Dassault Falcon 20

Historical safety data and incident record for the Dassault Falcon 20 aircraft.

Safety Rating

9.8/10

Total Incidents

46

Total Fatalities

73

Incident History

October 5, 2021 2 Fatalities

Career Aviation

Thomson-McDuffie County Georgia

On October 5, 2021, at 0544 eastern daylight time, a Dassault Fanjet Falcon airplane, N283SA, was destroyed when it was involved in an accident near the Thomson-McDuffie County Airport (HQU), Thomson, Georgia. The captain and first officer were fatally injured. The airplane was operated as Pak West Airlines Flight 887 dba Sierra West Airlines, as an on-demand cargo flight under the provisions of Title 14 Code of Federal Regulations Part 135. According to operator records, the flight crew initiated the first flight of the night at 2132 mountain daylight time from their home base of El Paso International Airport (ELP), El Paso, Texas to Lubbock Preston Smith International Airport (LBB), Lubbock, Texas. After about a 2 hour and 20-minute ground delay waiting for the freight, the accident flight was initiated from LBB to HQU. Review of preliminary air traffic control communications provided by the Federal Aviation Administration (FAA) revealed that the flight was in contact with the Atlanta Air Route Traffic Control Center (ATL center) for about the final 40 minutes of the flight. At 0503 eastern daylight time, Pak West Flight 887 (PKW887) requested information about the Notices to Airman (NOTAMs) for the instrument landing system (ILS) localizer runway 10 instrument approach procedure at HQU. ATL Center informed the flight crew of two NOTAMs; the first pertained to the ILS runway 10 glidepath being unserviceable and the second applied to the localizer being unserviceable. The controller informed the flight crew that the localizer NOTAM was not in effect until later in the morning after their expected arrival, which was consistent with the published NOTAM. About 0525, ATL center asked PKW887 which approach they would like, to which they responded with the “ILS runway one zero approach.” The controller responded, “roger, standby for that.” At 0526, ATL center cleared PKW887 to CEDAR intersection which was the initial approach fix for the ILS or localizer/non-directional beacon (NDB) runway 10 approach. About 0537, ATL center informed PKW887 that they were 15 miles southwest from CEDAR and “cross CEDAR at or above 3,000 cleared ILS localizer one zero into Thomson McDuffie.” PKW887 readback the clearance and the controller stated it was a “good readback”, however, the controller informed the flight crew that they were transmitting on the “guard” emergency frequency of 121.5, rather than the center frequency. About 1 minute later, the controller advised PKW887 of a telephone number to call to cancel their instrument flight rules (IFR) clearance once on the ground; however, about 0543, PKW887 had just crossed CEDAR and requested to cancel their IFR clearance. The controller advised PKW887 to “squawk vfr” and no further communications were received. Surveillance video located at HQU showed that about 0539 the airport and runway lights were activated from off to on. About 0542 the airplane’s landing lights came into view in the pitchblack horizon and were subsequently visible for about 2 minutes. The video showed the airplane approaching runway 10 in a relatively constant descent and heading; however, about 25 seconds before the airplane’s landing lights disappeared, a momentary right turn, followed by a left turn and increased descent rate was observed. No explosion or glow of fire was observed when the landing lights disappeared about 0544. Review of preliminary FAA Automatic Dependent Surveillance – Broadcast (ADS-B) data revealed that the airplane crossed CEDAR intersection about 2,500 ft mean sea level (msl). The airplane continued toward runway 10 in a descent; the final data recorded was at 0543:54 with the airplane at 800 ft msl and 1.36 nautical miles from the runway threshold. Figure 1 provides an overview of the ADS-B data from the approach and the location of the wreckage. A search was initiated for the airplane based upon inquiries from the operator’s dispatch to the airport and an active emergency locator beacon near the runway. The airplane was located about .70 nautical mile from runway 10 about 0630. According to FAA airman and operator records, the captain held an airline transport pilot certificate with a type rating in the accident airplane. He was issued a first-class medical certificate in January 2021. He had accumulated a total flight experience of about 12,000 hours, with 1,665 hours in the accident make and model airplane, of which 1,325 hours were The first officer held a second-in-command type rating in the accident airplane. He was issued a second-class medical certificate in March 2021. He had accumulated a total flight experience of about 11,000 hours, of which 1,250 hours were in the accident make and model airplane. The initial impact point coincided with broken pine tree branches among a forest where the trees were about 150 ft tall. The debris path was oriented on a heading of about 100° and spanned about 880 ft from the initial impact to the main wreckage area. The airplane was heavily fragmented, however, there was no evidence of fire. The largest fragments of wreckage were concentrated in three primary areas overviewed in Figure 2. The figure shows the initial impact point and a pop-out drone image that describes the three areas. All major components of the airplane were located in the debris path. Flight control continuity could not be determined from the control surfaces to the cockpit due to the heavy fragmentation, however, within the fragmented flight control areas continuity was observed. The flaps were observed to be extended, and the right landing gear was observed to be down. The horizontal stabilizer and its jack screw were found to be within a normal envelope. Examination of the cockpit found the flap selector in the full flaps 40° position and the landing gear handle was selected down. Both engines exhibited impact damage and varying degrees of foreign object debris ingestion that had the appearance of wood chips and green vegetation in the center core of the engine when viewed with a borescope. Several fan blades exhibited leading edge gouging, knicks, and torsional twisting. The airplane was not required to be equipped with a cockpit voice recorder (CVR); however, a CVR was installed. It was located in the debris path near the empennage and was retained for read-out and transcription. The airplane was not equipped with a flight data recorder, nor was it required.

