Traverse City – Toledo
Flight / Schedule
Traverse City – Toledo
Aircraft
Dassault Falcon 20Registration
N183GA
MSN
147
Year of Manufacture
1968
Date
April 8, 2003 at 01:49 PM
Type
CRASHFlight Type
Training
Flight Phase
Landing (descent or approach)
Crash Site
Airport (less than 10 km from airport)
Crash Location
Toledo-Express Ohio
Region
North America • United States of America
Coordinates
41.5864°, -83.8131°
Crash Cause
Human factor
Narrative Report
On April 8, 2003 at 01:49 PM, Traverse City – Toledo experienced a crash involving Dassault Falcon 20, operated by Grand Aire Express - Executive Aire Express, with the event recorded near Toledo-Express Ohio.
The flight was categorized as training and the reported phase was landing (descent or approach) at a airport (less than 10 km from airport) crash site.
3 people were known to be on board, 3 fatalities were recorded, 0 survivors were identified or estimated. This corresponds to an estimated fatality rate of 100.0%.
Crew on board: 2, crew fatalities: 2, passengers on board: 1, passenger fatalities: 1, other fatalities: 0.
The listed crash cause is human factor. The flight crew of the Fan Jet Falcon (DA-20) were practicing ILS approaches in instrument meteorological conditions with low clouds and rime ice. A first officer (FO) in training occupied the right seat, while the pilot-in-command (PIC), who was also the company chief pilot/check airman/designated flight instructor, occupied the left seat and was handling the radios. On the second approach, the airplane struck trees and burned, 1.57 nm from approach end of the runway. The landing gear was found extended, and the trailing edge and droop leading edge flaps were retracted. The wing and engine cowl anti-ice valves were found closed, consistent with it being off in the cockpit. Radar data revealed that on approach, the airspeed decreased from 188 knots to 141 knots at the outer marker, and continued to decrease down to 106 knots, when the airplane entered an abrupt descent and disappeared from radar. Simulator flights matched the radar profile with a flight idle approach, a power reduction inside the outer marker, and 1/4 inch of ice on the wings. In the simulator, the airplane stalled about 2 miles from the end of the runway with an airspeed of 103 kts. At flight idle, the engine power in the last 2 minutes of approach was below the recommended power setting for wing or engine anti-ice to be effective. Vref and stall speeds were computed to be 129 kts and 96 kts, with wing flaps and droop leading edges retracted. The PIC had about 1,100 hours in the make and model. The PIC did not have any documented previous flight instruction experience in make and model or any other multi-engine airplanes. The PIC had given 4 pilot proficiency checks in the DA-20 since receiving his check airman designation. The company Director of Operations reported that the accident FO was the first student the PIC had taken through the initial second-in-command course. The PIC and FO had received all of their turbojet experience with the operator.
Aircraft reference details include registration N183GA, MSN 147, year of manufacture 1968.
Geospatial coordinates for this crash are approximately 41.5864°, -83.8131°.
Fatalities
Total
3
Crew
2
Passengers
1
Other
0
Crash Summary
The flight crew of the Fan Jet Falcon (DA-20) were practicing ILS approaches in instrument meteorological conditions with low clouds and rime ice. A first officer (FO) in training occupied the right seat, while the pilot-in-command (PIC), who was also the company chief pilot/check airman/designated flight instructor, occupied the left seat and was handling the radios. On the second approach, the airplane struck trees and burned, 1.57 nm from approach end of the runway. The landing gear was found extended, and the trailing edge and droop leading edge flaps were retracted. The wing and engine cowl anti-ice valves were found closed, consistent with it being off in the cockpit. Radar data revealed that on approach, the airspeed decreased from 188 knots to 141 knots at the outer marker, and continued to decrease down to 106 knots, when the airplane entered an abrupt descent and disappeared from radar. Simulator flights matched the radar profile with a flight idle approach, a power reduction inside the outer marker, and 1/4 inch of ice on the wings. In the simulator, the airplane stalled about 2 miles from the end of the runway with an airspeed of 103 kts. At flight idle, the engine power in the last 2 minutes of approach was below the recommended power setting for wing or engine anti-ice to be effective. Vref and stall speeds were computed to be 129 kts and 96 kts, with wing flaps and droop leading edges retracted. The PIC had about 1,100 hours in the make and model. The PIC did not have any documented previous flight instruction experience in make and model or any other multi-engine airplanes. The PIC had given 4 pilot proficiency checks in the DA-20 since receiving his check airman designation. The company Director of Operations reported that the accident FO was the first student the PIC had taken through the initial second-in-command course. The PIC and FO had received all of their turbojet experience with the operator.
Cause: Human factor
Occupants & Outcome
Crew On Board
2
Passengers On Board
1
Estimated Survivors
0
Fatality Rate
100.0%
Known people on board: 3
Operational Details
Schedule / Flight
Traverse City – Toledo
Flight Type
Training
Flight Phase
Landing (descent or approach)
Crash Site
Airport (less than 10 km from airport)
Region / Country
North America • United States of America
