Chehalis – Lewiston
Flight / Schedule
Chehalis – Lewiston
Aircraft
Cessna 340Registration
N68718
MSN
340A-1527
Year of Manufacture
1982
Operator
Pacific Cataract and Laser InstituteDate
October 25, 2010 at 07:45 AM
Type
CRASHFlight Type
Private
Flight Phase
Flight
Crash Site
Mountains
Crash Location
Morton Washington
Region
North America • United States of America
Coordinates
46.5571°, -122.2752°
Crash Cause
Technical failure
Narrative Report
On October 25, 2010 at 07:45 AM, Chehalis – Lewiston experienced a crash involving Cessna 340, operated by Pacific Cataract and Laser Institute, with the event recorded near Morton Washington.
The flight was categorized as private and the reported phase was flight at a mountains crash site.
3 people were known to be on board, 3 fatalities were recorded, 0 survivors were identified or estimated. This corresponds to an estimated fatality rate of 100.0%.
Crew on board: 1, crew fatalities: 1, passengers on board: 2, passenger fatalities: 2, other fatalities: 0.
The listed crash cause is technical failure. About 14 minutes after departing on the cross-country flight in instrument meteorological conditions, the airplane was observed on radar climbing through 14,800 feet mean sea level (msl). At this time, the pilot radioed to air traffic control (ATC) that he was returning to the departure airport. About 7 seconds later, the pilot transmitted that he had lost an engine and again stated that he was returning to the departure airport. About 50 seconds later, the pilot transmitted, “We’re losing it.” There was no further communication with the pilot. Radar data revealed that at 14,800 feet msl the airplane began a right 360-degree turn at 8 degrees per second, and about 120 degrees into the turn, it began a descent averaging 5,783 feet per minute. The airplane remained in a right turn until radar contact was lost at 10,700 feet msl. The airplane impacted a 30-degree slope of a densely forested mountain about 2,940 feet msl in a near vertical, slightly right-wing-low attitude. A logger working in the area reported hearing a “very loud roaring sound,” like an airplane diving toward his location and that it seemed to be “really under power.” The logger described the weather as being “socked in,” with light rain and not much wind. Post accident examination revealed that propeller damage was the result of impact forces, with no indications of fatigue or propeller failure before impact. It was also noted that the left propeller was being operated under conditions of some power at impact, while the right propeller was not operating under conditions of significant power at impact. Based on these findings, it is most likely that the pilot experienced a partial loss of power of the right engine and, after incorrectly initiating a right turn into the failed engine, allowed the rate of turn to increase to the point that the airplane became uncontrollable before impact with terrain. The reason for the partial loss of engine power was not determined because postaccident examination of the airframe and both engines did not reveal any mechanical malfunctions or failures that would have precluded normal operation.
Aircraft reference details include registration N68718, MSN 340A-1527, year of manufacture 1982.
Geospatial coordinates for this crash are approximately 46.5571°, -122.2752°.
Fatalities
Total
3
Crew
1
Passengers
2
Other
0
Crash Summary
About 14 minutes after departing on the cross-country flight in instrument meteorological conditions, the airplane was observed on radar climbing through 14,800 feet mean sea level (msl). At this time, the pilot radioed to air traffic control (ATC) that he was returning to the departure airport. About 7 seconds later, the pilot transmitted that he had lost an engine and again stated that he was returning to the departure airport. About 50 seconds later, the pilot transmitted, “We’re losing it.” There was no further communication with the pilot. Radar data revealed that at 14,800 feet msl the airplane began a right 360-degree turn at 8 degrees per second, and about 120 degrees into the turn, it began a descent averaging 5,783 feet per minute. The airplane remained in a right turn until radar contact was lost at 10,700 feet msl. The airplane impacted a 30-degree slope of a densely forested mountain about 2,940 feet msl in a near vertical, slightly right-wing-low attitude. A logger working in the area reported hearing a “very loud roaring sound,” like an airplane diving toward his location and that it seemed to be “really under power.” The logger described the weather as being “socked in,” with light rain and not much wind. Post accident examination revealed that propeller damage was the result of impact forces, with no indications of fatigue or propeller failure before impact. It was also noted that the left propeller was being operated under conditions of some power at impact, while the right propeller was not operating under conditions of significant power at impact. Based on these findings, it is most likely that the pilot experienced a partial loss of power of the right engine and, after incorrectly initiating a right turn into the failed engine, allowed the rate of turn to increase to the point that the airplane became uncontrollable before impact with terrain. The reason for the partial loss of engine power was not determined because postaccident examination of the airframe and both engines did not reveal any mechanical malfunctions or failures that would have precluded normal operation.
Cause: Technical failure
Occupants & Outcome
Crew On Board
1
Passengers On Board
2
Estimated Survivors
0
Fatality Rate
100.0%
Known people on board: 3
Operational Details
Schedule / Flight
Chehalis – Lewiston
Operator
Pacific Cataract and Laser InstituteFlight Type
Private
Flight Phase
Flight
Crash Site
Mountains
Region / Country
North America • United States of America