Private Mexican

Palenque Chiapas

In unknown circumstances, the crew made a belly landing near Palenque Airport. By night, the aircraft crash landed in an open field and came to rest. The occupant(s) was/were not found but law enforcement officials found 3 tons of cocaine on board. The aircraft seems to be written off.

Alliance Air Charter

San Luis Potosí San Luis Potosí

The aircraft departed Santiago de Querétaro Airport on a night cargo flight to Laredo, Texas, carrying two pilots and a load consisting of automotive parts. En route, the crew encountered engine problems and was clearted to divert to San Luis Potosí-Ponciano Arriaga Airport for an emergency landing. On approach, the crew realized he could not make it and decided to attempt an forced landing. The airplane struck the ground, lost its undercarriage and came to rest in an agricultural area located in Peñasco, about 6 km northeast of runway 14 threshold. The left wing was bent and partially torn off. Both crew members escaped with minor injuries and the aircraft was damaged beyond repair.

March 3, 2014 4 Fatalities

Iran Aseman Airlines

Kish Island Hormozgan

The Aircraft mission was Calibration flight. The flight was planned for departure from Mehrabad airport, Tehran to Kish Island airport. Eight persons were onboard of the aircraft (3 Pilots, 4 Ground technicians, a Security guard member). The flight was under operation of Iran Aseman Airline with valid Air Operation Certificate (AOC No; FS-102). The aircraft has taken off from RWY 29L from THR airport at 15:03 Local time and reached to cruise level FL270.The aircraft has landed on RWY 09 L Kish island airports at 16:44 local time. Four ground technicians have got off from the aircraft and refueling was done. At time 17:44 LMT , the aircraft has taken off RWY 27R and requested to join Right downwind up to 1000 ft. and 8 miles from the airport. After successful performing 7 complete flight (approach & climbing) for Navigation – Aids inspection purposes; at the 8th cycle, just at turning to the final stage of approach before runway threshold the aircraft crashed into the sea and was destroyed at time 18:45 local time. All four occupants were killed.

Aerotaxis Dos Mil

Newnan-Coweta County Georgia

A technician was in charge to ferry the airplane to a hangar for a maintenance control. While taxiing, the Falcon went out of control, rolled down an embankment and collided with a utility pole. The nose was severely damaged and the aircraft was damaged beyond repair. According to the technician, who escaped uninjured, the brakes failed while taxiing.

Peruvian Air Force - Fuerza Aérea del Perú

Chiclayo Lambayeque

Shortly after takeoff from Chiclayo Airport, while climbing, the crew contacted ATC, reported technical problems and was cleared for an immediate return. On final approach, the crew was forced to make an emergency landing when the aircraft crash landed about 500 metres short of runway. All 8 occupants escaped uninjured while the aircraft was damaged beyond repair.

Aerotaxis Dos Mil

Vail Colorado

During taxi the airplane was observed to run over a tire chock with the left main gear tire. During a turn out of the ramp, the left main gear was observed to run over the nose gear chock that had been removed from the nose gear by the pilot during pre-flight. During the departure roll, the left main gear tire failed and the pilot elected to abort the takeoff attempt. The airplane did not stop on the remaining runway surface and departed the runway overrun area, coming to rest in snow-covered terrain. An examination of the airplane's systems revealed no anomalies.

December 17, 2009 2 Fatalities

FL Aviation Group

Matthew Town Inagua

On December 17, 2009 at approximately 7:30 pm local (2330UTC), N28RK a Dassault Sud, Falcon Fan Jet, Mystere 20, Series D aircraft which departed Joaquin Balaguer Int’l Airport (MDJB) in the Dominican Republic, for Ft Lauderdale Executive Airport, (FXE) Ft Lauderdale, Florida, USA, crashed in a remote area of Matthew Town, Great Inagua, Bahamas. The accident occurred approximately 11.5 miles due east of Great Inagua International Airport at coordinates N 20° 58’ 30” latitude and W 073° 40’ 00.7” longitude. The aircraft made contact with the terrain on a heading of approximately 105 degrees magnetic. The accident occurred in area that was not accessible by land and the investigation team had to be airlifted by helicopter to the site. Witnesses on the island of Great Inagua reported hearing a loud bang that rattled doors and windows of their homes, but they did not report seeing the aircraft fall from the sky. The aircraft was under the command of Captain Harold Roy Mangels and First Office Freddy Castro. The aircraft reportedly departed Aruba, in the Netherland Antilles and made a fuel stop at Dr. Joaquin Balaguer Int’l Airport, Santo Domingo in the Dominican Republic. The final destination filed by the crew was Ft. Lauderdale Executive Airport, Ft Lauderdale Florida. The accident occurred approximately 6 mile off the filed flight path. ATC records and instructions were for the aircraft N28RK to maintain 28,000 ft (FL280). The aircraft transponder was reported as inoperative. It begun a rapid descent, with no report of an emergency declared or mayday call out. Investigation of the crash site indicates the airplane made contact with the terrain at a high rate of speed and approximately a 45 degree angle. The aircraft was destroyed on impact. The crew of a United States Coast Guard helicopter was on a training mission in the Great Inagua area at the time of the accident. They reported hearing a loud bang and noticed a huge explosion and fireball emanating from the ground in an area close to their location. The crew of the US Coast Guard helicopter reported that they did not see any in-flight fire prior to the fireball that they saw. The post impact fire engulfed approximately five (5) acres of trees and brush in the National Wildlife Refuge at Great Inagua. The coast guard helicopter crew stated that they discontinued their training mission and went to the site to investigate. Upon arrival at the site the crew reported that they lowered rescue personnel to the ground to investigate and search for survivors, but, due to the heat and extent of the fire on the ground, they had to discontinue the search. They reported the accident to authorities at Great Inagua. This information was further passed along to the National Transportation Safety Board who alerted the accident investigation unit of the Bahamas Civil Aviation Department. Night time conditions prevailed at the time of the accident. The crew of the aircraft received fatal injuries. A search of the area discovered no distinguishable human remains. Approximately less than 1% of what is believed to be possible human flesh / internal body parts were recovered. In addition clothing (piece of a pant with belt buckle fastened) was recovered, which possibly may have been worn by a member of the crew at the time of the accident. All recovered remains and clothing retrieved were gathered by officers of the Royal Bahamas Police Force that accompanied the investigation team and sent to the Forensic Science Laboratory at the Royal Bahamas Police Force, Nassau Bahamas for DNA analysis and possible identification. The aircraft broke into many pieces after contact with the terrain. Debris was spread over a large area of rough terrain. What remained of the aircraft post impact was either not found or possibly further destroyed by the post impact fire. The “four corners” of the airplane were confirmed in the area downstream of where the initial ground impact occurred. However, engine cowling parts were found prior to the point of initial ground impact. This may suggest an aircraft over-speed condition prior to ground impact. Less than 10% of the aircraft was recovered. An explosion occurred when N28RK made contact with the terrain. A post impact fire ensued. Approximately 5 acres of the national park was destroyed by the fire. Parts of the aircraft including personal effect, aircraft parts and furnishing, seat and seat cushions were also destroyed in the post impact fire.

