Convair C-131 Samaritan

Historical safety data and incident record for the Convair C-131 Samaritan aircraft.

Safety Rating

9/10

Total Incidents

8

Total Fatalities

80

Incident History

February 8, 2019 1 Fatalities

Conquest Air Cargo

Miami Florida

According to the first officer, during the first cargo flight of the day, the left engine propeller control was not working properly and the captain indicated that they would shut down the airplane and contact maintenance if the left engine propeller control could not be reset before the return flight. For the return flight, the engines started normally, and both propellers were cycled. The captain and the first officer were able to reset the left propeller control, so the airplane departed with the first officer as the pilot flying. The takeoff and initial climb were normal; however, as the airplane climbed through 4,000 ft, the left engine propeller control stopped working and the power was stuck at 2,400 rpm. The captain tried to adjust the propeller control and inadvertently increased power to 2,700 rpm. The captain then took control of the airplane and tried to stabilize the power on both engines. He leveled the airplane at 4,500 ft, canceled the instrument flight rules flight plan, and flew via visual flight rules direct toward the destination airport. The first officer suggested that they return to the departure airport, but the captain elected to continue as planned (The destination airport was located about 160 nautical miles from the departure airport). The first officer's postaccident statements indicated that he did not challenge the captain's decision. When the flight began the descent to 1,500 ft, the right engine began to surge and lose power. The captain and the first officer performed the engine failure checklist, and the captain feathered the propeller and shut down the engine. Shortly afterward, the left engine began to surge and lose power. The captain told the first officer to declare an emergency. The airplane continued to descend, and the airplane impacted the water "violently," about 32 miles east of the destination airport. The captain was unresponsive after the impact and the first officer was unable to lift the captain from his seat. Because the cockpit was filling rapidly with water, the first officer grabbed the life raft and exited the airplane from where the tail section had separated from the empennage. The first officer did not know what caused both engines to lose power. The airplane was not recovered from the ocean, so examination and testing to determine the cause of the engine failures could not be performed. According to the operator, the flight crew should have landed as soon as practical after the first sign of a mechanical issue. Thus, the crew should have diverted to the closest airport when the left engine propeller control stopped working and not continued the flight toward the destination airport.

February 5, 1996 4 Fatalities

Business Air Connection

Saint Johns-Industrial Arizona

Witnesses observed the aircraft departing from runway 14 with a rolling start. They said the aircraft rotated at the departure end of the runway and remained in ground effect with an excessive, nose high attitude. It then struck the airport perimeter fence, a barrier wall, and power lines. Power line wires were dragged through a residential area, resulting in additional damage. The airplane then crashed in a pasture and burned. Investigation revealed the airplane had been loaded to a gross weight (GW) of 50,870 lbs. Its maximum GW was limited to 48,000 lbs at sea level with the use of antidetonation injection (ADI) fluid and 40,900 lbs without ADI. Density altitude at the airport was 6200 feet. For conditions at the airport, maximum GW for takeoff with ADI and 15° of flaps was 43,205 lbs; without ADI and with 13 degrees of flaps, maximum GW was 38,909 lbs. The airplane flaps were found in the retracted position, but there was no performance data for takeoff with the flaps retracted. No ADI fluid was found in the line to the right engine, although it was intact; the ADI tank was destroyed; the ADI line to the left engine was damaged. The airplane was being flown under provision of a ferry permit, which did not provide for the cargo or the two passengers that were aboard. The first pilot (PIC) had accrued about 8 hours of flight experience in the make and model of airplane.

November 15, 1985 4 Fatalities

United States Navy - USN

Dothan AFB Alabama

The crew (two pilots and two engineers) departed Dothan AFB for a local post maintenance test flight. Just after liftoff, the elevators jammed. The aircraft went out of control and crashed. All four occupants were killed.

April 30, 1983 14 Fatalities

United States Navy - USN

Jacksonville-Towers Field NAS Florida

After takeoff from Jacksonville-Towers Field NAS, while climbing, the left engine failed. The crew declared an emergency and was cleared to return. On final approach, the airplane crashed in the St Johns River about 125 yards short off shore. The aircraft came to rest in shallow waters and was destroyed. A passenger was rescued while 14 other occupants were killed.

United States Coast Guard - USCG

Corpus Christi Texas

The crew was completing a local training flight at Corpus Christi Airport. Following an approach in reduced visibility due to foggy conditions, the airplane landed hard on runway 10R. Upon touchdown, the aircraft went out of control, veered off runway and came to rest. All eight crew members evacuated safely while the aircraft was damaged beyond repair.

Command Aviation

Dillingham Alaska

After takeoff from Dillingham Airport, while on a company ferry flight to Anchorage, the right engine surged at meto power and the crew was forced to shut it down. The decision to return was taken and the crew followed a circuit pattern then started the descent. On final approach, the airplane descended into trees and crashed in a wooded area located few hundred yards short of runway 01. The aircraft was destroyed while all three occupants escaped with minor injuries.

United States Navy - USN

Galivan California

The crew was engaged in a local training flight out from El Toro MCAS. After takeoff, while climbing, the airplane went out of control and crashed in the garden of the Saddleback College located about 8 miles southeast of the airfield. Four crew members were killed while two others were injured.

December 17, 1960 53 Fatalities

United States Air Force - USAF

Munich Bavaria

The aircraft was engaged in a special flight from Munich to RAF Northolt, near London, carrying British students who were flying back home for Christmas and a crew of seven. One minute after takeoff from Munich-Riem Airport, while climbing to an altitude of 1,000 meters, the crew informed ground about the failure of the left engine and obtained the permission to return for an emergency landing. Few seconds later, the copilot informed ground that he was unable to control the loss of altitude. In a limited visibility due to fog (800 meters horizontal and 40 meters vertical), the airplane struck the top of the St Paul church with its left wing and crashed in a huge explosion in the center of a commercial district of Munich. The airplane exploded while hitting a tramway, several cars and people and debris were scattered in the street and several shops as well. All 20 occupants on board the aircraft were killed as well as 33 people on the ground, essentially people sitting in the tramway. Nine other people were seriously injured.

Safety Profile

Reliability

Reliable

This rating is based on historical incident data and may not reflect current operational safety.

Primary Operators (by incidents)

United States Navy - USN3
Business Air Connection1
Command Aviation1
Conquest Air Cargo1
United States Air Force - USAF1
United States Coast Guard - USCG1