was 500 ft below the specified minimum altitude of 2,000 ft mean sea level. According to airplane performance calculations, 5 seconds after the tower controller told the pilot to check his altitude, the pilot made an abrupt elevator-up input that further decreased airspeed, and the airplane entered an aerodynamic stall. A witness saw the airplane abruptly transition from a straight-and-level flight attitude to a nose-down, steep left bank, vertical descent toward the ground, consistent with the stall. Additionally, a review of security camera footage established that the airplane had transitioned from a wings-level descent to a near vertical spiraling descent. A post accident examination of the airplane did not reveal any anomalies that would have precluded normal operation during the accident flight. Although the pilot had monocular vision following a childhood injury that resulted in very limited vision in his left eye, he had passed a medical flight test and received a Statement of Demonstrated Ability. The pilot had flown for several decades with monocular vision and, as such, his lack of binocular depth perception likely did not impede his ability to monitor the cockpit instrumentation during the accident flight. The pilot had recently purchased the airplane, and records indicated that he had obtained make and model specific training about 1 month before the accident and had flown the airplane about 10 hours before the accident flight. The pilot's instrument proficiency and night currency could not be determined from the available records; therefore, it could not be determined whether a lack of recent instrument or night experience contributed to the pilot's difficulty in maintaining control of the airplane.
Bil Mar Foods
After the pilot finished the preflight inspection in the hangar, the maintenance technician pulled the airplane out of the hangar and connected the auxiliary power cart to the airplane. Shortly thereafter, the pilot boarded the airplane and proceeded with the normal checklist. The pilot signaled to the maintenance technician to disconnect the power cart. The maintenance technician subsequently signaled that the pilot was clear to start the engines. After departure, the pilot noted a problem with the landing gear, and, after establishing that the tow bar was, most likely, still attached to the nosewheel, he diverted to a nearby airport for a precautionary landing. During the landing, the nose landing gear collapsed and the primary structure in the nose of the airplane was substantially damaged.
N48BS LLC
Toward the end of a 6 hour, 20 minute flight, during a night visual approach, the pilot flew the airplane to a left traffic pattern downwind leg. At some point, he lowered the landing gear and set the flaps to 30 degrees. He turned the airplane to a left base leg, and after doing so, was heard on the common traffic frequency stating that he had an "engine out." The airplane then passed through the final leg course, the pilot called "base to final," and the airplane commenced a right turn while maintaining altitude. The angle of bank was then observed to increase to where the airplane's wings became vertical, then inverted, and the airplane rolled into a near-vertical descent, hitting the ground upright in a right spin. Subsequent examination of the airplane and engines revealed that the right engine was not powered at impact, and the propeller from that engine was not in feather. No mechanical anomalies could be found with the engine that could have resulted in its failure. The right fuel tank was breeched; however, fuel calculations, confirmed by some fuel found in the right fuel tank as well as fuel found in the engine fuel filter housing, indicated that fuel exhaustion did not occur. Unknown is why the pilot did not continue through a left turn descent onto the final approach leg toward airport, which would also have been a turn toward the operating engine. The pilot had a communication device capable of voice calls, texting, e-mail and alarms, among other functions. E-mails were sent by the device until 0323, and an alarm sounded at 0920. It is unknown if or how much pilot fatigue might have influenced the outcome.
ProSoft Technology
The pilot was executing a day visual flight rules full-stop landing and touched down on the main landing gear near the approach end of the runway. Soon after the initial touchdown, the airplane became airborne again. Instead of initiating a go-around, the pilot attempted to continue the landing sequence. During that attempt, the airplane bounced on the runway three or four times, each time the rebound back into the air and the runway contact was more severe. During the last contact the airplane impacted the runway with sufficient force to result in the failure of the right main landing gear actuator rod, and in the right propeller contacting the runway surface multiple times. The pilot then initiated a go-around, but since the right engine had failed due to the multiple propeller strikes, the airplane produced asymmetrical thrust and began to roll to the right, veering off the right side of the runway. Soon thereafter its right wing collided with a tree and the airplane impacted terrain in an open field. The airplane was consumed by fire shortly after the collision. Post crash inspection found no evidence of mechanical failure or malfunction with the airframe or either engine.