Ameristar Jet Charter

Jamestown-Chautauqua County New York

The co-pilot was performing a nighttime approach and landing to runway 25. No runway condition reports were received by the flight crew while airborne, and a NOTAM was in effect, stating, “thin loose snow over patchy thin ice.” After landing, the co-pilot called out that the airplane was sliding and the wheel brakes were ineffective. The captain took the controls, activated the air brakes, and instructed the co-pilot to deploy the drag chute. The crew could not stop the airplane in the remaining runway distance and the airplane overran the runway by approximately 100 feet. After departing the runway end, the landing gear contacted a snow berm that was the result of earlier plowing. The captain turned the airplane around and taxied to the ramp. Subsequent inspection of the airplane revealed a fractured nose gear strut and buckling of the fuselage. The spring-loaded drag chute extractor cap activated, but the parachute remained in its tail cone container. Both flight crewmembers reported that the runway was icy at the time of the accident and braking action was “nil.” The airport manager reported that when the airplane landed, no airport staff were on duty and had not been for several hours. He also reported that when the airport staff left for the evening, the runway conditions were adequate. The runway had been plowed and sanded approximately 20 hours prior to the accident, sanded two more times during the day, and no measurable precipitation was recorded within that time frame. The reason that the drag chute failed to deploy was not determined.

Jet 2000

Kiel-Holtenau Schleswig-Holstein

En route from Moscow-Domodedovo to Luton, while cruising over Germany, the crew declared an emergency following smoke spreading in the cabin and the cockpit. The crew was cleared to divert to Kiel-Holtenau Airport. After landing by night on runway 26 which is 1,265 metres long, the aircraft was unable to stop within the remaining distance. It overran and came to rest in a ravine. All 6 occupants escaped uninjured while the aircraft was damaged beyond repair.

January 9, 2006 11 Fatalities

Islamic Revolutionary Guard Corps

Orumiyeh West Azerbaijan

While approaching Orumiyeh Airport, the crew contacted ATC and reported technical problems with the landing gear. They seemed to be down but the three green lights did not came on in the cockpit panel. In accordance with ATC, the crew completed a low pass in front of the control tower then initiated a circuit when both engines flamed out. The aircraft went out of control and crashed in a field located 12 km from Orumiyeh Airport. The aircraft was destroyed and all 11 occupants were killed, among them General Ahmad Kazemi, Chief Commander of the Revolutionary Guard Land Forces and Commander Hanif, Head of the Land Forces intelligence services.

USA Jet Airlines

Lorain Ohio

The small, twin-engine business jet was about 15 feet above the runway on takeoff, when a flock of birds from both sides of the runway flew up in front of the airplane. The number two engine "surged," and "loud reports" were heard before the copilot noted a complete loss of power on the number two engine instruments. The airplane climbed for about 10 seconds, before the copilot observed the gas producer (N1) gauge on the number one engine decay through 50 percent. The stall warning horn sounded, and the pilot adjusted the flight controls for landing. The airplane contacted the runway with the landing gear retracted, overran the runway, struck a fence, crossed a road, and came to rest in a cornfield about 1,000 feet beyond the initial point of ground contact. Post accident examination of both engines revealed evidence and damage consistent with multiple bird ingestion.

Jet 2000

Moscow-Sheremetyevo Moscow oblast

Aircraft lost power on both engines while on approach to Moscow-Vnukovo airport. The crew decided to divert to Sheremetievo Airport when the undercarriage collapsed on landing. The aircraft veered off runway and slid in a grassy area before coming to rest. Nobody was injured but the aircraft was damaged beyond repair.

Jet Sul Taxi Aéreo

Oranjestad Dutch Antilles

Following an uneventful positioning flight from Porlamar, the aircraft landed at Oranjestad-Reina Beatrix Airport with its undercarriage retracted. The aircraft slid on ity belly for few dozen metres before coming to rest. Both pilots escaped uninjured while the aircraft was damaged beyond repair.

