Phoenix Air - USA
Safety Score
9.9/10Total Incidents
4
Total Fatalities
3
Recent Incidents
Douglas C-47 Skytrain (DC-3)
The pilot stated that on initial climb, at about 400 feet agl, the crew smelled something burning, followed by light smoke in the cabin. Both engines appeared normal visually. The odor and smoke increased, and the left fire warning light illuminated. The left engine was shut down and the prop feathered. The pilot increased power on the right engine; however, the airplane would not climb or maintain airspeed. A gear and flaps up forced landing was made into a field. The pilot stated that he believed an exhaust clamp broke allowing a segment of exhaust to scorch cowling and activate the fire warning system. Examination of the left engine revealed that the lower fire detection elements were fused and broken free, and that the hydraulic lines were burned through.
Dassault Falcon 20
The crew arrived at the airport about 20 minutes before the planned midnight takeoff time, after the pilot-in-command had spent the day moving furniture. A night watchman noted that the preflight inspection and takeoff roll to rotation/lift-off was normal. There was no post-takeoff radio call to either unicom or ATC, although the crew had filed an IFR flight plan. After taking off from runway 36, the aircraft crashed about 1.8 mile north of the runway. The wreckage was found after interruption of electrical power to a nearby city. Initial impact was with trees, while in a shallow/left/descending turn. An area of trees about 1/2 mile long was damaged by impact and fire. Before coming to rest, the aircraft hit a powerline support tower. There was evidence the aircraft was traveling at about 260 knots, when it crashed. No preimpact part failure or malfunction was found that would have resulted in the accident. Both pilots were killed.
Beechcraft 65 Queen Air
The aircraft was found crashed in shallow water near Key Largo, FL. Attempts to locate the pilot or current operator were fruitless. The circumstances surrounding the crash and the cause are unknown.
Beechcraft H18
The flight had not yet been scheduled when the pilot retired for the evening at 2230 to 2300 est. At 0230, he was awoken and notified to make a night cargo flight. The owner obtained a weather briefing and filed a flight plan, then briefed the pilot later. The pilot arrived at the airport at 0430. He preflighted the aircraft while the owner updated the weather briefing. The aircraft was cleared as filed with a clearance void time of 0500; the clearance was radioed to the pilot by unicom. During takeoff, at 0510, the aircraft was observed climbing northbound to aprx 800 feet agl in moderate snowfall with the landing light on. A short time later, the aircraft crashed approximately one mile northeast of the airport while in a steep nose down, right wing low attitude. No pre- impact part failure/malfunction was found. Reportedly, when the pilot 1st hired on, he exaggerated his flight experience; he had problems with instrument flying and was not scheduled for flights in marginal weather; and he was given extra help. At the time of the accident, snow was falling, mixed icing was forecast in clouds and there was a sigmet for moderate to severe turbulences below 8,000 feet. The pilot, sole on board, was killed.
Airline Information
Country of Origin
United States of America
Risk Level
Low Risk
