Ameristar Jet Charter

Safety profile and incident history for Ameristar Jet Charter.

Safety Score

9.9/10

Total Incidents

5

Total Fatalities

5

Recent Incidents

McDonnell Douglas MD-83

Detroit-Willow Run (Ypsilanti) Michigan

A McDonnell Douglas MD-83, registration N786TW, suffered a runway excursion following an aborted takeoff from runway 23L at Detroit-Willow Run Airport, Michigan, USA. The aircraft had been chartered by the University of Michigan Basketball team for a flight to a game in Washington, DC. The flight crew prepared for take-off and calculated V-speeds (V1, VR, V2) using "Normal Thrust Takeoff", a 10 kts headwind, and a take-off weight of 146,600 lbs. The V-speeds for this configuration were 139 kts, 142 kts, and 150 kts, respectively. However, the flight crew chose to increase VR to 150 kts to allow for more control during take-off in the presence of windshear. During takeoff roll, at 14:51:56 (about 3,000 ft down the runway) and about 138 kts of airspeed, the control column was pulled back slightly from a non-dimensional value of -7 to -5.52. The airplane’s left elevator followed the control input and moved from a position of -15° trailing edge down to -13° trailing edge down. The right elevator did not change and stayed at approximately -16° trailing edge down. At 14:52:01 a large control column input was made (151 kts and 4100 ft down the runway) to a non-dimensional 18.5 and the left elevator moves to a position near 15° trailing edge up. After 14:52:05 the right elevator moves to -13° trailing edge down, but no more. The airplane does not respond in pitch and does not rotate. The captain decided to abort the takeoff. The maximum ground speed was 163 kts (173 kts airspeed) and the airplane began to decelerate as soon as the brakes were applied at 14:52:08. Spoilers were deployed at 14:52:10 and thrust reversers were deployed between 14:52:13 and 14:52:15. The aircraft could not be stopped on the runway. The airplane’s ground speed was 100 kts when it left the paved surface. The aircraft overran the end of the runway, damaged approach lights, went through the perimeter fence and crossed Tyler Road. It came to rest on grassy terrain, 345 meters past the end of the runway, with the rear fuselage across a ditch. The nose landing gear had collapsed. Runway 23L is a 7543 ft long runway.

Dassault Falcon 20

Jamestown-Chautauqua County New York

The co-pilot was performing a nighttime approach and landing to runway 25. No runway condition reports were received by the flight crew while airborne, and a NOTAM was in effect, stating, “thin loose snow over patchy thin ice.” After landing, the co-pilot called out that the airplane was sliding and the wheel brakes were ineffective. The captain took the controls, activated the air brakes, and instructed the co-pilot to deploy the drag chute. The crew could not stop the airplane in the remaining runway distance and the airplane overran the runway by approximately 100 feet. After departing the runway end, the landing gear contacted a snow berm that was the result of earlier plowing. The captain turned the airplane around and taxied to the ramp. Subsequent inspection of the airplane revealed a fractured nose gear strut and buckling of the fuselage. The spring-loaded drag chute extractor cap activated, but the parachute remained in its tail cone container. Both flight crewmembers reported that the runway was icy at the time of the accident and braking action was “nil.” The airport manager reported that when the airplane landed, no airport staff were on duty and had not been for several hours. He also reported that when the airport staff left for the evening, the runway conditions were adequate. The runway had been plowed and sanded approximately 20 hours prior to the accident, sanded two more times during the day, and no measurable precipitation was recorded within that time frame. The reason that the drag chute failed to deploy was not determined.