Grand Aire Express - Executive Aire Express

Saint Louis-Lambert Missouri

The twin engine turbofan powered airplane was ditched into a river after a complete loss of power from both engines. The airplane was on a second approach to land on runway 30R after having been instructed by air traffic control (ATC) to climb during the final approach segment of the first approach due to inadequate separation from another airplane. Subsequent to the first approach, the airplane was issued vectors for the second approach by ATC. Communications transcripts show that the flight crew asked ATC how far they would be vectored during the second approach, but the flight crew did not inform ATC of their low fuel state until the airplane was already on a "base turn...to join final." The airplane subsequently lost power from both engines. During interviews, both pilots stated that there were no problems with the airplane. The second-in-command (SIC) stated that the airplane "ran out of fuel" and that the fuel quantity indicators read 0 and 100 pounds when each respective engine stopped producing power. The SIC also stated that after being instructed to climb to 5,000 feet after their first approach, he questioned the pilot-in-command about landing at another airport located about 14 nautical miles west-southwest of the destination airport. The SIC said that the PIC elected to continue with the second approach to the original destination. Research indicated that the flight crew did not obtain a weather briefing prior to the accident flight. Additionally, the Terminal Aerodrome Forecast that was valid at the time the aircraft's flight plan was filed showed a forecast ceiling consisting of overcast clouds at 1,500 feet above ground level at the aircraft's arrival time at the destination. 14 CFR Part 91.169 requires that an alternate airport be listed in the flight plan when forecast ceilings are less than 2,000 feet. No alternate was listed in the flight plan for the accident flight. Additionally, 14 CFR Part 91.167 requires that aircraft operated in instrument meteorological conditions maintain fuel reserves that allow flight to the intended destination and then continued flight to the listed alternate, and an additional 45 minutes at normal cruise speed. In 1993, the FAA/industry advisory committee developed advisory material for fuel planning and management for 14 CFR Part 121 and 135 air carrier flight operations, but the material was never published.

April 8, 2003 3 Fatalities

Grand Aire Express - Executive Aire Express

Toledo-Express Ohio

The flight crew of the Fan Jet Falcon (DA-20) were practicing ILS approaches in instrument meteorological conditions with low clouds and rime ice. A first officer (FO) in training occupied the right seat, while the pilot-in-command (PIC), who was also the company chief pilot/check airman/designated flight instructor, occupied the left seat and was handling the radios. On the second approach, the airplane struck trees and burned, 1.57 nm from approach end of the runway. The landing gear was found extended, and the trailing edge and droop leading edge flaps were retracted. The wing and engine cowl anti-ice valves were found closed, consistent with it being off in the cockpit. Radar data revealed that on approach, the airspeed decreased from 188 knots to 141 knots at the outer marker, and continued to decrease down to 106 knots, when the airplane entered an abrupt descent and disappeared from radar. Simulator flights matched the radar profile with a flight idle approach, a power reduction inside the outer marker, and 1/4 inch of ice on the wings. In the simulator, the airplane stalled about 2 miles from the end of the runway with an airspeed of 103 kts. At flight idle, the engine power in the last 2 minutes of approach was below the recommended power setting for wing or engine anti-ice to be effective. Vref and stall speeds were computed to be 129 kts and 96 kts, with wing flaps and droop leading edges retracted. The PIC had about 1,100 hours in the make and model. The PIC did not have any documented previous flight instruction experience in make and model or any other multi-engine airplanes. The PIC had given 4 pilot proficiency checks in the DA-20 since receiving his check airman designation. The company Director of Operations reported that the accident FO was the first student the PIC had taken through the initial second-in-command course. The PIC and FO had received all of their turbojet experience with the operator.

Grand Aire Express - Executive Aire Express

Detroit-City (Coleman A. Young) Michigan

The airplane sustained substantial damage on impact with terrain and objects after traveling off the end of the runway during a main wheels up landing. The captain reported that prior to takeoff, he closed the cargo door and the copilot confirmed the door light was out. After takeoff at an altitude of about 600 feet, the cockpit door popped open and the crew noticed the cargo door was open. The captain elected to return to land. The captain reported he requested repeatedly for gear and flaps extension, but the copilot was late in doing so and it "caused us to overshoot the runway centerline." The copilot then began calling for a go around/missed approach at which time he raised the gear and the retracted some of the flaps. The copilot reported the captain continued to descend toward the runway and overshot the runway centerline to the right. The copilot reported that at this time he lowered the gear. The nose gear extended prior to touchdown, however the main gear did not. The airplane touched down approximately 1/2 way down the runway and traveled off the end. A witness reported noticing that the exterior door latch was not down as the airplane taxied to the runway.