Security Aviation
The airline transport pilot was landing a retractable landing gear-equipped turboprop airplane on a 10,900 foot long, by 150 foot wide paved runway. According to the pilot, while on approach to land, he selected 10 degrees of wing flaps, and then selected the landing gear selector switch to the down position, which was followed by "three greens", indicating the landing gear was down, locked, and safe for landing. He said that after touchdown, during the initial landing roll, the landing gear retracted, and the airplane slid on the underside of the fuselage. The airplane veered to the right of the runway centerline, and the right wing collided with numerous runway edge lights. A post crash fire ensued when the right wing's fuel tank was breached. The airplane received structural damage to the underside of the fuselage, and the right wing was destroyed. Propeller strike marks originated in the vicinity of the accident airplane's touchdown point, and extended to the airplane's final resting point, about 2,200 feet from initial contact. A postaccident inspection of the airplane by the IIC and another NTSB air safety investigator, disclosed no evidence of any pre accident mechanical malfunction of the landing gear assembly or its associated operating systems. The airplane was placed on jack stands and hydraulic pressure was supplied to the airplane's hydraulic system using a hydraulic ground power unit. The airplane's landing gear retraction system was cycled numerous times, with no mechanical anomalies noted.
NL Five
The airplane, flown by an airline transport pilot, departed in day visual meteorological conditions for an 18-nautical mile flight from the home base airport to another airport where the pilot planned to conduct a practice instrument approach. The pilot contacted approach control and requested a practice ILS approach. The controller instructed the pilot to proceed northwest bound and maintain 2,500 feet msl. Radar indicated the airplane tracked a northerly heading instead of a northwesterly heading as instructed. The airplane continued on a northerly heading until 1113:48 when it was about 5 miles southwest of the destination airport at 1,900 feet msl with a ground speed of 172 knots. At this point, the controller instructed the pilot to turn southbound and remain clear of Class C airspace. Radar coverage for the next 50 seconds was intermittent. At 1114:29, radar picked up the airplane about 4 miles southwest of the destination airport at 1,800 feet msl, a ground speed of 106 knots, and a heading of 101 degrees. The airplane continued heading east-southeast for about 30 seconds and its ground speed continued to decay. At 1114:58, it entered an abrupt descent, going from 1700 feet to 200 feet in 15 seconds. The last radar return was recorded at 1115:13 and showed the airplane at 200 feet msl, a ground speed of 64 knots, and a heading of 093 degrees. Several witnesses observed the airplane descend in a "flat spin" and impact a shallow canal in a residential area. Examination of the accident site revealed that the airplane impacted the canal in a nearly flat and level attitude. No evidence of any pre-impact mechanical discrepancies with the airframe or engines was found that would have prevented normal operation. Testing of the electronic engine controls revealed that both units were functional, but under some conditions would trip to manual mode. Further investigation determined that the units tripping to manual mode was due to an electrical overstress that failed the same thermistor within each unit. The reason for the electrical overstress or when it occurred could not be determined; however, it is probable it occurred at impact when the units were submerged in water. Even if the units tripped to manual mode in flight, this would only result in the loss of the torque and temperature limiting and propeller synchrophaser systems, meaning the pilot would have to manually adjust the power levers as required to maintain the proper torque and exhaust gas temperature. Post accident toxicology testing of the pilot's blood revealed chlorpheniramine, an over-the-counter sedating antihistamine, at more than ten times higher than the level expected with a typical maximum over-the-counter dose. It is probable that the pilot's performance and judgment were substantially impaired by his very high blood level of chlorpheniramine.
