Cleveland - Columbus

The airplane was destroyed by impact forces and fire after it impacted the intersection of runway 23 and 32 while attempting a missed-approach. The pilot's crew day started at 1300 and the 14 hour duty limit was 0300 the following morning. The second leg of the flight was delayed 1 hour and 36 minutes due to a freight delay. The operator reported the pilot exceeded his 14 hour crew day by 45 minutes as a result of the freight delay. The flight was cleared for the runway 23 ILS instrument approach. A witness, who was monitoring the Unicom radio frequency, reported that he heard clicking sounds on the Unicom frequency (to bring up the runway light intensity), but the pilot did not make any radio transmissions. The witness reported the ground fog was very thick. Two witnesses reported they heard the airplane's engines. They then heard the engines go to "full power," and then they heard the airplane impact the ground. They saw an initial flash, but could not see the airplane on fire from 2,500 feet away. FAR 135.213 requires that, "Weather observations made and furnished to pilots to conduct IFR operations at an airport must be made at the airport where those IFR operations are conducted." The destination did not have authorized weather reporting, and the operator's Operating Specifications did not list an alternate weather reporting source. At 0253, the observed weather 20 miles to the north, indicated the following: winds 190 at 4 knots, 1/4 statute mile visibility, fog, indefinite ceilings 100 feet, temperature 22 degrees C, dew point 22 degrees C, altimeter 30.00. From the initial point of impact (POI), the wreckage path continued for about 210 feet on a heading of about 180 degrees. The outboard section of the left wing outboard of the nacelle was found on runway 32, about 85 feet from the POI. Separated, unburned, portions of the left aileron and left flap were also found on the runway. The remaining pieces of the left wing were located with the main wreckage. The right wing was located with the main wreckage and the entire span of the right wing from the wing root to the wingtip exhibited continuity. The inspection of the airplane revealed no preexisting anomalies.

Flight / Schedule

Cleveland - Columbus

Registration

N158GA

MSN

60-0608-7961195

Year of Manufacture

1979

Date

July 18, 2002 at 03:45 AM

Type

CRASH

Flight Type

Cargo

Flight Phase

Landing (descent or approach)

Crash Site

Airport (less than 10 km from airport)

Crash Location

Columbus-Municipal (Bakalar) Indiana

Region

North America • United States of America

Crash Cause

Human factor

Narrative Report

On July 18, 2002 at 03:45 AM, Cleveland - Columbus experienced a crash involving Piper PA-60 Aerostar (Ted Smith 600), operated by Grand Aire Express - Executive Aire Express, with the event recorded near Columbus-Municipal (Bakalar) Indiana.

The flight was categorized as cargo and the reported phase was landing (descent or approach) at a airport (less than 10 km from airport) crash site.

1 people were known to be on board, 1 fatalities were recorded, 0 survivors were identified or estimated. This corresponds to an estimated fatality rate of 100.0%.

Crew on board: 1, crew fatalities: 1, passengers on board: 0, passenger fatalities: 0, other fatalities: 0.

The listed crash cause is human factor. The airplane was destroyed by impact forces and fire after it impacted the intersection of runway 23 and 32 while attempting a missed-approach. The pilot's crew day started at 1300 and the 14 hour duty limit was 0300 the following morning. The second leg of the flight was delayed 1 hour and 36 minutes due to a freight delay. The operator reported the pilot exceeded his 14 hour crew day by 45 minutes as a result of the freight delay. The flight was cleared for the runway 23 ILS instrument approach. A witness, who was monitoring the Unicom radio frequency, reported that he heard clicking sounds on the Unicom frequency (to bring up the runway light intensity), but the pilot did not make any radio transmissions. The witness reported the ground fog was very thick. Two witnesses reported they heard the airplane's engines. They then heard the engines go to "full power," and then they heard the airplane impact the ground. They saw an initial flash, but could not see the airplane on fire from 2,500 feet away. FAR 135.213 requires that, "Weather observations made and furnished to pilots to conduct IFR operations at an airport must be made at the airport where those IFR operations are conducted." The destination did not have authorized weather reporting, and the operator's Operating Specifications did not list an alternate weather reporting source. At 0253, the observed weather 20 miles to the north, indicated the following: winds 190 at 4 knots, 1/4 statute mile visibility, fog, indefinite ceilings 100 feet, temperature 22 degrees C, dew point 22 degrees C, altimeter 30.00. From the initial point of impact (POI), the wreckage path continued for about 210 feet on a heading of about 180 degrees. The outboard section of the left wing outboard of the nacelle was found on runway 32, about 85 feet from the POI. Separated, unburned, portions of the left aileron and left flap were also found on the runway. The remaining pieces of the left wing were located with the main wreckage. The right wing was located with the main wreckage and the entire span of the right wing from the wing root to the wingtip exhibited continuity. The inspection of the airplane revealed no preexisting anomalies.

Aircraft reference details include registration N158GA, MSN 60-0608-7961195, year of manufacture 1979.

Fatalities

Total

1

Crew

1

Passengers

0

Other

0

Crash Summary

The airplane was destroyed by impact forces and fire after it impacted the intersection of runway 23 and 32 while attempting a missed-approach. The pilot's crew day started at 1300 and the 14 hour duty limit was 0300 the following morning. The second leg of the flight was delayed 1 hour and 36 minutes due to a freight delay. The operator reported the pilot exceeded his 14 hour crew day by 45 minutes as a result of the freight delay. The flight was cleared for the runway 23 ILS instrument approach. A witness, who was monitoring the Unicom radio frequency, reported that he heard clicking sounds on the Unicom frequency (to bring up the runway light intensity), but the pilot did not make any radio transmissions. The witness reported the ground fog was very thick. Two witnesses reported they heard the airplane's engines. They then heard the engines go to "full power," and then they heard the airplane impact the ground. They saw an initial flash, but could not see the airplane on fire from 2,500 feet away. FAR 135.213 requires that, "Weather observations made and furnished to pilots to conduct IFR operations at an airport must be made at the airport where those IFR operations are conducted." The destination did not have authorized weather reporting, and the operator's Operating Specifications did not list an alternate weather reporting source. At 0253, the observed weather 20 miles to the north, indicated the following: winds 190 at 4 knots, 1/4 statute mile visibility, fog, indefinite ceilings 100 feet, temperature 22 degrees C, dew point 22 degrees C, altimeter 30.00. From the initial point of impact (POI), the wreckage path continued for about 210 feet on a heading of about 180 degrees. The outboard section of the left wing outboard of the nacelle was found on runway 32, about 85 feet from the POI. Separated, unburned, portions of the left aileron and left flap were also found on the runway. The remaining pieces of the left wing were located with the main wreckage. The right wing was located with the main wreckage and the entire span of the right wing from the wing root to the wingtip exhibited continuity. The inspection of the airplane revealed no preexisting anomalies.

Cause: Human factor

Occupants & Outcome

Crew On Board

1

Passengers On Board

0

Estimated Survivors

0

Fatality Rate

100.0%

Known people on board: 1

Operational Details

Schedule / Flight

Cleveland - Columbus

Flight Type

Cargo

Flight Phase

Landing (descent or approach)

Crash Site

Airport (less than 10 km from airport)

Region / Country

North America • United States of America

Aircraft Details

Registration

N158GA

MSN

60-0608-7961195

Year of Manufacture

1979