August 5, 2001 3 Fatalities

Naske Air

Narsarsuaq Kommune Kujalleq

The flight, during which the accident occurred, was part of a non-scheduled international cargo flight from Gdansk (EPGD) to Louisville (KSDF). The flight crew had previously on August 4, 2001, on another charter flight, flown the aircraft from Hanover (EDDV) to Palma de Mallorca (LEPA) and then to EPGD in order to bring the aircraft in position for the cargo flight. The flight was chartered by a cargo courier to depart EPGD at 2000 hrs on August 4, 2001, and arrive at KSDF at 0900 hrs on August 5, 2001. Technical landings (fuel uplift) were planned at EKCH in Denmark, at Keflavik (BIKF) in Iceland, at BGBW in Greenland and at Sept-Iles (CYZV) in Canada. The aircraft had a two hour delay at LEPA due to a slot time. For that reason, the aircraft did not arrive at EPGD until 2106 hrs. The aircraft was refuelled and the flight crew loaded the cargo themselves. The aircraft departed EPGD at 2218 hrs and arrived at EKCH at 2238 hrs. Then the aircraft departed EKCH at 2313 hrs and arrived at BIKF at 0202 hrs. At BIKF, the aircraft was refuelled with 1034 USG of JET A1. The commander filed an ATC flight plan for BGBW with Kangerlussuaq (BGSF) in Greenland as destination alternate. At BIKF no weather reports for BGBW were valid for the flight crew’s flight planning. The handling agent directed the Commander’s attention to the lack of updated weather reports for BGBW, but the Commander seemed not to be concerned. It was the general opinion of the handling agent that the Commander seemed stressed. At 0246 hrs, the flight crew requested start up and shortly after they got an ATC clearance to BGBW via EMBLA, 63N 30W, 62N 40W and NA at FL 240 with cruise Mach at 0.76. The aircraft departed BIKF at 0300 hrs and the flight crew got an ATC clearance with FL 260 as the final cruising level inbound BGBW. The First Officer was the pilot flying and the Commander was the pilot non-flying. At 0423:24 hrs, the Commander contacted Narsarsuaq Flight Information Service (FIS) on frequency 121.300 MHz. The Commander reported that they expected to be overhead NA (358 KHz) at 0438 hrs. At this time, the aircraft was cruising at FL 260 and was inbound NA on a magnetic track of 280° approximately 50 nm east of the aerodrome. Through link to Gander ATC, Narsarsuaq FIS cleared the aircraft to descend out of controlled airspace on QNH 1004 and to report FL 195 descending. The Commander was now the pilot flying and the First Officer was the pilot non-flying. The Commander had experience of flying to BGBW. The aircraft left FL 260, and at 0434:27 hrs, the First Officer reported that the aircraft was passing FL 195. Narsarsuaq FIS requested the flight crew to report 10 nm from the aerodrome. While descending, the flight crew made a briefing on the NDB/DME approach procedure to runway 07. At 0437:00 hrs, the First Officer reported that the aircraft was 10 NM from NA. Narsarsuaq FIS requested the flight crew to contact Narsarsuaq AFIS on frequency 119.100 MHz. At 0437:17 hrs, the flight crew was in contact with Narsarsuaq AFIS and the First Officer reported passing FL 130. The AFIS Operator reported that there was no reported traffic in the TIZ and that the flight crew could make an approach by their own discretion. The weather was reported to be a wind direction and speed of 080° at 24 knots, visibility 10 kilometres with broken clouds at 6000 feet and overcast at 9000 feet, light rain, temperature +14°C, dew point +3°C and the QNH 1004 hPa. At 0440:26 hrs and at 0440:52 hrs, one of the flight crewmembers made cockpit call outs of passing 6 nm and 8 nm respectively outbound from NA. At 0441:45 hrs, one of the flight crewmembers made a cockpit call out of the aircraft being on base. The Commander ordered the extension of the landing gear. With reference to the CVR read out, there were no audible flight crew call outs concerning the use of checklists, altitude checks and Standard Operating Procedures (SOP) during the descent, the initial and the final approach phase. At 0442:29 hrs, the First Officer reported that the aircraft was on final to runway 07. The AFIS operator reported the threshold wind for runway 07 to be 070° at 22 knots gusting to 29 knots and the runway to be free. The AFIS operator made a visual scan of the approach sector, but he did not see the aircraft, as he normally would have, when an aircraft was established on final in dark night and under similar weather conditions. At approximately 0443:07 hrs, the aircraft impacted in landing configuration mountainous terrain at approximately 700 feet msl. The accident occurred 4.5 nm southwest of the aerodrome. On the CVR read out, there were no audible flight crew call outs immediately before the impact. Several times from 0452 hrs until 0459 hrs, Narsarsuaq AFIS tried to get in radio contact with the aircraft, but there was no reply.

Grand Aire Express - Executive Aire Express

Peterborough Ontario

The Dassault-Breguet Falcon 20E aircraft was on an unscheduled charter cargo flight from Detroit Willow Run, Michigan, USA, to Peterborough, Ontario. The flight was being conducted at night and under instrument flight rules in instrument meteorological conditions. Nearing the destination, the flight crew received a clearance to conduct a non-directional beacon runway 09 approach at Peterborough Airport. The flight crew did not acquire the runway environment during this approach and conducted a missed approach procedure. They obtained another clearance for the same approach from Toronto Area Control Centre. During this approach, the flight crew acquired the runway environment and manoeuvred the aircraft for landing on runway 09. The aircraft touched down near the runway midpoint, and the captain, who was the pilot flying, elected to abort the landing. The captain then conducted a left visual circuit to attempt another landing. As the aircraft was turning onto the final leg, the approach became unstabilized, and the flight crew elected to overshoot; however, the aircraft pitched nose-down, banked left, and struck terrain. As it travelled 400 feet through a ploughed farm field, the aircraft struck a tree line and came to rest about 2000 feet before the threshold of runway 09, facing the opposite direction. The aircraft was substantially damaged. No serious injuries occurred.

SmithAir - USA

Boise Idaho

After extending the gear for landing, the down-and-locked indication (green light) for the left main gear was not illuminated. The crew performed the emergency checklist procedures for abnormal gear extension with no success. The aircraft subsequently landed with the left main landing gear retracted. Inspection of the landing gear revealed that the pin (part number MY20248-001), which is part of the forward gear door lock, was corroded and cracked at the point of rotation, preventing proper movement of the gear door uplock.