Chrysalis 1
Impact forces and fire destroyed the airplane when it impacted the terrain after a loss of control during cruise flight. The pilot received a weather brief by AFSS prior to departure concerning the IFR conditions along the route of flight, which included, rain, freezing rain, icing, turbulence, and snow. The cloud tops were forecast to be 25,000 feet. The pilot filed a flight plan with a cruise flight level of 28,000 feet. About 32 minutes after takeoff, at 1345:58, the pilot reported he had an attitude gyro problem and that he was hand flying the airplane. The airplane's altitude remained at about 28,000 feet for the next seven minutes. At 1352:46, the pilot stated he had an emergency, but at 1352:53, the pilot stated, "Uh it came back on never mind." At 1353:26, the pilot stated, "I need to get to uh anywhere I can get a visual." At 1353:56, the airplane was cleared to climb to 31,000 feet, and radar data indicated the airplane was currently at 27,000 feet. The radar data indicated the airplane went into a series of steep descents and climbs over the next 4.5 minutes until radar contact was lost at 2,500 feet. The pilot of a commercial airline who was flying in the same sector as the accident airplane reported that he heard the accident pilot state that he was in a spin. The commercial airline pilot stated they were flying at 33,000 feet and were "barely above the tops" of the clouds. The airplane impacted the terrain in a steep nose down attitude and burst into flames. The engines, flight controls, and flight instruments did not exhibit any pre-existing anomalies. A witness reported that two days prior to the accident, the pilot had advised him that the airplane's attitude gyro was having problems. There was no record that the pilot had the attitude gyro inspected prior to the accident. A witness reported the pilot routinely flew with the autopilot engaged soon after takeoff. He reported that he had never observed the pilot hand-fly the airplane in instrument conditions.
Alexander Leasing
The pilot was on a visual rules flight from Culebra, Puerto Rico to San Juan, Puerto Rico. No flight plan was filed and a weather briefing was not obtained. The pilot contacted San Juan Radar Approach Control 10 miles east of Fajardo, Puerto Rico and the controller stated the airplane was in radar contact 3 miles east of Fajardo airport. The pilot was instructed to enter a right downwind for runway 10 south of plaza Carolina. The pilot acknowledged the transmission and reported he was at 1,600 feet. Two minutes later the controller stated on the radio frequency, radar contact was lost. The airplane was located by ground personnel on the side of El Yunque Mountain. Review of weather data revealed a weak cold front extended over Puerto Rico. Satellite imagery at the time of the accident revealed a band of low clouds obscuring the accident site. A police helicopter pilot who attempted to reach the crash site reported instrument flight conditions. Examination of the airframe, flight controls, engine assemblies and accessories revealed no anomalies.
Lufttaxi Flug
The crew (one instructor and one pilot under training) departed Dortmund-Wickede Airport for a training mission. At an altitude of 3,200 feet, while completing stall exercises, the crew lost control of the airplane that crashed in a flat attitude in a sandy field located near Ascheberg, bursting into flames. Both occupants were killed.
Executive Wings
During the takeoff roll the pilot stated the right engine had an over torque condition and he was unable to control the aircraft. The aircraft went off the runway to the left and crashed coming to rest upright. A post crash fire erupted and destroyed the aircraft. The mechanic rated passenger stated he was observing the right engine gauges during this maintenance test flight and did not observe any over torque indications. When he looked up from the instruments at about the time the aircraft should lift off, the aircraft was drifting to the left. The pilot, who was looking at the engine instruments, looked up, saw the aircraft was about to drift off the runway, and retarded both power levers. The passenger/mechanic (who was also a pilot) reported that the pilot placed the propellers in reverse. Six thousand feet of runway remained at the abort point. The aircraft pitched up and then crashed on the left wing and nose. Cessna Service Newsletter SLN99-15 and AlliedSignal Operating Information Letter OI 331-17 report an abnormality that may affect the model engine in which an uncommanded engine fuel flow increase or fluctuation may occur, resulting in an unexpected high torque and asymmetric thrust. The condition is associated with an open torque motor circuit within the engine fuel control. A system malfunction resulting in engine acceleration to maximum power would produce an overtorque of about 2,288 foot-pounds (ft-lb). This power output is restricted by a fuel flow stop in the engine fuel control. Normal takeoff power is 1,669 ft-lbs; therefore, one engine accelerating to the stop limit while one engine continued to operate normally would cause a torque differential of 619 ft-lbs. The total loss of power in one engine during takeoff while one engine continued to operate normally would result in a torque differential of 1,669 ft-lbs. The Cessna 441 Flight Manual states that at 91 knots indicated airspeed, the airplane is controllable with one engine inoperative (that is, with a torque differential between engines of up to 1,669 ft-lbs). However, if an electronic engine control failure occurs on one engine and the other engine is retarded to idle, the fuel flow to the failed engine will not be reduced, and a torque differential of about 2,288 ft-lbs will occur, at which point the airplane is uncontrollable by the pilot.