January 9, 2007 2 Fatalities

Learjet 24

Guadalajara Jalisco

On January 9, 2007, at 2323 central standard time, a Gates Learjet model 24F airplane, N444TW, serial number 348, was destroyed upon impact with terrain, about 18.8 nautical miles east of Guadalajara, State of Jalisco, in the Republic of Mexico. The airline transport-rated pilot and the commercial pilot functioning as first officer were fatally injured. The airplane was registered to the Sierra American Corporation of Wilmington, Delaware, and was being operated by Ameristar Jet Charter, Inc., of Addison, Texas, as Ameristar flight 878, a Title 14 Code of Federal Regulations Part 135 on-demand cargo flight. Night visual meteorological conditions prevailed and an instrument flight rules (IFR) flight plan was filed for the flight from Laredo, Texas. The cargo flight had originated in Laredo, Texas, at about 2210, with the Don Miguel Hidalgo International Airport (MMGL) near Guadalajara, Mexico, as its intended destination. Mexican Air Traffic Control personnel reported that the flight had approached MMGL from the north. At 2313, Guadalajara Approach Control cleared the flight to descend to 12,000 feet, provided an altimeter setting of 30.28, and told the flight to expect radar vectors for the ILS runway 28 approach to MMGL. After being provided a vector of 190 to intercept the localizer for the ILS runway 28 approach, there were communications between the flight and the controller to clarify which runway was active, and at 2318:00, the flight was given a right turn to a heading of 200 degrees. At 2318:56 the flight was cleared to descend to 10,000 feet, and at 2320:38, the flight was cleared to descend to 9,000 feet. The airplane was last observed on radar descending through 9,200 feet, while crossing the GDL VOR 085 degree radial.

Learjet 25

Del Rio Texas

The cargo flight was cleared for a visual approach to the 5,000-foot long, by 150-foot wide asphalt runway. Based on estimated landing weight of the aircraft, the Vref was estimated at 116 KIAS. Air traffic Control (ATC) radar data revealed that the flight maintained a ground speed above 190 knots on final approach, to include the touchdown zone for runway 13. The first evidence of braking was noted at a point 1,247 feet from the departure end of the runway. Braking signatures on the asphalt as well as off the pavement were consistent with an operational anti-skid system. Witnesses at the airport also observed the airplane flying very fast and touching down long. Both crewmembers, the 4,689-hour captain and the 2,873-hour first officer, were familiar with the airport, and the flight was 20 minutes ahead of its scheduled arrival time. The airplane overran the departure end of runway 13, impacted the airport perimeter fence, proceeded across a roadway, took out another fence, and collided with two trees in a cemetery. The airplane was found to be within weight and balance limits for all phases of the flight. The installed cockpit voice recorder (CVR) was found not to be functional.

August 24, 2001 2 Fatalities

Learjet 25

Ithaca-Tompkins New York

While departing from the airport, with the second-in-command (SIC) at the controls, the airplane impacted a fence, and subsequently the ground about 1,000 feet beyond the departure end of the runway. A witness on the ramp area south of the runway, stated that he heard the engines spool up; however, due to the fog, he could only see the strobe lights on the airplane. He then observed the airplane rotate about 3,500 feet from the departure end of the runway and begin to climb at a steep angle, before losing sight of it when it was about 150 feet above ground level. The weather reported, at 0550 was, calm winds; 1/2 statute miles of visibility, fog; overcast cloud layer at 100 feet; temperature and dew point of 17 degrees Celsius. Excerpts of the cockpit voice recorder (CVR) transcript revealed that the flightcrew discussed the prevailing visibility at the airport on numerous occasions, and indicated that it appeared to be less than one mile. Examination of the wreckage revealed no anomalies with the airframe or engines. According to the FAA Instrument Flying Handbook, "Flying in instrument meteorological conditions (IMC) can result in sensations that are misleading to the body's sensory system...A rapid acceleration, such as experienced during takeoff, stimulates the otolith organs in the same way as tilting the head backwards. This action creates the somatogravic illusion of being in a nose-up attitude, especially in situations without good visual references. The disoriented pilot may push the aircraft into a nose-low or dive attitude."

Airline Information

Country of Origin

United States of America

Risk Level

Low Risk

Common Aircraft in Incidents

Learjet 252
McDonnell Douglas MD-831
Learjet 241
Dassault Falcon 201