Reliant Airlines

El Paso-Intl Texas

The airplane was dispatched as a cargo flight to pick up a load of 118 boxes of automotive seatbelts. After refueling and loading the cargo on board, the flight crew taxied to runway 22 for a no-flap takeoff, which called for a V1 speed of 141 knots. The first officer was the flying pilot for this leg of the flight. The crew reported that the initial takeoff roll from the 11,009 foot runway was normal. At approximately 120 knots, the flight crew reported hearing a loud bang followed by a vibration. The captain called for the first officer to abort the takeoff. The captain later stated that he believed he saw the #2 engine "roll back." The flight crew reported that the brakes were not effective in slowing the airplane. A witness stated that the airplane was going west on the runway at a high rate of speed when it "went up to two feet, then came back down." Another witness stated that he saw the airplane "exit off the end of the runway" and after about "seventy-five to one hundred feet, the front wheels lifted off the ground about ten feet." The airplane overran the departure end of the runway, went through the airport's chain link perimeter fence, across a 4-lane highway, collided with 3 vehicles on the roadway, and went through a second chain link fence, before coming to rest. The airplane came to rest on its belly, 2,010 feet from the departure threshold of runway 22. The investigation revealed that the flight crew was provided an inaccurate weight for the cargo, and the airplane was found to be 942 pounds over the maximum takeoff weight at the time of the accident. The density altitude was calculated to be 5,614 feet at the time of the accident. Both crewmembers were current and properly certified; however, the captain had upgraded to his present position two months prior to the accident, and the first officer had accumulated a total of 123.8 hours in the Falcon 20 at the time of the accident. Both engines were operated in a test cell and performed within limits. About 90% of the right outboard main landing gear tire's retread was found on the runway approximately 7,200 feet from where the aircraft had commenced its takeoff roll. The operator stated that since the aircraft was over maximum gross weight, the long taxi to the runway could have resulted in the brakes and tires heating more than normal.

March 3, 1997 4 Fatalities

Islamic Republic of Iran Air Force

Ardabil Ardabil

While approaching Ardabil Airport in poor weather conditions, the aircraft struck the ground few km short of runway. All four crew members were killed. They were completing a humanitarian flight from Tehran.

February 7, 1997 4 Fatalities

Estornel Air Services

Mt Chivilme Salta

The aircraft was completing a cargo flight from Córdoba to Salta with an intermediate stop in San Miguel de Tucumán, carrying two passengers and two pilots. The crew departed San Miguel de Tucumán-Teniente Benjamin Matienzo Airport at 2145LT and was cleared to climb to FL180. At 2201LT, the crew reported over PONPI VOR located 55 nm from Salta. Two minutes later, the crew was cleared to descent on top of the clouds in VMC conditions. While cruising at an altitude of 6,970 feet, the aircraft struck the slope of Mt Chivilme located 36,4 km southwest of Salta Airport. The aircraft was destroyed by impact forces and all four occupants were killed.

Bangko Sentral NG Pilipinas

Davao City Davao del Sur

The aircraft was completing a cargo flight from Davao City to Manila, carrying six passengers, two pilots and a load consisting of eight crates of gold. Just after liftoff, while climbing to a height of about 75 feet, the aircraft stalled and landed back on runway. Unable to stop within the remaining distance, the aircraft overran and came to rest in a banana plantation, broken in three. All eight occupants escaped uninjured.

January 20, 1995 10 Fatalities

Leadair Unijet

Paris-Le Bourget Seine-Saint-Denis

After takeoff from runway 25 at Paris-Le Bourget Airport, while in initial climb, the aircraft collided with birds. The left engine failed then exploded. The crew declared an emergency and was cleared to return. On short final, after the left engine detached, the aircraft nosed down to an angle of 15°, struck the ground and crashed near runway 21 threshold. It slid for 430 metres then came to rest, bursting into flames. The aircraft was destroyed by fire and all 10 occupants were killed, among them CEO of the food group Saint-Louis.

December 2, 1991 4 Fatalities

French Air Force - Armée de l'Air

Élancourt Yvelines

The crew departed Luxeuil-Saint Sauveur AFB on a training flight to Vélizy-Villacoublay AFB on behalf of the 'Système de Navigation d’Attaque' (SNA). On approach, both engines lost power and the crew elected to divert to Toussus-le-Noble Airport for an emergency landing. The captain eventually attempted to land on a sports field when the aircraft struck a concrete wall and crashed, bursting into flames. The wreckage was found in Élancourt, about 17 km west of Vélizy-Villacoublay AFB. The aircraft christened 'Étoile du Berger' was destroyed and all four crew members were killed. Crew: Cdt Jean-Luc Luciani, Cpt Christian Huth, Cpt Pierre Schmitt, Lt Philippe Hirson.

Grup-Air

Kiel-Holtenau Schleswig-Holstein

Following a wrong approach configuration, the twin engine aircraft landed too far down a wet runway. After touchdown, the crew realized he would not be able to stop the airplane within the remaining distance and decided to initiate a go-around procedure. Power was added on both engines and the aircraft took off. After passing over the runway end at low altitude, the aircraft struck trees, stalled and crashed in a wooded area. Nine occupants were injured, some of them seriously, while one pilot was killed.

June 29, 1989 2 Fatalities

Phoenix Air - USA

Cartersville Georgia

The crew arrived at the airport about 20 minutes before the planned midnight takeoff time, after the pilot-in-command had spent the day moving furniture. A night watchman noted that the preflight inspection and takeoff roll to rotation/lift-off was normal. There was no post-takeoff radio call to either unicom or ATC, although the crew had filed an IFR flight plan. After taking off from runway 36, the aircraft crashed about 1.8 mile north of the runway. The wreckage was found after interruption of electrical power to a nearby city. Initial impact was with trees, while in a shallow/left/descending turn. An area of trees about 1/2 mile long was damaged by impact and fire. Before coming to rest, the aircraft hit a powerline support tower. There was evidence the aircraft was traveling at about 260 knots, when it crashed. No preimpact part failure or malfunction was found that would have resulted in the accident. Both pilots were killed.

