Grand Aire Express - Executive Aire Express

Safety profile and incident history for Grand Aire Express - Executive Aire Express.

Safety Score

9.9/10

Total Incidents

7

Total Fatalities

6

Recent Incidents

November 30, 2004 2 Fatalities

MBB HFB-320 Hansa Jet

Chesterfield-Spirit of St Louis Missouri

The Hansa 320, a corporate turbojet airplane departed runway 26L at night on a maintenance ferry flight at 1954 central standard time, and was destroyed when it impacted a river two miles west of the departure airport. Radar track data indicated that the airplane climbed to about 900 feet msl at about 180 knots before it began losing altitude and impacted the river. The current weather was: winds 270 degrees at 13 knots gusting to 19 knots, visibility 7 miles, light rain, 1,000 feet scattered ceiling, 1,800 feet broken, 2,400 feet overcast, temperature 2 degrees Celsius (C), dew point 2 degrees C, altimeter 29.90. The FAA had issued the pilot a Special Flight Permit for the flight. The limitations listed in the flight permit included the following limitations: Limitation number 6 stipulated, "IFR in VMC conditions approved, provided all equipment required for IFR flight is operational and certified iaw 14 CFR Part 91.413. If this equipment is NOT certified and operational, then VFR in VMC conditions ONLY." The ferry permit listed, "Additional Limitations: Engine power assurance runs, compass swing, and functional check of avionics equipment must be performed, and appropriate maintenance entries in the aircraft log prior to departure." The pilot was informed that none of the additional limitations had been performed prior to takeoff. The pilot had aborted a previous takeoff at about 1830 due to no airspeed indications. At the request of the pilot, maintenance personnel disconnected the lines to the pitot tubes and blew out the tubes, but no leak check, as required by FAR 91.411, was performed prior to the accident flight. The pilot performed a high-speed taxi to test the airspeed indicators prior to takeoff. The copilot did not have any ground school or flight time in a Hansa 320. The second-in-command requirements stated in FAR 61.55 9 (f) (1), required that the flight be conducted under day VFR or day IFR. The Toxicology report for the pilot indicated that 0.106 (ug/ml, ug/g) Diphenhydramine was detected in the blood. Diphenhydramine is an antihistamine commonly used in over-the-counter cold/allergy preparations. In therapeutic doses, the medication commonly results in drowsiness, and has measurable effects on performance of complex cognitive and motor tasks (e.g. flying an aircraft). The pilot's currency in the Hansa 320 expired on November 30, 2004, the day of the accident. He would be required to have an FAA checkride in a Hansa 320 to be a pilot-in-command (PIC) after November 30th. Engine teardown inspections revealed that both engines were developing power at the time of impact. The inspection of the elevator trim system revealed that the elevator trim cables were improperly installed when they were replaced to comply with an Airworthiness Directive (AD) 224-01-11. The maintenance manager who inspected the installation of the elevator trim cables did not perform an operational check of the elevator trim tabs. The maintenance manager signed the aircraft log stating the "Aircraft is approved for one time ferry flight from SUS to TOL," although all stipulations of the ferry permit had not been met, and that a leak check of the pitot-static system had not been performed after the pitot tubes had been blown out.

