Oklahoma City - Greeley
Flight / Schedule
Oklahoma City - Greeley
Aircraft
Cessna 550 Citation IIRegistration
N13VP
MSN
550-0263
Year of Manufacture
1981
Operator
AirleaseDate
May 20, 2002 at 08:01 AM
Type
CRASHFlight Type
Charter/Taxi (Non Scheduled Revenue Flight)
Flight Phase
Takeoff (climb)
Crash Site
Airport (less than 10 km from airport)
Crash Location
Oklahoma City-Wiley Post Oklahoma
Region
North America • United States of America
Crash Cause
Human factor
Narrative Report
On May 20, 2002 at 08:01 AM, Oklahoma City - Greeley experienced a crash involving Cessna 550 Citation II, operated by Airlease, with the event recorded near Oklahoma City-Wiley Post Oklahoma.
The flight was categorized as charter/taxi (non scheduled revenue flight) and the reported phase was takeoff (climb) at a airport (less than 10 km from airport) crash site.
6 people were known to be on board, 0 fatalities were recorded, 6 survivors were identified or estimated. This corresponds to an estimated fatality rate of 0.0%.
Crew on board: 2, crew fatalities: 0, passengers on board: 4, passenger fatalities: 0, other fatalities: 0.
The listed crash cause is human factor. The twin-tubofan airplane overran the runway during an aborted takeoff, impacting two fences before coming to rest. The pilot reported experiencing no anomalies with the airplane during the preflight inspection and taxi portion of the flight. During takeoff roll, at V1 (103 knots), the pilot began to pull aft on the control yoke. The pilot noticed the nose landing gear was not coming off of the runway and at 120 knots, with full aft control input, elected to abort the takeoff. He pulled the power to idle and applied maximum braking. Upon seeing the localizer antennas approaching the airplane at the departure end of the runway, the pilot veered the airplane to the right of centerline. The airplane departed the runway surface and impacted the fences. Post-accident examination of the runway revealed tire skid marks on the runway that led to the airplane's final resting place. The tire skid marks measured 1,765 feet in length. Examination of the wreckage revealed no pre-existing brake system anomalies that would have hindered the airplane's braking capability. Examination of the elevator trim system revealed it was 12 degrees out of trim in the nose down direction. The airplane underwent a Phase B and Phase 1 through 5 inspections approximately 5 months prior to the accident. The manufacturer's inspection manual indicates the elevator system should be examined every Phase 5 inspection. The aircraft's flight manual informs the pilot that the right elevator and trim tab should be inspected during the exterior inspection to ensure the elevator trim tab position matches its indicator.
Aircraft reference details include registration N13VP, MSN 550-0263, year of manufacture 1981.
Fatalities
Total
0
Crew
0
Passengers
0
Other
0
Crash Summary
The twin-tubofan airplane overran the runway during an aborted takeoff, impacting two fences before coming to rest. The pilot reported experiencing no anomalies with the airplane during the preflight inspection and taxi portion of the flight. During takeoff roll, at V1 (103 knots), the pilot began to pull aft on the control yoke. The pilot noticed the nose landing gear was not coming off of the runway and at 120 knots, with full aft control input, elected to abort the takeoff. He pulled the power to idle and applied maximum braking. Upon seeing the localizer antennas approaching the airplane at the departure end of the runway, the pilot veered the airplane to the right of centerline. The airplane departed the runway surface and impacted the fences. Post-accident examination of the runway revealed tire skid marks on the runway that led to the airplane's final resting place. The tire skid marks measured 1,765 feet in length. Examination of the wreckage revealed no pre-existing brake system anomalies that would have hindered the airplane's braking capability. Examination of the elevator trim system revealed it was 12 degrees out of trim in the nose down direction. The airplane underwent a Phase B and Phase 1 through 5 inspections approximately 5 months prior to the accident. The manufacturer's inspection manual indicates the elevator system should be examined every Phase 5 inspection. The aircraft's flight manual informs the pilot that the right elevator and trim tab should be inspected during the exterior inspection to ensure the elevator trim tab position matches its indicator.
Cause: Human factor
Occupants & Outcome
Crew On Board
2
Passengers On Board
4
Estimated Survivors
6
Fatality Rate
0.0%
Known people on board: 6
Operational Details
Schedule / Flight
Oklahoma City - Greeley
Operator
AirleaseFlight Type
Charter/Taxi (Non Scheduled Revenue Flight)
Flight Phase
Takeoff (climb)
Crash Site
Airport (less than 10 km from airport)
Region / Country
North America • United States of America
Aircraft Details
Similar Plane Crashes
United States Signal Corps - USSC
De Havilland DH.4
The single engine airplane departed Dayton-McCook Field for a local test flight. Shortly after takeoff, the aircraft stalled and crashed, killing both occupants. Crew: Maj Oscar Brindley, Lt Col Henry Damm.
United States Signal Corps - USSC
De Havilland DH.4
Lt. Frank Stuart Patterson, son and nephew of the co-founders of National Cash Register, is killed in the crash of his DH.4M, AS-32098, at Wilbur Wright Field during a flight test of a new mechanism for synchronizing machine gun and propeller, when a tie rod breaks during a dive from 15,000 feet (4,600 m), causing the wings to separate from the aircraft. Wishing to recognize the contributions of the Patterson family (owners of NCR) the area of Wright Field east of Huffman Dam (including Wilbur Wright Field, Fairfield Air Depot, and the Huffman Prairie) is renamed Patterson Field on 6 July 1931, in honor of Lt. Patterson.
United States Signal Corps - USSC
De Havilland DH.4
The aircraft crashed in unknown circumstances.
United States Signal Corps - USSC
De Havilland DH.4
The crew was completing a training mission. At an altitude of about 4,000 feet, the aircraft entered a spin and crashed in an open field near Everman-Barron Field Airport. A crew was killed and the second occupants was injured. The aircraft was destroyed.
U.S. Air Mail Service
De Havilland DH.4
Crashed following an engine failure. Pilot fate unknown.
United States Signal Corps - USSC
De Havilland DH.4
The accident occurred in unknown circumstances.
