McAlester – Idabel
Flight / Schedule
McAlester – Idabel
Aircraft
Beechcraft 90 King AirRegistration
N1551C
MSN
LJ-1365
Year of Manufacture
1994
Operator
EagleMedDate
February 14, 2017 at 11:45 AM
Type
CRASHFlight Type
Ambulance
Flight Phase
Flight
Crash Site
Plain, Valley
Crash Location
Rattan Oklahoma
Region
North America • United States of America
Coordinates
34.2004°, -95.4130°
Crash Cause
Human factor
Narrative Report
On February 14, 2017 at 11:45 AM, McAlester – Idabel experienced a crash involving Beechcraft 90 King Air, operated by EagleMed, with the event recorded near Rattan Oklahoma.
The flight was categorized as ambulance and the reported phase was flight at a plain, valley crash site.
3 people were known to be on board, 0 fatalities were recorded, 3 survivors were identified or estimated. This corresponds to an estimated fatality rate of 0.0%.
Crew on board: 1, crew fatalities: 0, passengers on board: 2, passenger fatalities: 0, other fatalities: 0.
The listed crash cause is human factor. The pilot stated that the engine start and airplane power-up were normal for the air medical flight with two medical crewmembers. The engine ice vanes were lowered (as required for ground operations) and then were subsequently raised before takeoff. Takeoff and climbout were routine, and the pilot leveled off the airplane at the assigned cruise altitude. The air traffic controller informed the pilot of heavy showers near the destination airport, and the pilot "put the ice vanes down." The pilot indicated that, shortly afterward, the airplane experienced two "quick" electrical power fluctuations in which "everything went away and then came back," and "[s]econds later the entire [electrical] system failed." Due to the associated loss of navigation capability while operating in instrument meteorological conditions (IMC), the pilot set a general course for better weather conditions based on information from his preflight weather briefing. While the pilot attempted to find a suitable hole in the clouds to descend through under visual conditions, the left engine lost power. The pilot ultimately located a field through the cloud cover and executed a single-engine off-airport landing, which resulted in substantial damage to the right engine mount and firewall. A postaccident examination of the airplane and systems did not reveal any anomalies consistent with an in-flight electrical system malfunction. The three-position ignition and engine start/starter-only switches were in the ON position, and the engine anti-ice switches were in the ON position. When the airplane battery was initially checked during the examination, the voltmeter indicated 10.7 volts (normal voltage is 12 volts); the battery was charged and appeared to function normally thereafter. The loss of electrical power was likely initiated by the pilot inadvertently selecting the engine start switches instead of the engine anti-ice (ice vane) switches. This resulted in the starter/generators changing to starter operation and taking the generator function offline. Airplane electrical power was then being supplied solely by the battery, which caused it to deplete and led to a subsequent loss of electrical power to the airplane. A postaccident examination revealed that neither wing fuel tank contained any visible fuel. The left nacelle fuel tank did not contain any visible fuel, and the right nacelle fuel tank appeared to contain about 1 quart of fuel. The lack of fuel onboard at the time of the accident is consistent with a loss of engine power due to fuel exhaustion. This was a result of the extended flight time as the pilot attempted to exit instrument conditions after the loss of electrical power to locate a suitable airport. Further, the operator reported that 253 gallons (1,720 lbs) of fuel were on board at takeoff, and the accident flight duration was 3.65 hours. At maximum range power, the expected fuel consumption was about 406 lbs/hour, resulting in an endurance of about 4.2 hours. Thus, the pilot did not have the adequate fuel reserves required for flying in IMC. Both the pilot and medical crewmembers described a lack of communication and coordination among crewmembers as the emergency transpired. This resulted in multiple course adjustments that hindered the pilot's ability to locate visual meteorological conditions before the left engine fuel supply was exhausted.
Aircraft reference details include registration N1551C, MSN LJ-1365, year of manufacture 1994.
Geospatial coordinates for this crash are approximately 34.2004°, -95.4130°.
Fatalities
Total
0
Crew
0
Passengers
0
Other
0
Crash Summary
The pilot stated that the engine start and airplane power-up were normal for the air medical flight with two medical crewmembers. The engine ice vanes were lowered (as required for ground operations) and then were subsequently raised before takeoff. Takeoff and climbout were routine, and the pilot leveled off the airplane at the assigned cruise altitude. The air traffic controller informed the pilot of heavy showers near the destination airport, and the pilot "put the ice vanes down." The pilot indicated that, shortly afterward, the airplane experienced two "quick" electrical power fluctuations in which "everything went away and then came back," and "[s]econds later the entire [electrical] system failed." Due to the associated loss of navigation capability while operating in instrument meteorological conditions (IMC), the pilot set a general course for better weather conditions based on information from his preflight weather briefing. While the pilot attempted to find a suitable hole in the clouds to descend through under visual conditions, the left engine lost power. The pilot ultimately located a field through the cloud cover and executed a single-engine off-airport landing, which resulted in substantial damage to the right engine mount and firewall. A postaccident examination of the airplane and systems did not reveal any anomalies consistent with an in-flight electrical system malfunction. The three-position ignition and engine start/starter-only switches were in the ON position, and the engine anti-ice switches were in the ON position. When the airplane battery was initially checked during the examination, the voltmeter indicated 10.7 volts (normal voltage is 12 volts); the battery was charged and appeared to function normally thereafter. The loss of electrical power was likely initiated by the pilot inadvertently selecting the engine start switches instead of the engine anti-ice (ice vane) switches. This resulted in the starter/generators changing to starter operation and taking the generator function offline. Airplane electrical power was then being supplied solely by the battery, which caused it to deplete and led to a subsequent loss of electrical power to the airplane. A postaccident examination revealed that neither wing fuel tank contained any visible fuel. The left nacelle fuel tank did not contain any visible fuel, and the right nacelle fuel tank appeared to contain about 1 quart of fuel. The lack of fuel onboard at the time of the accident is consistent with a loss of engine power due to fuel exhaustion. This was a result of the extended flight time as the pilot attempted to exit instrument conditions after the loss of electrical power to locate a suitable airport. Further, the operator reported that 253 gallons (1,720 lbs) of fuel were on board at takeoff, and the accident flight duration was 3.65 hours. At maximum range power, the expected fuel consumption was about 406 lbs/hour, resulting in an endurance of about 4.2 hours. Thus, the pilot did not have the adequate fuel reserves required for flying in IMC. Both the pilot and medical crewmembers described a lack of communication and coordination among crewmembers as the emergency transpired. This resulted in multiple course adjustments that hindered the pilot's ability to locate visual meteorological conditions before the left engine fuel supply was exhausted.
Cause: Human factor
Occupants & Outcome
Crew On Board
1
Passengers On Board
2
Estimated Survivors
3
Fatality Rate
0.0%
Known people on board: 3
Operational Details
Schedule / Flight
McAlester – Idabel
Operator
EagleMedFlight Type
Ambulance
Flight Phase
Flight
Crash Site
Plain, Valley
Region / Country
North America • United States of America