Warrington Development Corporation
On April 20, 1996, about 1215 Atlantic standard time, N441W, a Cessna 441, crashed on landing in Walkers Cay, Bahamas, while on a 14 CFR Part 91 personal flight. Visual meteorological conditions prevailed at the time and a VFR flight plan had been filed. The airplane was substantially damaged and the private pilot and three passengers reported no injuries. The flight originated from Destin, Florida, about 2 hours 30 minutes earlier. The pilot stated that on final approach he landed short of the runway. The main landing gear sheared off the airplane and the nose gear collapsed.
Superior Aviation
During the takeoff roll on runway 30R, the MD-82, N954U, collided with the Cessna 441, N441KM, which was positioned on the runway waiting for takeoff clearance. The pilot of the Cessna acted on an apparently preconceived idea that he would use his arrival runway, runway 30R, for departure. After receiving taxi clearance to back-taxi into position and hold on runway 31, the pilot taxied into a position at an intersection on runway 30R, which was the assigned departure runway for the MD-82. The ATIS current at the time the Cessna pilot was operating in the Lambert-St. Louis area listed runways 30R and 30L as the active runways for arrivals and departures; there was no mention of the occasional use of runway 31. Air traffic control personnel were not able to maintain visual contact with the Cessna after it taxied from the well lighted ramp area into the runway/taxiway environment of the northeast portion of the airport. An operational ASDE-3, particularly ASDE-3 enhanced with AMASS, could be used to supplement visual scan of the northeast portion of the airport.
G. G. Trucking
The pilot of the Cessna 441 Conquest was conducting an international charter flight from General Mitchell International Airport in Milwaukee, Wisconsin, to Gods Lake Narrows, Manitoba. The pilot landed the aircraft at Fort Frances, Ontario, to clear customs and refuel, and then continued his visual flight rules (VFR) flight to Gods Lake Narrows. During the take-off at Fort Frances, the aircraft experienced a power loss in the left engine. The pilot elected to continue the take-off but was unable to control the aircraft after it became airborne. The aircraft veered to the left and crashed on the airfield. The accident occurred at 0425 central daylight time (CDT), at night, on the Fort Frances Municipal Airport. All seven occupants sustained minor injuries and the aircraft was damaged beyond repair.
Air Travel Services
The pilot reported that immediately after takeoff, he had a collision with a flight of birds. He stated that the right engine immediately had a partial loss of power. He stated that he did not attempt to raise the landing gear nor the flaps following the loss of engine power, and the aircraft would not maintain altitude. Examination of the aircraft engines revealed that there was rotational scratching of the turbine housings on the right engine, and no rotational scratching on the turbine housing of the left engine.
Tahiti Conquest Airlines
The twin engine aircraft departed Papeete-Faaa Airport on an ambulance flight to Maupiti, carrying two doctors and one pilot. After takeoff, while climbing by night, the pilot informed ATC about minor problems with the engine but preferred to return for a safe landing. On final approach, the aircraft went out of control and crashed in the sea few km from the airport. All three occupants were killed. At the time of the accident, it was dark but weather conditions were excellent.
