Lake Ozark – South Bend

The turbo-prop airplane departed controlled flight after initiating an ATC directed turn during cruise climb. The airplane subsequently entered a rapidly descending spiral turn, impacting the terrain and exploding. A witness reported hearing an "unusually loud" engine sound prior to seeing the airplane in a nose-low descent. The witness stated the airplane was "heading straight down, and did between a quarter and half of turn, but was not spinning wildly." The witness reported the airplane disappeared behind a nearby ridgeline and was followed by a "loud sound, and an immediate large cloud of black smoke." Aircraft radar track data showed the airplane heading to the northeast, while climbing to a maximum altitude of 13,800 feet msl. The airplane then entered an increasingly tighter, right descending turn. The calculated descent rate was 7,000 feet/min. Instrument flight rules (IFR) conditions prevailed at altitude and marginal visual flight rules (MVFR) conditions prevailed at the accident site. The instrument-rated pilot received a weather briefing prior to departure. During the briefing the pilot was told of building thunderstorm activity near the departure airport and along the route of flight. The pilot told the briefer he was going to depart shortly to keep ahead of the approaching weather. A witness at the departure airport reported that the passenger was concerned about flying in "bad weather" and the pilot told the passenger that the weather was only going to get worse and that they "needed to go to get ahead of it." A two-dimensional reconstruction determined that all primary airframe structural components, flight control surfaces, powerplant components, and propeller blades were present. Flight control continuity could not be established due to the extensive damage to all components. Inspection of the recovered flight control components did not exhibit any evidence of pre-impact malfunction. The standby attitude indicator gyro and its case showed evidence of rotational damage, consistent with the gyro rotating at the time of impact. Both solid-state Attitude & Heading Reference System (AHRS) units were destroyed during the accident, and as a result no information was available.

Flight / Schedule

Lake Ozark – South Bend

Aircraft

Pilatus PC-12

Registration

N451ES

MSN

425

Year of Manufacture

2001

Date

September 14, 2002 at 03:55 PM

Type

CRASH

Flight Type

Executive/Corporate/Business

Flight Phase

Flight

Crash Site

Plain, Valley

Crash Location

Westphalia Missouri

Region

North America • United States of America

Coordinates

38.4420°, -91.9993°

Crash Cause

Human factor

Narrative Report

On September 14, 2002 at 03:55 PM, Lake Ozark – South Bend experienced a crash involving Pilatus PC-12, operated by Pilatus Partners, with the event recorded near Westphalia Missouri.

The flight was categorized as executive/corporate/business and the reported phase was flight at a plain, valley crash site.

2 people were known to be on board, 2 fatalities were recorded, 0 survivors were identified or estimated. This corresponds to an estimated fatality rate of 100.0%.

Crew on board: 1, crew fatalities: 1, passengers on board: 1, passenger fatalities: 1, other fatalities: 0.

The listed crash cause is human factor. The turbo-prop airplane departed controlled flight after initiating an ATC directed turn during cruise climb. The airplane subsequently entered a rapidly descending spiral turn, impacting the terrain and exploding. A witness reported hearing an "unusually loud" engine sound prior to seeing the airplane in a nose-low descent. The witness stated the airplane was "heading straight down, and did between a quarter and half of turn, but was not spinning wildly." The witness reported the airplane disappeared behind a nearby ridgeline and was followed by a "loud sound, and an immediate large cloud of black smoke." Aircraft radar track data showed the airplane heading to the northeast, while climbing to a maximum altitude of 13,800 feet msl. The airplane then entered an increasingly tighter, right descending turn. The calculated descent rate was 7,000 feet/min. Instrument flight rules (IFR) conditions prevailed at altitude and marginal visual flight rules (MVFR) conditions prevailed at the accident site. The instrument-rated pilot received a weather briefing prior to departure. During the briefing the pilot was told of building thunderstorm activity near the departure airport and along the route of flight. The pilot told the briefer he was going to depart shortly to keep ahead of the approaching weather. A witness at the departure airport reported that the passenger was concerned about flying in "bad weather" and the pilot told the passenger that the weather was only going to get worse and that they "needed to go to get ahead of it." A two-dimensional reconstruction determined that all primary airframe structural components, flight control surfaces, powerplant components, and propeller blades were present. Flight control continuity could not be established due to the extensive damage to all components. Inspection of the recovered flight control components did not exhibit any evidence of pre-impact malfunction. The standby attitude indicator gyro and its case showed evidence of rotational damage, consistent with the gyro rotating at the time of impact. Both solid-state Attitude & Heading Reference System (AHRS) units were destroyed during the accident, and as a result no information was available.

Aircraft reference details include registration N451ES, MSN 425, year of manufacture 2001.

Geospatial coordinates for this crash are approximately 38.4420°, -91.9993°.

Fatalities

Total

2

Crew

1

Passengers

1

Other

0

Crash Summary

The turbo-prop airplane departed controlled flight after initiating an ATC directed turn during cruise climb. The airplane subsequently entered a rapidly descending spiral turn, impacting the terrain and exploding. A witness reported hearing an "unusually loud" engine sound prior to seeing the airplane in a nose-low descent. The witness stated the airplane was "heading straight down, and did between a quarter and half of turn, but was not spinning wildly." The witness reported the airplane disappeared behind a nearby ridgeline and was followed by a "loud sound, and an immediate large cloud of black smoke." Aircraft radar track data showed the airplane heading to the northeast, while climbing to a maximum altitude of 13,800 feet msl. The airplane then entered an increasingly tighter, right descending turn. The calculated descent rate was 7,000 feet/min. Instrument flight rules (IFR) conditions prevailed at altitude and marginal visual flight rules (MVFR) conditions prevailed at the accident site. The instrument-rated pilot received a weather briefing prior to departure. During the briefing the pilot was told of building thunderstorm activity near the departure airport and along the route of flight. The pilot told the briefer he was going to depart shortly to keep ahead of the approaching weather. A witness at the departure airport reported that the passenger was concerned about flying in "bad weather" and the pilot told the passenger that the weather was only going to get worse and that they "needed to go to get ahead of it." A two-dimensional reconstruction determined that all primary airframe structural components, flight control surfaces, powerplant components, and propeller blades were present. Flight control continuity could not be established due to the extensive damage to all components. Inspection of the recovered flight control components did not exhibit any evidence of pre-impact malfunction. The standby attitude indicator gyro and its case showed evidence of rotational damage, consistent with the gyro rotating at the time of impact. Both solid-state Attitude & Heading Reference System (AHRS) units were destroyed during the accident, and as a result no information was available.

Cause: Human factor

Occupants & Outcome

Crew On Board

1

Passengers On Board

1

Estimated Survivors

0

Fatality Rate

100.0%

Known people on board: 2

Operational Details

Schedule / Flight

Lake Ozark – South Bend

Flight Type

Executive/Corporate/Business

Flight Phase

Flight

Crash Site

Plain, Valley

Region / Country

North America • United States of America

Aircraft Details

Aircraft

Pilatus PC-12

Registration

N451ES

MSN

425

Year of Manufacture

2001