De Havilland DHC-8-100 (Dash-8)
Safety Rating
9.2/10Total Incidents
9
Total Fatalities
70
Incident History
Skyward Express
The airplane departed Nairobi-Wilson Airport on a charter flight to El Wak, carrying 37 passengers and 4 crew members. While descending to El Wak Airport, the pilot continued to the east and elected to land on an airfield located 18 km east of El Wak, near Bur Ache, in Somalia. After landing, the airplane veered to the left and impacted a pile of earth and rocks, causing the left main gear to collapse. All 41 occupants evaacuated safely and the aircraft was damaged beyond repair.
Airlines PNG
On the afternoon of 13 October 2011, an Airlines PNG Bombardier DHC-8-103, registered P2-MCJ (MCJ), was conducting a regular public transport flight from Nadzab, Morobe Province, to Madang, Madang Province under the Instrument Flight Rules (IFR). On board the aircraft were two flight crew, a flight attendant, and 29 passengers. Earlier in the afternoon, the same crew had flown MCJ from Port Moresby to Nadzab. The autopilot could not be used because the yaw damper was unserviceable so the aircraft had to be hand-flown by the pilots. At Nadzab, the aircraft was refuelled with sufficient fuel for the flight to Madang and a planned subsequent flight from Madang to Port Moresby. MCJ departed Nadzab at 1647 LMT with the Pilot-in-Command as the handling pilot. The aircraft climbed to 16,000 ft with an estimated arrival time at Madang of 1717. Once in the cruise, the flight crew diverted right of the flight planned track to avoid thunderstorms and cloud. The Pilot-in-Command reported that communications between Madang Tower and an aircraft in the vicinity of Madang indicated a storm was approaching the aerodrome. He recalled that he had intended to descend below the cloud in order to be able to see across the sea to Madang and had been concentrating on manoeuvring the aircraft to remain clear of thunderstorms and cloud, so he had been looking mainly outside the cockpit. Because of the storm in the vicinity of the airport, he said there had been „some urgency<U+201F> to descend beneath the cloud base to position for a right base for runway 07 at Madang, the anticipated approach. On this route, the descent to Madang was steep (because of the need to remain above the Finisterre Ranges until close to Madang) and, although the aircraft was descending steeply, the propellers were at their cruise setting of 900 revolutions per minute (RPM). Neither pilot noticed the airspeed increasing towards the maximum operating speed (VMO); the Pilot-in-Command reported afterwards that he had been „distracted<U+201F> by the weather. When the aircraft reached VMO as it passed through 10,500 ft, with a rate of descent between 3,500 and 4,200 ft per minute, and the propellers set at 900 RPM, the VMO overspeed warning sounded. The Pilot-in-command reported that he had been about to ask the First Officer to increase the propeller speed to 1,050 RPM to slow the aircraft when this occurred. He raised the nose of the aircraft in response to the warning and this reduced the rate of descent to about 2,000 ft per minute, however, the VMO overspeed warning continued. The First Officer recalled the Pilot-in-Command moved the power levers back „quite quickly<U+201F>. Shortly after the power levers had been moved back, both propellers oversped simultaneously, exceeding their maximum permitted speed of 1,200 RPM by over 60 % and seriously damaging the left hand engine and rendering both engines unusable. Villagers on the ground reported hearing a loud „bang<U+201F> as the aircraft passed overhead. The noise in the cockpit was deafening, rendering communication between the pilots extremely difficult, and internal damage to the engines caused smoke to enter the cockpit and cabin through the bleed air and air conditioning systems. The emergency caught both pilots by surprise. There was confusion and shock on the flight deck, a situation compounded by the extremely loud noise from the overspeeding propellers. About four seconds after the double propeller overspeed began, the beta warning horn started to sound intermittently, although the pilots stated afterwards they did not hear it. The left propeller RPM reduced to 900 RPM (in the governing range) after about 10 seconds. It remained in the governing range for about 5 seconds before overspeeding again for about 15 seconds, then returned to the governing range. During this second overspeed of the left propeller, the left engine high speed compressor increased above 110 % NH, becoming severely damaged in the process. About 3 seconds after the left propeller began overspeeding for the second time, the right propeller went into uncommanded feather due to a propeller control unit (PCU) beta switch malfunction, while the right engine was still running at flight idle (75% NH). Nine seconds after the double propeller overspeed event began, the Pilot-in-command shouted to the First Officer „what have we done?<U+201F> The First Officer replied there had been a double propeller overspeed. The Pilot-in-command then shouted a second and third time „what have we done?