Nuna Air
The twin engine aircraft departed Sondreströmfjord on a charter flight to Goose Bay, carrying six sailors and two pilots. Seventeen minutes after takeoff, while cruising at FL220, the aircraft entered an uncontrolled descent and the crew did not send any distress call. At an altitude of 7,000 feet, the aircraft disintegrated and debris scattered on a wide area. The wreckage was found about 148 southwest of Sondreströmfjord and all eight occupants were killed.
JC Air
Shortly after takeoff from Toussus-le-Noble Airport runway 07L, while climbing in limited visibility due to fog, the twin engine aircraft initiated a right turn when control was lost. It nosed down and eventually crashed in an open field located in Saclay, about 5 km southeast of the airport. The aircraft disintegrated on impact and all seven occupants were killed. At the time of the accident, the visibility was poor due to thick fog. For unknown reasons, the pilot initiated a right turn after takeoff while departure procedures define a straight in climb. Five of the six passengers were automobile journalists flying to Montluçon where they were supposed to visit the Dunlop facilities and perform drive tests on the last BMW M3. The sixth passenger was a marketing Director by a BMW dealer who chartered the aircraft. Crew: Daniel Douzard. Passengers: François-Xavier Beaudet, Denis Charpentier, Raymond Bochet, Geoffroy Lemaignen, Marc Duick, Jean-Claude Depincé.
United States Government
A Cessna 441 operated by the US Customs Services collided with terrain while on an authorized night tactical flight. The copilot did not meet the currency standards as required by USCS and was not qualified in the aircraft. The flight originated during the daylight hours and continued to astronomical twilight. The pilots did not dark adapt previous to the night conditions. Dark adaption was impeded by flight through various light conditions created by terrain and ambient light levels. With night vision impeded the pilot would not have been able to distinguish relief of the terrain. The acft collided with a small ridge that abruptly rose 300 feet. Both occupants were killed.
Africair
Crashed in unknown circumstances about 10 km from Maiduguri Airport. All four occupants were injured.
Brown Air Services
The accident occurred at Blackbushe airfield following a go-around from an approach to land on runway 26. The aircraft appeared to begin the go-around normally but was then seen to bank to the left and start turning left. The turn continued through 135° of heading, at a low height, with the bank angle increasing progressively, until the aircraft crashed into trees, semi-inverted, approximately 550 meters from the runway 26 threshold. The reason for the initiation of the go-around was an unsafe main landing gear indication caused by a defective microswitch. The reasons for the subsequent loss of control could not be determined.
Samaritan AirEvac - Samaritan Health Services
The aircraft was on an emergency medical service (ems/medevac) flight with a pilot and a flight nurse aboard to transport a maternity patient from Flagstaff to Phoenix. During a night arrival, the pilot began a VOR-A approach in IMC, then he reported a problem with his avionics and elected to make a missed approach. During the missed approach, he said that he 'lost' an inverter, then reported the gyros were inoperative. Radar vectors were being provided when he stated 'we have big trouble here.' Soon thereafter, radar and radio contacts were lost and the aircraft crashed approximately 7 miles southeast of the airport. During impact, the aircraft made a deep crater and was demolished. No preimpact engine or airframe failure was found. An investigation revealed the #2 (copilot's) attitude indicator was inoperative on the previous flight. A discrepancy report was taken to the avionics department, but the requested entry was not made in the aircraft form-4. The pilot took off before corrective action was taken. The operations manual requested 1,000 hours multi-engine time as pic and training by esignated cfi's. The pilot had approximately 837 hours multi-engine time, recorded 9 training flights in N6858S with non-designated instructors, completed a part 135 flight check on 2/17/88. Both occupants were killed.