Dassault Falcon 20

Saint Louis-Lambert Missouri

The twin engine turbofan powered airplane was ditched into a river after a complete loss of power from both engines. The airplane was on a second approach to land on runway 30R after having been instructed by air traffic control (ATC) to climb during the final approach segment of the first approach due to inadequate separation from another airplane. Subsequent to the first approach, the airplane was issued vectors for the second approach by ATC. Communications transcripts show that the flight crew asked ATC how far they would be vectored during the second approach, but the flight crew did not inform ATC of their low fuel state until the airplane was already on a "base turn...to join final." The airplane subsequently lost power from both engines. During interviews, both pilots stated that there were no problems with the airplane. The second-in-command (SIC) stated that the airplane "ran out of fuel" and that the fuel quantity indicators read 0 and 100 pounds when each respective engine stopped producing power. The SIC also stated that after being instructed to climb to 5,000 feet after their first approach, he questioned the pilot-in-command about landing at another airport located about 14 nautical miles west-southwest of the destination airport. The SIC said that the PIC elected to continue with the second approach to the original destination. Research indicated that the flight crew did not obtain a weather briefing prior to the accident flight. Additionally, the Terminal Aerodrome Forecast that was valid at the time the aircraft's flight plan was filed showed a forecast ceiling consisting of overcast clouds at 1,500 feet above ground level at the aircraft's arrival time at the destination. 14 CFR Part 91.169 requires that an alternate airport be listed in the flight plan when forecast ceilings are less than 2,000 feet. No alternate was listed in the flight plan for the accident flight. Additionally, 14 CFR Part 91.167 requires that aircraft operated in instrument meteorological conditions maintain fuel reserves that allow flight to the intended destination and then continued flight to the listed alternate, and an additional 45 minutes at normal cruise speed. In 1993, the FAA/industry advisory committee developed advisory material for fuel planning and management for 14 CFR Part 121 and 135 air carrier flight operations, but the material was never published.

April 8, 2003 3 Fatalities

Dassault Falcon 20

Toledo-Express Ohio

The flight crew of the Fan Jet Falcon (DA-20) were practicing ILS approaches in instrument meteorological conditions with low clouds and rime ice. A first officer (FO) in training occupied the right seat, while the pilot-in-command (PIC), who was also the company chief pilot/check airman/designated flight instructor, occupied the left seat and was handling the radios. On the second approach, the airplane struck trees and burned, 1.57 nm from approach end of the runway. The landing gear was found extended, and the trailing edge and droop leading edge flaps were retracted. The wing and engine cowl anti-ice valves were found closed, consistent with it being off in the cockpit. Radar data revealed that on approach, the airspeed decreased from 188 knots to 141 knots at the outer marker, and continued to decrease down to 106 knots, when the airplane entered an abrupt descent and disappeared from radar. Simulator flights matched the radar profile with a flight idle approach, a power reduction inside the outer marker, and 1/4 inch of ice on the wings. In the simulator, the airplane stalled about 2 miles from the end of the runway with an airspeed of 103 kts. At flight idle, the engine power in the last 2 minutes of approach was below the recommended power setting for wing or engine anti-ice to be effective. Vref and stall speeds were computed to be 129 kts and 96 kts, with wing flaps and droop leading edges retracted. The PIC had about 1,100 hours in the make and model. The PIC did not have any documented previous flight instruction experience in make and model or any other multi-engine airplanes. The PIC had given 4 pilot proficiency checks in the DA-20 since receiving his check airman designation. The company Director of Operations reported that the accident FO was the first student the PIC had taken through the initial second-in-command course. The PIC and FO had received all of their turbojet experience with the operator.

July 18, 2002 1 Fatalities

Piper PA-60 Aerostar (Ted Smith 600)

Columbus-Municipal (Bakalar) Indiana

The airplane was destroyed by impact forces and fire after it impacted the intersection of runway 23 and 32 while attempting a missed-approach. The pilot's crew day started at 1300 and the 14 hour duty limit was 0300 the following morning. The second leg of the flight was delayed 1 hour and 36 minutes due to a freight delay. The operator reported the pilot exceeded his 14 hour crew day by 45 minutes as a result of the freight delay. The flight was cleared for the runway 23 ILS instrument approach. A witness, who was monitoring the Unicom radio frequency, reported that he heard clicking sounds on the Unicom frequency (to bring up the runway light intensity), but the pilot did not make any radio transmissions. The witness reported the ground fog was very thick. Two witnesses reported they heard the airplane's engines. They then heard the engines go to "full power," and then they heard the airplane impact the ground. They saw an initial flash, but could not see the airplane on fire from 2,500 feet away. FAR 135.213 requires that, "Weather observations made and furnished to pilots to conduct IFR operations at an airport must be made at the airport where those IFR operations are conducted." The destination did not have authorized weather reporting, and the operator's Operating Specifications did not list an alternate weather reporting source. At 0253, the observed weather 20 miles to the north, indicated the following: winds 190 at 4 knots, 1/4 statute mile visibility, fog, indefinite ceilings 100 feet, temperature 22 degrees C, dew point 22 degrees C, altimeter 30.00. From the initial point of impact (POI), the wreckage path continued for about 210 feet on a heading of about 180 degrees. The outboard section of the left wing outboard of the nacelle was found on runway 32, about 85 feet from the POI. Separated, unburned, portions of the left aileron and left flap were also found on the runway. The remaining pieces of the left wing were located with the main wreckage. The right wing was located with the main wreckage and the entire span of the right wing from the wing root to the wingtip exhibited continuity. The inspection of the airplane revealed no preexisting anomalies.

