Anguilla - Sint Maarten

The commander intended to fly the BN-2 Islander aircraft from Anguilla Wallblake International Airport (AXA) to the neighbouring island of St Maarten (SXM) to await cargo inbound on another flight. The cabin of the aircraft was configured for cargo operations with no passenger seats fitted, as the only other planned occupant was the operator’s Chief Engineer, who would be sitting beside the commander in the right hand seat. However, the commander asked the operator if he could take a family member with him to SXM. The operator agreed and an extra seat was fitted. Witnesses stated that the commander appeared "rushed" prior to departure. The commander stated that he partially carried out the normal pre-flight inspection. He then started the engines. Before taxiing he realised that the nose landing gear chocks were still in place so he shut down the left hand engine, removed and stowed the chocks and then restarted the left engine. The aircraft took off from runway 10 at 14:15 hrs. At between 100 ft and 150 ft the commander initiated a left turn but after some initial movement the ailerons jammed. When he discovered that he was unable to straighten the ailerons he attempted to return to land on runway 10. The other flight controls did not appear to be restricted. With the ailerons jammed, the aircraft continued to turn to the left, losing altitude as it flew over a settlement to the north of the aerodrome, until pointed directly at the Air Traffic Control tower, causing the Air Traffic Control Officer (ATCO) to abandon the tower. The commander judged that the aircraft was too fast and high to attempt a landing and therefore initiated a go-around, applying full power. He continued the left turn, losing height and speed to position the aircraft for another approach but, as the aircraft descended over the northern edge of the runway, its left wing struck the perimeter fence. On impact the aircraft spun about its vertical axis with its wings level and continued sliding sideways on its right side for approximately 80 ft before coming to rest facing north-west.

Flight / Schedule

Anguilla - Sint Maarten

Registration

VP-AAG

MSN

88

Year of Manufacture

1969

Operator

Air Montserrat

Date

February 2, 2008 at 02:20 PM

Type

CRASH

Flight Type

Cargo

Flight Phase

Landing (descent or approach)

Crash Site

Airport (less than 10 km from airport)

Crash Location

Anguilla All Anguilla

Region

Central America • Anguilla

Crash Cause

Human factor

Narrative Report

On February 2, 2008 at 02:20 PM, Anguilla - Sint Maarten experienced a crash involving Britten-Norman Islander, operated by Air Montserrat, with the event recorded near Anguilla All Anguilla.

The flight was categorized as cargo and the reported phase was landing (descent or approach) at a airport (less than 10 km from airport) crash site.

3 people were known to be on board, 0 fatalities were recorded, 3 survivors were identified or estimated. This corresponds to an estimated fatality rate of 0.0%.

Crew on board: 1, crew fatalities: 0, passengers on board: 2, passenger fatalities: 0, other fatalities: 0.

The listed crash cause is human factor. The commander intended to fly the BN-2 Islander aircraft from Anguilla Wallblake International Airport (AXA) to the neighbouring island of St Maarten (SXM) to await cargo inbound on another flight. The cabin of the aircraft was configured for cargo operations with no passenger seats fitted, as the only other planned occupant was the operator’s Chief Engineer, who would be sitting beside the commander in the right hand seat. However, the commander asked the operator if he could take a family member with him to SXM. The operator agreed and an extra seat was fitted. Witnesses stated that the commander appeared "rushed" prior to departure. The commander stated that he partially carried out the normal pre-flight inspection. He then started the engines. Before taxiing he realised that the nose landing gear chocks were still in place so he shut down the left hand engine, removed and stowed the chocks and then restarted the left engine. The aircraft took off from runway 10 at 14:15 hrs. At between 100 ft and 150 ft the commander initiated a left turn but after some initial movement the ailerons jammed. When he discovered that he was unable to straighten the ailerons he attempted to return to land on runway 10. The other flight controls did not appear to be restricted. With the ailerons jammed, the aircraft continued to turn to the left, losing altitude as it flew over a settlement to the north of the aerodrome, until pointed directly at the Air Traffic Control tower, causing the Air Traffic Control Officer (ATCO) to abandon the tower. The commander judged that the aircraft was too fast and high to attempt a landing and therefore initiated a go-around, applying full power. He continued the left turn, losing height and speed to position the aircraft for another approach but, as the aircraft descended over the northern edge of the runway, its left wing struck the perimeter fence. On impact the aircraft spun about its vertical axis with its wings level and continued sliding sideways on its right side for approximately 80 ft before coming to rest facing north-west.

Aircraft reference details include registration VP-AAG, MSN 88, year of manufacture 1969.

Fatalities

Total

0

Crew

0

Passengers

0

Other

0

Crash Summary

The commander intended to fly the BN-2 Islander aircraft from Anguilla Wallblake International Airport (AXA) to the neighbouring island of St Maarten (SXM) to await cargo inbound on another flight. The cabin of the aircraft was configured for cargo operations with no passenger seats fitted, as the only other planned occupant was the operator’s Chief Engineer, who would be sitting beside the commander in the right hand seat. However, the commander asked the operator if he could take a family member with him to SXM. The operator agreed and an extra seat was fitted. Witnesses stated that the commander appeared "rushed" prior to departure. The commander stated that he partially carried out the normal pre-flight inspection. He then started the engines. Before taxiing he realised that the nose landing gear chocks were still in place so he shut down the left hand engine, removed and stowed the chocks and then restarted the left engine. The aircraft took off from runway 10 at 14:15 hrs. At between 100 ft and 150 ft the commander initiated a left turn but after some initial movement the ailerons jammed. When he discovered that he was unable to straighten the ailerons he attempted to return to land on runway 10. The other flight controls did not appear to be restricted. With the ailerons jammed, the aircraft continued to turn to the left, losing altitude as it flew over a settlement to the north of the aerodrome, until pointed directly at the Air Traffic Control tower, causing the Air Traffic Control Officer (ATCO) to abandon the tower. The commander judged that the aircraft was too fast and high to attempt a landing and therefore initiated a go-around, applying full power. He continued the left turn, losing height and speed to position the aircraft for another approach but, as the aircraft descended over the northern edge of the runway, its left wing struck the perimeter fence. On impact the aircraft spun about its vertical axis with its wings level and continued sliding sideways on its right side for approximately 80 ft before coming to rest facing north-west.

Cause: Human factor

Occupants & Outcome

Crew On Board

1

Passengers On Board

2

Estimated Survivors

3

Fatality Rate

0.0%

Known people on board: 3

Operational Details

Schedule / Flight

Anguilla - Sint Maarten

Operator

Air Montserrat

Flight Type

Cargo

Flight Phase

Landing (descent or approach)

Crash Site

Airport (less than 10 km from airport)

Region / Country

Central America • Anguilla

Aircraft Details

Registration

VP-AAG

MSN

88

Year of Manufacture

1969