<U+201F>. The First Officer repeated that there was a double propeller overspeed and said that the right engine had shut down. The Pilot-in-Command shouted that he could not hear the First Officer, who – just as the left propeller began governing again and the overspeed noise subsided – repeated that the right engine had shut down and asked if the left engine was still working. The Pilot-in-command replied that it was not working. Both pilots then agreed that they had „nothing<U+201F>. At this point, about 40 seconds after the propeller overspeed event began, the left propeller was windmilling and the left engine was no longer producing any power because of the damage caused to it by the overspeed. The right engine was operating at flight idle, although the propeller could not be unfeathered and therefore could not produce any thrust. On the order of the Pilot-in-Command, the First Officer made a mayday call to Madang Tower and gave the aircraft's GPS position; he remained in a radio exchange with Madang Tower for 63 seconds. The flight crew did not conduct emergency checklists and procedures. Instead, their attention turned to where they were going to make a forced landing. The aircraft descended at a high rate of descent, with the windmilling left propeller creating extra drag. The asymmetry between the windmilling left propeller and the feathered right propeller made the aircraft difficult to control. The average rate of descent between the onset of the emergency and arrival at the crash site was 2,500 ft per minute and at one point exceeded 6,000 ft per minute, and the VMO overspeed warning sounded again. During his long radio exchange with Madang Tower, the First Officer had said that they would ditch the aircraft, although, after a brief discussion, the Pilot-in-command subsequently decided to make a forced landing in the mouth of the Guabe River. The First Officer asked the Pilot-in-command if he should shut both engines down and the Pilot-in-command replied that he should shut „everything<U+201F> down. Approximately 800 feet above ground level and 72 seconds before impact, the left propeller was feathered and both engines were shut down. The Pilot-in-Command reported afterwards that he ultimately decided to land beside the river instead of in the river bed because the river bed contained large boulders. The area chosen beside the river bed also contained boulders beneath the vegetation, but they were not readily visible from the air. He recalled afterwards that he overshot the area he had originally been aiming for. The aircraft impacted terrain at 114 knots with the flaps and the landing gear retracted. The Flight Attendant, who was facing the rear of the aircraft, reported that the tail impacted first. During the impact sequence, the left wing and tail became detached. The wreckage came to rest 300 metres from the initial impact point and was consumed by a fuel-fed fire. The front of the aircraft fractured behind the cockpit and rotated through 180 degrees, so that it was inverted when it came to rest. Of the 32 occupants of the aircraft only the two pilots, the flight attendant, and one passenger survived by escaping from the wreckage before it was destroyed by fire.
Flugfélag Íslands
The flight crew got visual contact with the runway at BGGH and decided to deviate to the right (west) of the offset localizer (LLZ) to runway 23. The flight continued towards the runway from a position right of the extended runway centerline. As the aircraft approached runway 23, it was still in the final right turn over the landing threshold. The aircraft touched down on runway 23 between the runway threshold and the touchdown zone and to the left of the runway centerline. The right main landing gear (MLG) shock strut fuse pin sheared leading to a right MLG collapse. The aircraft skidded down the runway and departed the runway to the right. Neither passengers nor crew suffered any injuries. The aircraft was substantially damaged. The accident occurred in daylight under visual meteorological conditions (VMC).
DAC Aviation
The aircraft departed Nairobi on a humanitarian mission to Moba, carrying 18 passengers and 4 crew members on behalf of the United Nations Organization. After touchdown, the left main gear collapsed. The aircraft veered off runway to the left and came to rest in a marsh field. All 22 occupants escaped uninjured and the aircraft was damaged beyond repair. It appears that the pilot-in-command was distracted during the last segment by pedestrians at the runway threshold and the aircraft landed hard.
Wideroe - Wideroe's Flyveselskap
Widerøe flight WIF 921 took off from Tromsø airport (ENTC) at time 1401 with an estimated landing time at Hammerfest airport (ENHF) 1442. On board the aircraft, a DHC-8-103 with registration LN-WIK, were a crew of two pilots and one cabin attendant, 26 fare paying passengers and one passive cabin attendant. The crew had taken off from ENHF earlier in the day, when the weather and wind did not cause any problems. During the approach to ENHF the crew was informed about variable and occasional gusty wind from south-east. The wind direction favoured runway 23 and the crew planned the landing accordingly. The copilot was Pilot Flying (PF) and the commander was Pilot Not Flying (PNF). The copilot was newly hired and was flying under supervision. The crew was kept updated on the wind conditions by the AFIS operator, and at times the gusty wind conditions favoured runway 05. The copilot left the control to the commander who continued the approach to runway 05. Just before landing the wind direction veered to the right and increased in strength, resulting in a significant tail wind component. This resulted in a marked increase in the descent rate which the commander tried to stop by advancing to full power. However, the altitude was too low and the airplane touched down hard just inside the runway edge on runway 05. At touch down the right main landing gear leg failed. The airplane slid on the belly, right partly retracted main wheel and wing tip for some 650 m, and stopped just after the second (TWY B) turnoff to the apron. The fire and rescue vehicles were quickly at the scene and sprayed foam on the plane to prevent fire. The cabin attendant calmed the passengers who wanted to get out of the plane quickly due to smoke and burned smell in the cabin. It took 33 seconds from the commander ordered evacuation until this was initiated. The delay was mainly caused by the fact that the order did not get through the cabin’s Public Address (PA) system.