Reliant Airlines

Binghamton New York

During arrival, the cargo flight (reliant 232) contacted Binghamton approach control and received vectors for an ILS runway 16 approach. At that time, the atis had information (information kilo) that there was light freezing rain, that all paved surfaces had a thin layer of ice, and that braking action was poor. The copilot made the approach and landing. The captain reported that touchdown was normal in the 1st 1,000 feet of the runway and that the airbrake was used, but they did not know that braking action was nil until they were on the landing roll. By the time they realized braking was nil, there was insufficient runway remaining for a safe go-around. The captain reported he deployed the drag chute, but a witness who saw the chute, reported it did not open. Subsequently, the aircraft continued off the departure end of the 6,298 feet runway, went down a steep embankment and was extensively damaged. The required distance to stop on an icy runway was estimated to be 5,344 feet.

Segas International

Lugano-Agno Ticino

During the takeoff roll on runway 21, just before reaching V1 (112 knots), the captain thought that the right engine lost power. He decided to abandon the takeoff maneuver and initiated an emergency braking procedure. Unable to stop within the remaining distance, the aircraft overran at a speed of about 60-70 knots, rolled in a snow covered field and eventually collided with an embankment, coming to rest, broken in two. Both pilots were injured.

Drenair

Keflavik Southern Peninsula (Suðurnes)

Recently purchased by the Spanish operator Drenair, the aircraft departed West Palm Beach, Florida, on a delivery flight to Spain, carrying four passengers and two pilots. After a fuel stop in Bedford, Massachusetts, and Goose Bay, Newfoundland, the aircraft continued to Keflavik, Iceland. While approaching Keflavik, the crew declared an emergency due to fuel exhaustion, informed ATC about his position and ditched the aircraft approximately 70 km southwest of Keflavik. All six occupants were quickly rescued by the crew of a helicopter while the aircraft sank and was lost.

Air Truck

Las Palmas-Gando (Gran Canaria) Canary Islands

During the last segment, the aircraft was unstable and upon touchdown, it went out of control. It veered off runway to the left and came to rest. Both crew members escaped uninjured while the aircraft was damaged beyond repair.

May 31, 1981 3 Fatalities

Algerian Government

Bamako Bamako City District

On final approach to Bamako Intl Airport, the crew encountered poor weather conditions with stormy weather and severe turbulences. The airplane went out of control and crashed 8 km short of runway. Both passengers and a crew member were injured while three other crew members were killed. Both passengers were the Algerian Minister of Foreign Affairs Mohamed Seddick Benyahia and his chief of staff. They were en route to Freetown to take part to a conference about the war in the Western Sahara.

May 18, 1978 4 Fatalities

Flight Safety International

Memphis Tennessee

The crew was performing a local training flight at Memphis Airport. Following several maneuvers and while circling in the traffic pattern at an altitude of 2,000 feet, the twin engine airplane collided with a private Cessna 150 registered N6423K and carrying two pilots. Following the collision, both airplane entered a dive and crashed about 3,8 miles west of the airport. All six occupants in both aircrafts were killed.

R.J. Reynolds Tobacco Company

Naples Florida

Shortly after takeoff from Naples Airport, while initial climb, the airplane collided with a flock of seagulls that entered the engines. Both engines' compressors stalled, the airplane lost speed then stalled and crashed in an open field located past the runway end. The aircraft was damaged beyond repair and all 11 occupants were seriously injured.

August 7, 1976 3 Fatalities

Hansa Jet Corporation

Chilpancingo-Doctor Alfonso G. Alarcón Guerrero

Following an uneventful flight from Houston, the crew was cleared to descend from 37,000 feet to 19,000 feet for an approach to Acapulco-General Juan N. Álvarez Airport. For unknown reasons, the crew continued the descent below 19,000 feet when, at an altitude of 9,000 feet, the airplane struck the slope of a mountain located 20 km southwest of Chilpancingo, about 70 km north of Acapulco. At the time of the accident, the visibility was reduced by night and rain falls.

January 22, 1976 5 Fatalities

GLAM - Groupe de Liaisons Aériennes Ministérielles

Rambouillet Yvelines

Few minutes after takeoff from Vélizy-Villacoublay, en route to Francazal Airbase in Toulouse, the airplane went out of control and crashed in unknown circumstances in Rambouillet, about 30 km southwest of its departure point. The aircraft was destroyed and all five occupants were killed.

Ling-Temco-Vought

Grand Prairie-Hensley Field NAS Texas

During the takeoff roll on runway 17 at Grand Prairie-Hensley Field NAS, the pilot-in-command elected to takeoff but this was impossible due to an incorrect trim setting. As the aircraft unrotated, the crew decided to attempt an emergency braking procedure but the aircraft was unable to stop within the remaining distance. It overran runway 17, collided with a fence and eventually came to rest into the Mountain Creek Lake. All five occupants were injured, both pilots seriously.

November 21, 1974 2 Fatalities

Air Taxi Company

Kermanshah Kermanshah

On approach to Kermanshah Airport, the crew encountered poor visibility due to foggy conditions. Apparently to establish a visual contact with the ground, the crew decided to reduce his altitude when the airplane struck a hill located 3 km short of runway threshold. Out of control, the airplane crashed in flames 300 meters further. Two crew members were killed while a third occupant was injured.

Federal Express - FedEx

Fort Worth-Meacham Texas

The crew expected to make a straight-in approach but was cleared by ATC to make an ILS circling approach that was completed in rain showers with a tailwind of 8 knots. After touchdown on a wet runway, the crew encountered difficulties to decelerate properly as the airplane suffered hydroplaning. Unable to stop within the remaining distance, the airplane overran and came to rest few dozen yards further. Both pilots were seriously injured and the aircraft was damaged beyond repair.

