Chandigarh – New Delhi

On 25.03.2014, the operator received the travel programme for 27.3.2014, of Hon'ble Governor of Haryana from Chandigarh to Delhi. On 26.3.2014, the operations department took the flight clearances and filed the passenger manifest with the ATC and other concerned agencies. The flight plan was filed by a CPL holder, who is working as flight dispatcher with the Government of Haryana. The departure on 27.3.2014 was fixed at 1130 hrs. The cockpit crew reported at 1045 hrs for the flight. Pre flight medical examination including the breath analyzer test was carried out at 1100 hrs. The breath analyzer test for both the cockpit crew members was negative. Pre flight briefing among the crew members was carried out by using the documents prepared by the flight dispatcher. The aircraft was taxied under its own power from Haryana Government Hangar to bay no. D-2 in front of ATC building. No abnormality was observed or reported on the aircraft during this taxiing. The engines were shut down for passenger embarkation. As per the passenger manifest, in addition to the pilot and co-pilot there were 8 passengers. The baggage on board was approx. 50 lbs. There was 2100 lbs. of fuel on board. After boarding of the passengers, the aircraft engines were started at 1130 hrs. The aircraft was cleared for departure abeam „D<U+201F> link. The aircraft was taxied out via taxiway „D<U+201F>. After ATC departure clearance the aircraft was lined up for take-off. On clearance from ATC the take off roll was initiated and all the parameters were found normal. As per the pilot just before getting airborne some stiffness was found in rudder control as is felt in yaw damper engagement. The aircraft then pulled slightly to the left which as per the Commander was controllable. As per the pilot, the rotation was initiated at 98 knots. As per the DATCO the aircraft had lifted up to 10-15 feet AGL. The Commander has stated that after lift-off, immediately the left rudder got locked in forward position resulting in the aircraft yawing and rolling to left. The pilots tried to control it with right bank but the aircraft could not be controlled. Within 3-4 seconds of getting airborne the aircraft impacted the ground in left bank attitude. The initial impact was on pucca (tar road) and the wing has taken the first impact loads with lower surface metallic surface rubbing and screeching on ground. After the aircraft came to final halt, the co-pilot opened the door and evacuation was carried out. There was no injury to any of the occupants. The engine conditions lever could not be brought back as these were stuck. The throttle and pitch levers were retarded. The fuel shut off valves were closed. Battery and avionics were put off. Friction lock nuts were found loose. As per the Commander, after ensuring safety of passengers he had gone to cockpit to confirm that all switches were „off<U+201F>. At that time he has loosened the friction lock nuts to bring back the condition lever and throttle lever. However even after loosening the nut it was not possible to bring back these levers. Fire fighting vehicles were activated by pressing crash bell and primary alarm. Hand held RT set was used to announce the crash. RCFF vehicles proceeded to the site via runway and reported all the 10 personnel are safe and out of the disabled aircraft. Water and complementary agents (foam and dry chemical powder) were used. After fire was extinguished, the Fire Fighting vehicles reported back at crash bay except one CFT which was held at crash site under instruction of COO. The aircraft was substantially damaged. There was no fire barring burning of small patch of grass due coming in contact with the hot surfaces and oil. There was no injury to any of the occupants. The accident occurred in day light conditions.

Flight / Schedule

Chandigarh – New Delhi

Registration

VT-HRA

MSN

BB-1906

Year of Manufacture

2005

Date

March 27, 2014 at 11:39 AM

Type

CRASH

Flight Type

Government

Flight Phase

Takeoff (climb)

Crash Site

Airport (less than 10 km from airport)

Crash Location

Chandigarh Chandigarh

Region

Asia • India

Coordinates

30.7437°, 76.7823°

Crash Cause

Human factor

Narrative Report

On March 27, 2014 at 11:39 AM, Chandigarh – New Delhi experienced a crash involving Beechcraft 200 Super King Air, operated by Government of Haryana, with the event recorded near Chandigarh Chandigarh.

The flight was categorized as government and the reported phase was takeoff (climb) at a airport (less than 10 km from airport) crash site.

10 people were known to be on board, 0 fatalities were recorded, 10 survivors were identified or estimated. This corresponds to an estimated fatality rate of 0.0%.

Crew on board: 2, crew fatalities: 0, passengers on board: 8, passenger fatalities: 0, other fatalities: 0.