Wideroe - Wideroe's Flyveselskap
The twin engine aircraft departed Alta Airport at 1522LT on a regular schedule service to Båtsfjord, carrying 24 passengers and a crew of three. Following an uneventful flight, the crew started a LOC/DME approach to runway 21. Shortly after passing the missed approach point, the pilot-in-command lost visual contact with the runway so the captain took over controls and continued the approach. The airplane became unstable and the crew encountered control problems due to difficulties to disengage the autopilot system. This caused the aircraft to lose height during the last segment and it landed hard, causing the right main gear to collapse upon impact. The aircraft slid for few dozen metres then veered off runway to the right and came to rest in a grassy area 23 metres to the right of the runway. All 27 occupants evacuated safely while the aircraft was damaged beyond repair.
Ansett New Zealand - ANZ
At 08:17 Ansett New Zealand Flight 703 departed Auckland (AKL) as scheduled bound for Palmerston North (PMR). To the north of Palmerston North the pilots briefed themselves for a VOR/DME approach to runway 07 which was the approach they preferred. Subsequently Air Traffic Control specified the VOR/DME approach for runway 25, due to departing traffic, and the pilots re-briefed for that instrument approach. The IMC involved flying in and out of stratiform cloud, but continuous cloud prevailed during most of the approach. The aircraft was flown accurately to join the 14 nm DME arc and thence turned right and intercepted the final approach track of 250° M to the Palmerston North VOR. During the right turn, to intercept the inbound approach track, the aircraft’s power levers were retarded to 'flight idle' and shortly afterwards the first officer advised the captain ".... 12 DME looking for 4000 (feet)". The final approach track was intercepted at approximately 13 DME and 4700 feet, and the first officer advised Ohakea Control "Ansett 703" was "established inbound". Just prior to 12 miles DME the captain called "Gear down". The first officer asked him to repeat what he had said and then responded "OK selected and on profile, ten - sorry hang on 10 DME we’re looking for four thousand aren’t we so - a fraction low". The captain responded, "Check, and Flap 15". This was not acknowledged but the first officer said, "Actually no, we’re not, ten DME we’re..... (The captain whistled at this point) look at that". The captain had noticed that the right hand main gear had not locked down: "I don’t want that." and the first officer responded, "No, that’s not good is it, so she’s not locked, so Alternate Landing Gear...?" The captain acknowledged, "Alternate extension, you want to grab the QRH?" After the First Officer’s "Yes", the captain continued, "You want to whip through that one, see if we can get it out of the way before it’s too late." The captain then stated, "I’ll keep an eye on the airplane while you’re doing that." The first officer located the appropriate "Landing Gear Malfunction Alternate Gear Extension" checklist in Ansett New Zealand’s Quick Reference Handbook (QRH) and began reading it. He started with the first check on the list but the captain told him to skip through some checks. The first officer responded to this instruction and resumed reading and carrying out the necessary actions. It was the operator’s policy that all items on the QRH checklists be actioned, or proceeded through, as directed by the captain. The first officer started carrying out the checklist. The captain in between advised him to pull the Main Gear Release Handle. Then the GPWS’s audio alarm sounded. Almost five seconds later the aircraft collided with terrain. The Dash 8 collided with the upper slope of a low range of hills.
Bangkok Airways
On final approach to Koh Samui Airport runway 35, the aircraft entered an area of heavy rain falls. As the crew was unable to locate the runway, the captain decided to initiate a go-around procedure. With flaps fully extended, the crew increased power and started to gain height when the aircraft rolled to the left to an angle of 75° then entered an uncontrolled descent and crashed at a speed of 147 knots about 5 km short of runway threshold. The aircraft disintegrated on impact and all 38 occupants were killed.
Horizon Air
Shortly after takeoff from Seattle-Tacoma Intl Airport, the crew noted a right engine power loss and decided to return for a precautionary landing. After lowering the landing gear, a massive fire was discovered in the right engine nacelle. After landing, directional control and all braking were lost. The aircraft departed the left side of the runway 16L after the left power lever was moved to flight idle. The f/o advised tower that the aircraft was out of control. The aircraft rolled onto the ramp area where it struck a runway designator sign, ground equipment, and jetways B7 and B9. The aircraft was subsequently destroyed by fire. Investigation revealed that during overhaul the high pressure fuel filter cover was improperly installed on the engine and the improper installation was not discovered drg company installation of the engine on the aircraft. This led to a massive fuel leak and the nacelle fire. The fire/explosion caused the loss of the engine panels, reducing the effectiveness of the fire suppression system and allowing other systems to be damaged.
Safety Profile
Reliability
Reliable
This rating is based on historical incident data and may not reflect current operational safety.