Fred. Olsen's Air Transport - Fred. Olsen Flyselskap

Norwich Norfolk

The Dassault Falcon 20C jet aircraft was on charter to fly passengers from Norwich, U.K. to Gothenburg, Sweden, and during the morning it made an uneventful positioning flight from Oslo, Norway, to Norwich where it landed at 12:28 hrs. The six passengers boarded the aircraft at about 15:20 hrs and the aircraft received clearance from Norwich Tower to taxi out for take-off on runway 28. While taxying the crew received an airways clearance and the aircraft was lined up on the runway without delay. The co-pilot, a qualified commander on this type of aircraft, was in the left hand pilot's seat, and the aircraft commander in the right hand seat. No bird flocks were seen by either of the pilots whilst taxying to the active runway. The aircraft took-off at 15:37 hrs piloted from the left hand seat. On becoming airborne, at a position a little over halfway down the runway, the crew saw a flock of birds ahead flying just above the ground. The pilot increased slightly the aircraft's climb attitude and the flock passed underneath. A few seconds later a second flock was seen at a higher level and directly in the aircraft's flight path. The pilot lowered the aircraft nose and the flock passed overhead. On re-establishing the climb and at a height of between 100 and 200 feet a third flock was seen, again directly ahead. This flock extended from ground level to well above the aircraft and there was no possible way for the pilot to avoid it; almost immediately the crew heard the sound of multiple bird strikes on the aircraft, the commander described the noise as 'like a machine gun'. The pilot maintained the aircraft in the climb attitude and the commander, who was checking the aircraft's instruments, noticed the RPM on both engines running down very fast, he also observed the engine pressure ratio (EPR), and exhaust gas temperature (EGT) instrument readings dropping. The pilot heard a bang from the engines, followed by the sound of the engines running down in a rough and abnormal manner. He quickly asked if both engines had failed. This was confirmed by the commander who tried to move the thrust levers without any response from the engines. By this time the aircraft was at a height of approximately 300 feet with the landing gear still down, the crew not having had time to select it up because of their preoccupation with avoiding the bird flocks. The speed, which had been about 150 knots prior to the bird strikes, had dropped to 135 knots. The control column was eased forward to maintain speed and the aircraft began to lose height. The pilot saw a field ahead and slightly left of the aircraft which he considered the best forced landing area. On receiving confirmation of his decision from the commander, the pilot made a turn to the left and lined up the aircraft for an approach to the selected field. Visibility was not good because of approaching darkness but the crew were able to see some trees at the approach end of the field. These were avoided and a positive touch down made; the stall warning sounded just before the aircraft hit the ground. Battery and fuel switches were turned off either just before or after ground impact and an attempt was made to close the thrust levers, but these would not move. All three landing gear legs were torn off shortly after ground impact and the aircraft finally came to rest on the belly of the fuselage. The commander, although partially blinded by blood from cuts on his head, made his way to the main cabin door, which he opened, and all the occupants were evacuated.

Finnwings

Montreal-Mirabel Quebec

Shortly after takeoff from Mirabel Airport, while in initial climb, both engines stopped simultaneously. The pilot-in-command reduced his altitude and completed a safe belly landing in a snow covered field located near the airport. The airplane slid for several yards before coming to rest. All six occupants escaped uninjured while the aircraft was damaged beyond repair.

Fred-Air

Samedan Graubünden

While descending to Samedan Airport, weather conditions worsened rapidly. Despite the situation, the captain decided to continue the approach under VFR mode. In a limited visibility of 2 km in snow falls, the pilot-in-command passed over Lake Silvaplana at low height then initiated a right turn when the right wing tip struck the icy water. The airplane crash landed and slid for 200 meters before coming to rest. All five occupants were injured and the aircraft was written off.

General Transportation Company

Boca Raton Florida

On final approach to Boca Raton Airport, the captain attempted to retard the throttles but inadvertently shut down both engines. The airplane lost speed, stalled and struck the ground 900 feet short of runway 04 threshold. On impact, the undercarriage were torn off, the airplane slid for several yards and came to rest in a construction area. Both pilots were seriously injured and the aircraft was destroyed.

March 13, 1968 6 Fatalities

M Air

Parkersburg West Virginia

The aircraft was involved in a local training flight at Parkersburg-Wood County Wilson Airport, carrying four passengers and two pilots who were conducting touch-and-go maneuvers. Following a circuit, the pilot-in-command landed on a contaminated runway (slush, snow and ice). After touchdown, he attempted to takeoff when control was lost. The airplane veered off runway and crashed in flames on a dirt bank. It was destroyed and all six occupants were killed.

Trans Commerce Leasing

Goose Bay Newfoundland & Labrador

The aircraft was completing a transatlantic flight from Geneva to Goose Bay with an intermediate stop in Keflavik. On final approach to Goose Bay Airport, both engines failed simultaneously. The crew realized he could not reach the airport so the captain decided to attempt an emergency landing. The airplane belly landed, slid for several yards and came to rest 11 km short of runway. All seven occupants were rescued while the aircraft was damaged beyond repair.

Safety Profile

Reliability

Reliable

This rating is based on historical incident data and may not reflect current operational safety.

Primary Operators (by incidents)

Grand Aire Express - Executive Aire Express4
Aerotaxis Dos Mil2
Jet 20002
Reliant Airlines2
Air Taxi Company1
Air Truck1
Algerian Government1
Alliance Air Charter1
Ameristar Jet Charter1
Bangko Sentral NG Pilipinas1