Dassault Falcon 20

Detroit-City (Coleman A. Young) Michigan

The airplane sustained substantial damage on impact with terrain and objects after traveling off the end of the runway during a main wheels up landing. The captain reported that prior to takeoff, he closed the cargo door and the copilot confirmed the door light was out. After takeoff at an altitude of about 600 feet, the cockpit door popped open and the crew noticed the cargo door was open. The captain elected to return to land. The captain reported he requested repeatedly for gear and flaps extension, but the copilot was late in doing so and it "caused us to overshoot the runway centerline." The copilot then began calling for a go around/missed approach at which time he raised the gear and the retracted some of the flaps. The copilot reported the captain continued to descend toward the runway and overshot the runway centerline to the right. The copilot reported that at this time he lowered the gear. The nose gear extended prior to touchdown, however the main gear did not. The airplane touched down approximately 1/2 way down the runway and traveled off the end. A witness reported noticing that the exterior door latch was not down as the airplane taxied to the runway.

Dassault Falcon 20

Peterborough Ontario

The Dassault-Breguet Falcon 20E aircraft was on an unscheduled charter cargo flight from Detroit Willow Run, Michigan, USA, to Peterborough, Ontario. The flight was being conducted at night and under instrument flight rules in instrument meteorological conditions. Nearing the destination, the flight crew received a clearance to conduct a non-directional beacon runway 09 approach at Peterborough Airport. The flight crew did not acquire the runway environment during this approach and conducted a missed approach procedure. They obtained another clearance for the same approach from Toronto Area Control Centre. During this approach, the flight crew acquired the runway environment and manoeuvred the aircraft for landing on runway 09. The aircraft touched down near the runway midpoint, and the captain, who was the pilot flying, elected to abort the landing. The captain then conducted a left visual circuit to attempt another landing. As the aircraft was turning onto the final leg, the approach became unstabilized, and the flight crew elected to overshoot; however, the aircraft pitched nose-down, banked left, and struck terrain. As it travelled 400 feet through a ploughed farm field, the aircraft struck a tree line and came to rest about 2000 feet before the threshold of runway 09, facing the opposite direction. The aircraft was substantially damaged. No serious injuries occurred.

Piper PA-61 Aerostar (Ted Smith 601)

Mount Storm West Virginia

The pilot stated that the airplane was in cruise flight at 8,000 feet MSL, when the right engine lost power. He advised ATC of the loss of power and received radar vectors toward an airport. The pilot said he maintained the best single-engine rate-of-climb speed, but the airplane's altitude 'drifted down.' When the airplane entered clouds, it began to accumulate structural icing and would not maintain sufficient altitude. The airplane impacted mountainous terrain about 16 miles northwest of the airport. The pilot stated that he had departed on the cargo flight with 5 hours of fuel on board for what he estimated to be a 2 1/2 hour flight. Also, he reported that conditions were dark and foggy, when the accident occurred. Postaccident examination of the engines and their systems revealed no evidence of preimpact mechanical malfunction. Examination of the airplane wreckage revealed no evidence of preimpact failure of the airframe or its systems. During a postaccident engine test run, the right engine started normally and operated satisfactorily.

Airline Information

Country of Origin

United States of America

Risk Level

Low Risk

Common Aircraft in Incidents

Dassault Falcon 204
Piper PA-61 Aerostar (Ted Smith 601)1
Piper PA-60 Aerostar (Ted Smith 600)1
MBB HFB-320 Hansa Jet1