Edinburgh – Dundee

After an uneventful flight from Edinburgh the pilot made a visual approach to Runway 28 (landing distance available 1,400 metres) at Dundee. The pilot reported that the aircraft floated down the runway in the flare and bounced lightly on touchdown. During the bounce the aircraft initially yawed left and then rolled left in a normal pitch attitude with no stall warning. Full right rudder was applied but this was unable to correct the yaw. Power was applied to initiate a go-around, whilst maintaining full right rudder, but the pilot was unable to prevent the left wing from hitting the ground. This caused the aircraft to yaw rapidly to the left bringing one of its wheels into contact with a low wall. The pilot then reduced power and ditched in the River Tay, approximately 10 metres from the shore. The air traffic controllers on duty reported that the aircraft achieved a high nose attitude during the go-around before the left wing dropped and the aircraft veered to the left. The aircraft came to rest with the top of the fuselage out of the water and the pilot and passengers were able to evacuate though the main door and stand on the wing to await rescue by the airport's hovercraft. The hovercraft could only carry two passengers at a time thus the process was delayed resulting in the pilot and passengers suffering from mild hypothermia.

Flight / Schedule

Edinburgh – Dundee

Aircraft

Socata TBM-700

Registration

N700VA

MSN

233

Year of Manufacture

2002

Date

October 24, 2003 at 05:42 PM

Type

CRASH

Flight Type

Private

Flight Phase

Landing (descent or approach)

Crash Site

Lake, Sea, Ocean, River

Crash Location

Dundee Angus (Forfarshire)

Region

Europe • United Kingdom

Crash Cause

Human factor

Narrative Report

On October 24, 2003 at 05:42 PM, Edinburgh – Dundee experienced a crash involving Socata TBM-700, operated by Private American, with the event recorded near Dundee Angus (Forfarshire).

The flight was categorized as private and the reported phase was landing (descent or approach) at a lake, sea, ocean, river crash site.

4 people were known to be on board, 0 fatalities were recorded, 4 survivors were identified or estimated. This corresponds to an estimated fatality rate of 0.0%.

Crew on board: 1, crew fatalities: 0, passengers on board: 3, passenger fatalities: 0, other fatalities: 0.

The listed crash cause is human factor. After an uneventful flight from Edinburgh the pilot made a visual approach to Runway 28 (landing distance available 1,400 metres) at Dundee. The pilot reported that the aircraft floated down the runway in the flare and bounced lightly on touchdown. During the bounce the aircraft initially yawed left and then rolled left in a normal pitch attitude with no stall warning. Full right rudder was applied but this was unable to correct the yaw. Power was applied to initiate a go-around, whilst maintaining full right rudder, but the pilot was unable to prevent the left wing from hitting the ground. This caused the aircraft to yaw rapidly to the left bringing one of its wheels into contact with a low wall. The pilot then reduced power and ditched in the River Tay, approximately 10 metres from the shore. The air traffic controllers on duty reported that the aircraft achieved a high nose attitude during the go-around before the left wing dropped and the aircraft veered to the left. The aircraft came to rest with the top of the fuselage out of the water and the pilot and passengers were able to evacuate though the main door and stand on the wing to await rescue by the airport's hovercraft. The hovercraft could only carry two passengers at a time thus the process was delayed resulting in the pilot and passengers suffering from mild hypothermia.

Aircraft reference details include registration N700VA, MSN 233, year of manufacture 2002.

Fatalities

Total

0

Crew

0

Passengers

0

Other

0

Crash Summary

After an uneventful flight from Edinburgh the pilot made a visual approach to Runway 28 (landing distance available 1,400 metres) at Dundee. The pilot reported that the aircraft floated down the runway in the flare and bounced lightly on touchdown. During the bounce the aircraft initially yawed left and then rolled left in a normal pitch attitude with no stall warning. Full right rudder was applied but this was unable to correct the yaw. Power was applied to initiate a go-around, whilst maintaining full right rudder, but the pilot was unable to prevent the left wing from hitting the ground. This caused the aircraft to yaw rapidly to the left bringing one of its wheels into contact with a low wall. The pilot then reduced power and ditched in the River Tay, approximately 10 metres from the shore. The air traffic controllers on duty reported that the aircraft achieved a high nose attitude during the go-around before the left wing dropped and the aircraft veered to the left. The aircraft came to rest with the top of the fuselage out of the water and the pilot and passengers were able to evacuate though the main door and stand on the wing to await rescue by the airport's hovercraft. The hovercraft could only carry two passengers at a time thus the process was delayed resulting in the pilot and passengers suffering from mild hypothermia.

Cause: Human factor

Occupants & Outcome

Crew On Board

1

Passengers On Board

3

Estimated Survivors

4

Fatality Rate

0.0%

Known people on board: 4

Operational Details

Schedule / Flight

Edinburgh – Dundee

Flight Type

Private

Flight Phase

Landing (descent or approach)

Crash Site

Lake, Sea, Ocean, River

Region / Country

Europe • United Kingdom

Aircraft Details

Aircraft

Socata TBM-700

Registration

N700VA

MSN

233

Year of Manufacture

2002

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