The listed crash cause is human factor. On 25.03.2014, the operator received the travel programme for 27.3.2014, of Hon'ble Governor of Haryana from Chandigarh to Delhi. On 26.3.2014, the operations department took the flight clearances and filed the passenger manifest with the ATC and other concerned agencies. The flight plan was filed by a CPL holder, who is working as flight dispatcher with the Government of Haryana. The departure on 27.3.2014 was fixed at 1130 hrs. The cockpit crew reported at 1045 hrs for the flight. Pre flight medical examination including the breath analyzer test was carried out at 1100 hrs. The breath analyzer test for both the cockpit crew members was negative. Pre flight briefing among the crew members was carried out by using the documents prepared by the flight dispatcher. The aircraft was taxied under its own power from Haryana Government Hangar to bay no. D-2 in front of ATC building. No abnormality was observed or reported on the aircraft during this taxiing. The engines were shut down for passenger embarkation. As per the passenger manifest, in addition to the pilot and co-pilot there were 8 passengers. The baggage on board was approx. 50 lbs. There was 2100 lbs. of fuel on board. After boarding of the passengers, the aircraft engines were started at 1130 hrs. The aircraft was cleared for departure abeam „D<U+201F> link. The aircraft was taxied out via taxiway „D<U+201F>. After ATC departure clearance the aircraft was lined up for take-off. On clearance from ATC the take off roll was initiated and all the parameters were found normal. As per the pilot just before getting airborne some stiffness was found in rudder control as is felt in yaw damper engagement. The aircraft then pulled slightly to the left which as per the Commander was controllable. As per the pilot, the rotation was initiated at 98 knots. As per the DATCO the aircraft had lifted up to 10-15 feet AGL. The Commander has stated that after lift-off, immediately the left rudder got locked in forward position resulting in the aircraft yawing and rolling to left. The pilots tried to control it with right bank but the aircraft could not be controlled. Within 3-4 seconds of getting airborne the aircraft impacted the ground in left bank attitude. The initial impact was on pucca (tar road) and the wing has taken the first impact loads with lower surface metallic surface rubbing and screeching on ground. After the aircraft came to final halt, the co-pilot opened the door and evacuation was carried out. There was no injury to any of the occupants. The engine conditions lever could not be brought back as these were stuck. The throttle and pitch levers were retarded. The fuel shut off valves were closed. Battery and avionics were put off. Friction lock nuts were found loose. As per the Commander, after ensuring safety of passengers he had gone to cockpit to confirm that all switches were „off<U+201F>. At that time he has loosened the friction lock nuts to bring back the condition lever and throttle lever. However even after loosening the nut it was not possible to bring back these levers. Fire fighting vehicles were activated by pressing crash bell and primary alarm. Hand held RT set was used to announce the crash. RCFF vehicles proceeded to the site via runway and reported all the 10 personnel are safe and out of the disabled aircraft. Water and complementary agents (foam and dry chemical powder) were used. After fire was extinguished, the Fire Fighting vehicles reported back at crash bay except one CFT which was held at crash site under instruction of COO. The aircraft was substantially damaged. There was no fire barring burning of small patch of grass due coming in contact with the hot surfaces and oil. There was no injury to any of the occupants. The accident occurred in day light conditions.

Aircraft reference details include registration VT-HRA, MSN BB-1906, year of manufacture 2005.

Geospatial coordinates for this crash are approximately 30.7437°, 76.7823°.

Fatalities

Total

0

Crew

0

Passengers

0

Other

0

Crash Summary

On 25.03.2014, the operator received the travel programme for 27.3.2014, of Hon'ble Governor of Haryana from Chandigarh to Delhi. On 26.3.2014, the operations department took the flight clearances and filed the passenger manifest with the ATC and other concerned agencies. The flight plan was filed by a CPL holder, who is working as flight dispatcher with the Government of Haryana. The departure on 27.3.2014 was fixed at 1130 hrs. The cockpit crew reported at 1045 hrs for the flight. Pre flight medical examination including the breath analyzer test was carried out at 1100 hrs. The breath analyzer test for both the cockpit crew members was negative. Pre flight briefing among the crew members was carried out by using the documents prepared by the flight dispatcher. The aircraft was taxied under its own power from Haryana Government Hangar to bay no. D-2 in front of ATC building. No abnormality was observed or reported on the aircraft during this taxiing. The engines were shut down for passenger embarkation. As per the passenger manifest, in addition to the pilot and co-pilot there were 8 passengers. The baggage on board was approx. 50 lbs. There was 2100 lbs. of fuel on board. After boarding of the passengers, the aircraft engines were started at 1130 hrs. The aircraft was cleared for departure abeam „D<U+201F> link. The aircraft was taxied out via taxiway „D<U+201F>. After ATC departure clearance the aircraft was lined up for take-off. On clearance from ATC the take off roll was initiated and all the parameters were found normal. As per the pilot just before getting airborne some stiffness was found in rudder control as is felt in yaw damper engagement. The aircraft then pulled slightly to the left which as per the Commander was controllable. As per the pilot, the rotation was initiated at 98 knots. As per the DATCO the aircraft had lifted up to 10-15 feet AGL. The Commander has stated that after lift-off, immediately the left rudder got locked in forward position resulting in the aircraft yawing and rolling to left. The pilots tried to control it with right bank but the aircraft could not be controlled. Within 3-4 seconds of getting airborne the aircraft impacted the ground in left bank attitude. The initial impact was on pucca (tar road) and the wing has taken the first impact loads with lower surface metallic surface rubbing and screeching on ground. After the aircraft came to final halt, the co-pilot opened the door and evacuation was carried out. There was no injury to any of the occupants. The engine conditions lever could not be brought back as these were stuck. The throttle and pitch levers were retarded. The fuel shut off valves were closed. Battery and avionics were put off. Friction lock nuts were found loose. As per the Commander, after ensuring safety of passengers he had gone to cockpit to confirm that all switches were „off<U+201F>. At that time he has loosened the friction lock nuts to bring back the condition lever and throttle lever. However even after loosening the nut it was not possible to bring back these levers. Fire fighting vehicles were activated by pressing crash bell and primary alarm. Hand held RT set was used to announce the crash. RCFF vehicles proceeded to the site via runway and reported all the 10 personnel are safe and out of the disabled aircraft. Water and complementary agents (foam and dry chemical powder) were used. After fire was extinguished, the Fire Fighting vehicles reported back at crash bay except one CFT which was held at crash site under instruction of COO. The aircraft was substantially damaged. There was no fire barring burning of small patch of grass due coming in contact with the hot surfaces and oil. There was no injury to any of the occupants. The accident occurred in day light conditions.

Cause: Human factor

Occupants & Outcome

Crew On Board

2

Passengers On Board

8

Estimated Survivors

10

Fatality Rate

0.0%

Known people on board: 10

Operational Details

Schedule / Flight

Chandigarh – New Delhi

Flight Type

Government

Flight Phase

Takeoff (climb)

Crash Site

Airport (less than 10 km from airport)

Region / Country

Asia • India

Aircraft Details

Registration

VT-HRA

MSN

BB-1906

Year of Manufacture

2005