Saint Johns – Brownsville – Chetumal
Flight / Schedule
Saint Johns – Brownsville – Chetumal
Aircraft
Convair C-131 SamaritanRegistration
N131T
MSN
338
Year of Manufacture
1956
Operator
Business Air ConnectionDate
February 5, 1996 at 09:50 AM
Type
CRASHFlight Type
Cargo
Flight Phase
Takeoff (climb)
Crash Site
Airport (less than 10 km from airport)
Crash Location
Saint Johns-Industrial Arizona
Region
North America • United States of America
Crash Cause
Human factor
Narrative Report
On February 5, 1996 at 09:50 AM, Saint Johns – Brownsville – Chetumal experienced a crash involving Convair C-131 Samaritan, operated by Business Air Connection, with the event recorded near Saint Johns-Industrial Arizona.
The flight was categorized as cargo and the reported phase was takeoff (climb) at a airport (less than 10 km from airport) crash site.
4 people were known to be on board, 4 fatalities were recorded, 0 survivors were identified or estimated. This corresponds to an estimated fatality rate of 100.0%.
Crew on board: 2, crew fatalities: 2, passengers on board: 2, passenger fatalities: 2, other fatalities: 0.
The listed crash cause is human factor. Witnesses observed the aircraft departing from runway 14 with a rolling start. They said the aircraft rotated at the departure end of the runway and remained in ground effect with an excessive, nose high attitude. It then struck the airport perimeter fence, a barrier wall, and power lines. Power line wires were dragged through a residential area, resulting in additional damage. The airplane then crashed in a pasture and burned. Investigation revealed the airplane had been loaded to a gross weight (GW) of 50,870 lbs. Its maximum GW was limited to 48,000 lbs at sea level with the use of antidetonation injection (ADI) fluid and 40,900 lbs without ADI. Density altitude at the airport was 6200 feet. For conditions at the airport, maximum GW for takeoff with ADI and 15° of flaps was 43,205 lbs; without ADI and with 13 degrees of flaps, maximum GW was 38,909 lbs. The airplane flaps were found in the retracted position, but there was no performance data for takeoff with the flaps retracted. No ADI fluid was found in the line to the right engine, although it was intact; the ADI tank was destroyed; the ADI line to the left engine was damaged. The airplane was being flown under provision of a ferry permit, which did not provide for the cargo or the two passengers that were aboard. The first pilot (PIC) had accrued about 8 hours of flight experience in the make and model of airplane.
Aircraft reference details include registration N131T, MSN 338, year of manufacture 1956.
Fatalities
Total
4
Crew
2
Passengers
2
Other
0
Crash Summary
Witnesses observed the aircraft departing from runway 14 with a rolling start. They said the aircraft rotated at the departure end of the runway and remained in ground effect with an excessive, nose high attitude. It then struck the airport perimeter fence, a barrier wall, and power lines. Power line wires were dragged through a residential area, resulting in additional damage. The airplane then crashed in a pasture and burned. Investigation revealed the airplane had been loaded to a gross weight (GW) of 50,870 lbs. Its maximum GW was limited to 48,000 lbs at sea level with the use of antidetonation injection (ADI) fluid and 40,900 lbs without ADI. Density altitude at the airport was 6200 feet. For conditions at the airport, maximum GW for takeoff with ADI and 15° of flaps was 43,205 lbs; without ADI and with 13 degrees of flaps, maximum GW was 38,909 lbs. The airplane flaps were found in the retracted position, but there was no performance data for takeoff with the flaps retracted. No ADI fluid was found in the line to the right engine, although it was intact; the ADI tank was destroyed; the ADI line to the left engine was damaged. The airplane was being flown under provision of a ferry permit, which did not provide for the cargo or the two passengers that were aboard. The first pilot (PIC) had accrued about 8 hours of flight experience in the make and model of airplane.
Cause: Human factor
Occupants & Outcome
Crew On Board
2
Passengers On Board
2
Estimated Survivors
0
Fatality Rate
100.0%
Known people on board: 4
Operational Details
Schedule / Flight
Saint Johns – Brownsville – Chetumal
Operator
Business Air ConnectionFlight Type
Cargo
Flight Phase
Takeoff (climb)
Crash Site
Airport (less than 10 km from airport)
Region / Country
North America • United States of America
Aircraft Details
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