Gary Miller Leasing
Reason for the Cessna to veer in a semi-circle and collide with another aircraft is undetermined. Examination of the start lock assemblies could not be completed due to the extensive impact and fire damage. The aircraft was being prepared for a flight. During a manual speed governor check on the left engine the aircraft veered in a semi-circle. An attempt to examine the aircraft start locks was negated by the fire damage from the collision. Both occupants escaped uninjured.
OSG Tap %26 Dies
The pilot (a part time employee of the owner) was ferrying the aircraft for maintenance. Witnesses, who saw the pilot before take- off, noted that his speech was slurred and that he seemed angry because a tug would not start. One witness characterized him as being 'very mad' and said his face was 'flushed red.' The aircraft was observed to takeoff in a high nose-up attitude and climb about 500 to 1,000 feet before turning to the southwest and leveling. Subsequently, the plane turned back toward the airport, then it crashed and burned approximately 1-1/2 mile ssw of the airport while on a heading of northeast. Impact occurred while the aircraft was descending in a slightly left wing low attitude. The wreckage was scattered over an area that was approximately 600 feet long and about 45 feet wide at the widest point. According to witnesses, the engines were operating normally when the aircraft crashed. No preimpact mechanical problem was found. A toxicology check of the pilot's liver tissue fluid showed an alcohol level of 2,26‰. The pilot, sole on board, was killed.
Denver Air Center
On 5/1/86, the pilot had an acoustic tumor removed from his right ear which included the removal of the 8th nerve (balance nerve). His attending physician suggested approximately 1 year period of recuperation due to equilibrium problems associated with this type of surgery. On 7/12/86, he had a 1st class medical exam and received a medical certificate which was valid for flight test only. On 8/28/86, while taking off at night, the aircraft collided with rising terrain approximately 1.5 mile from the end of the runway at an elevation of about 5,600 feet. The airport elevation was 5,586 feet. A witness stated that he saw the aircraft takeoff, but it did not climb after takeoff. An investigation revealed that the accident occurred in an area that was isolated from ground lights. A post crash examination revealed no evidence of a mechanical failure or malfunction of the aircraft structure, flight controls, engine or propellers. According to the pilot's log book, his last night flight was on 3/22/85. He had been on duty for approximately 14 hours when the accident occurred. All seven occupants were killed.
Norving
In unknown circumstances, the twin engine airplane overran, lost its nose gear and came to rest. There were no casualties while the aircraft was damaged beyond repair.
Health Care %26 Retirement Corporation
N6857E was transporting executives from Holland, MI, to Muskegon. The pilot was executing an ASR approach to runway 06. The MDA is 537 feet agl. Copilot called out 1,200 feet then below 1,000 feet, pilot continued approach. Aircraft struck trees two miles from runway at 15 feet agl. The approach was conducted in heavy fog conditions. The pilot had descended below approach minimums on several occasions in the past. A pilot and two passengers were killed while three other occupants were seriously injured.
Colonial Oil Industries
During final approach the pilot noticed aircraft flying 'unusual' and elected go-around. During power-up, the aircraft lost power and a forced landing was made on a residential street near the airport. The pilot stated that he had inadvertently placed the fuel selector in crossfeed and had exhausted the fuel supply in the right wing by feeding both engines. There were no reported mechanical problems prior to the accident.
Hy Flight Associates
During arrival, the pilot was advised the destination weather was: estimated 500 feet overcast, visibility one mile with fog, airport below minimums. The pilot elected to make an NDB runway 23 approach, but said he would divert if a missed approach was made. He was provided radar vectors and was cleared for the approach. At the IAF (initial apch fix/tiney intersection), radar service was terminated and the pilot was told to contact tower. On tower frequency, the pilot was again reminded the airport was below minimums. Approximately two minutes later, he reported over the outer marker (OM) which was 4.2 miles past (southwest of) the NSB/final approach fix (FAF) and 3.9 miles northeast of the airport. Seconds later, the tower transmitted info (just recorded from ARTCC) that the aircraft was 2-1/2 mi east of course. Tower tried to notify the pilot, but radio and radar contact were lost. Investigations revealed the aircraft impacted a ridge nearly 4 miles past the NDB and two miles left of course at an elevation of approximately 1,900 feet, but before passing the OM. Minimum descent altitude (MDA) between the NDB and OM was 2,220 feet msl. MDA after passing the OM was 1,940 feet; airport elevation was 1,161 feet. No preimpact aircraft problems were found. The NDB facility operated satisfactorily during flight and ground checks. All five occupants were killed.
