Williston - Fargo
Flight / Schedule
Williston - Fargo
Aircraft
Cessna 550 Citation IIRegistration
N941JM
MSN
550-0146
Year of Manufacture
1980
Operator
Dirt DynamicsDate
November 30, 2018 at 01:53 PM
Type
CRASHFlight Type
Private
Flight Phase
Landing (descent or approach)
Crash Site
Airport (less than 10 km from airport)
Crash Location
Fargo-Hector North Dakota
Region
North America • United States of America
Crash Cause
Human factor
Narrative Report
On November 30, 2018 at 01:53 PM, Williston - Fargo experienced a crash involving Cessna 550 Citation II, operated by Dirt Dynamics, with the event recorded near Fargo-Hector North Dakota.
The flight was categorized as private and the reported phase was landing (descent or approach) at a airport (less than 10 km from airport) crash site.
11 people were known to be on board, 0 fatalities were recorded, 11 survivors were identified or estimated. This corresponds to an estimated fatality rate of 0.0%.
Crew on board: 1, crew fatalities: 0, passengers on board: 10, passenger fatalities: 0, other fatalities: 0.
The listed crash cause is human factor. The commercial pilot was conducting a cross-country, business flight with 10 passengers onboard the 8-passenger airplane. He reported that air traffic control cleared the flight for an instrument landing system (ILS) approach to the runway. While descending, the airplane entered instrument meteorological conditions (IMC) at 3,100 ft mean sea level (msl), and ice started to accumulate on the wing's leading edges, empennage, and windshield. The pilot activated the pneumatic deice boots multiple times during the approach and slowed the airplane to 120 knots. The airplane then exited the clouds about 400 ft above ground level (agl), and the pilot maintained 120 knots as the airplane flew over the airport fence; all indications for landing were normal. About 100 ft agl, the airplane started to pull right. He applied left correction inputs, but the airplane continued to pull right. He applied engine power to conduct a goaround, but the airplane landed in grass right of the runway, sustaining damage to the wings and landing gear. Witnesses and passengers reported that the airplane stalled. During examination of the airplane immediately after the accident, about 1/2 to 1 inch of mixed ice was found on the right wing's leading edge, the vertical and horizontal stabilizers, and the angle of attack probe. Ice was also observed on the windshield. The flaps were found in the "up" position. Flight control continuity was established. Although the airplane was originally certificated for two-pilot operation, the pilot was flying the airplane under a single-pilot exemption. The pilot received a logbook endorsement indicating that he had received single-pilot training and was properly qualified under the single-pilot exemption. However, he had not met the turbine flight time qualifications (1,000 hours) to be properly authorized to conduct the flight under the single-pilot exemption because he only had 500 hours. A review of cockpit voice recorder information indicated that, although the pilot verbalized that the landing gear was "all green," followed by stating "check, check, check," he did not verbalize all the approach or landing checklist items nor did he make any audible comments about activating the pneumatic deice boots or windshield anti-ice. A review of radar data for the flight indicated that, during the last 2 minutes of flight, while the airplane was on final approach to the runway, the indicated airspeed got as low as 99 knots. The last recorded radar return indicated that the airplane had an airspeed of 104 knots at 900 ft msl. The pilot's lack of minimum flight experience required to fly the airplane without a copilot likely led to task saturation as he flew the airplane entered IMC and icing conditions while on an ILS approach. He subsequently failed to lower the flaps during the approach, which resulted in a no-flap approach instead of a full-flap landing. The ice on the leading edges of the wings, the no-flap approach, and the low airspeed likely led to the exceedance of the airplane's critical angle of attack, which resulted in an aerodynamic stall.
Aircraft reference details include registration N941JM, MSN 550-0146, year of manufacture 1980.
Fatalities
Total
0
Crew
0
Passengers
0
Other
0
Crash Summary
The commercial pilot was conducting a cross-country, business flight with 10 passengers onboard the 8-passenger airplane. He reported that air traffic control cleared the flight for an instrument landing system (ILS) approach to the runway. While descending, the airplane entered instrument meteorological conditions (IMC) at 3,100 ft mean sea level (msl), and ice started to accumulate on the wing's leading edges, empennage, and windshield. The pilot activated the pneumatic deice boots multiple times during the approach and slowed the airplane to 120 knots. The airplane then exited the clouds about 400 ft above ground level (agl), and the pilot maintained 120 knots as the airplane flew over the airport fence; all indications for landing were normal. About 100 ft agl, the airplane started to pull right. He applied left correction inputs, but the airplane continued to pull right. He applied engine power to conduct a goaround, but the airplane landed in grass right of the runway, sustaining damage to the wings and landing gear. Witnesses and passengers reported that the airplane stalled. During examination of the airplane immediately after the accident, about 1/2 to 1 inch of mixed ice was found on the right wing's leading edge, the vertical and horizontal stabilizers, and the angle of attack probe. Ice was also observed on the windshield. The flaps were found in the "up" position. Flight control continuity was established. Although the airplane was originally certificated for two-pilot operation, the pilot was flying the airplane under a single-pilot exemption. The pilot received a logbook endorsement indicating that he had received single-pilot training and was properly qualified under the single-pilot exemption. However, he had not met the turbine flight time qualifications (1,000 hours) to be properly authorized to conduct the flight under the single-pilot exemption because he only had 500 hours. A review of cockpit voice recorder information indicated that, although the pilot verbalized that the landing gear was "all green," followed by stating "check, check, check," he did not verbalize all the approach or landing checklist items nor did he make any audible comments about activating the pneumatic deice boots or windshield anti-ice. A review of radar data for the flight indicated that, during the last 2 minutes of flight, while the airplane was on final approach to the runway, the indicated airspeed got as low as 99 knots. The last recorded radar return indicated that the airplane had an airspeed of 104 knots at 900 ft msl. The pilot's lack of minimum flight experience required to fly the airplane without a copilot likely led to task saturation as he flew the airplane entered IMC and icing conditions while on an ILS approach. He subsequently failed to lower the flaps during the approach, which resulted in a no-flap approach instead of a full-flap landing. The ice on the leading edges of the wings, the no-flap approach, and the low airspeed likely led to the exceedance of the airplane's critical angle of attack, which resulted in an aerodynamic stall.
Cause: Human factor
Occupants & Outcome
Crew On Board
1
Passengers On Board
10
Estimated Survivors
11
Fatality Rate
0.0%
Known people on board: 11
Operational Details
Schedule / Flight
Williston - Fargo
Operator
Dirt DynamicsFlight Type
Private
Flight Phase
Landing (descent or approach)
Crash Site
Airport (less than 10 km from airport)
Region / Country
North America • United States of America