Rosewood Enterprises
A student pilot in a Cessna 152, N5522L, had departed Redbird Airport at Dallas. He was practicing solo maneuvers in a privately designated practice area that overlapped the extended inbound course to runway 31L and 31R at Love Field. At the same time, a Cessna 441, N400BG, was being vectored for a back course ILS to rwy 31R. DFW approach control cleared N400BG to continue descending to 3,000 feet and fly heading 290°. While N400BG was descending thru approximately 3,600 feet, about 14 miles southeast of Love Field, the two aircraft collided. The Cessna 152 pilot was maneuvering at or near the edge of the practice area when the collision occurred. An investigation revealed the Cessna 152 had just completed an approximately 180° turn toward an easterly heading. Both aircraft were demolished in a quartering head-on collision. Radar info from both aircraft was displayed on the controller's scope. The Cessna 152 was depicted as a 1200 beacon code; however, it was not equipped with a mode C (altitude reporting) transponder. The controller did not provide a traffic advisory for the Cessna 441 pilot; but, in this situation, an advisory was not mandatory. All five pilot on both aircraft were killed.
Clinton Manges Oil %26 Refining Company
The aircraft crashed approximately 1.5 miles south of the departure end of runway 17 during an attempted runway 17 NDB approach. The aircraft was cleared for the approach at 2012 cst and the pilot canceled IFR reporting the airport in sight at 2014. A witness located approximately 1 mile south of the airport reported seeing the aircraft lights through the clouds, mist and fog as it was traveling south-southeast. The aircraft impacted the ground on a heading of 035° in a 10° to 15° left bank. Radar data indicates the aircraft was approximately 8 miles from the airport when IFR was canceled. Witnesses stated visibility in the area was about 1/8 of a mile during the time of the accident. The pilot, sole on board, was killed.
Private German
Crashed in unknown circumstances in a mountainous area located near Viigiú. The pilot, sole on board, was killed.
Montana Power Company
On approach to Butte-Bert Mooney Airport, the pilot encountered poor weather conditions and decided to initiate a go-around and to divert to another airport. At low height, the twin engine airplane struck a hill and crashed 11 miles south of the airport. Both occupants were killed.
Nichols Construction
After takeoff from Shreveport, the twin engine airplane climbed to its assigned altitude when the pilot obtained the permission to modify his route to avoid a storm. Then the aircraft flew to the east and climbed to the excessive altitude of 41,600 feet (some 6,600 feet above the maximum certified altitude for the aircraft) and the radio contact was lost with the pilot. An Air National Guard Convair F-106 Delta Dart fighter aircraft was dispatched and its pilot confirmed that both occupants seems to be unconscious. After few minutes, both engines stopped due to lack of fuel and the airplane entered a spin and eventually crashed in the Atlantic Ocean about 100 miles east of Norfolk, Virginia. Few debris were found floating on water but the main wreckage was never found as well as both occupants, the pilot Louis Benscotter and the football and baseball coach Robert Edward 'Bo' Rein aged 34.
Cessna Aircraft Company
The twin engine airplane departed Birmingham with one pilot and six potential customers on board for a demonstration flight to Mobile. While in normal cruise, the airplane suffered a complete in-flight breakup, dove into the ground and crashed near Demopolis. The aircraft was totally destroyed and all seven occupants were killed.
Safety Profile
Reliability
Reliable
This rating is based on historical incident data and may not reflect current operational safety.
