Edinburgh – Belfast

The aircraft landed at Edinburgh Airport, Scotland, at 00:03 and was parked there on Stand 31 in conditions including light and moderate snowfall. After preparation for a Royal Mail charter flight 670A to Belfast, start clearance was given at 15:03. At 15:12 hrs the crew advised ATC they were shutting down due to a technical problem. The crew then advised their company that a generator would not come on line. An avionics technician carried out diagnosis during which both engines were ground-run twice. No fault was found and the flight crew requested taxi clearance at 17:10. A normal take off from runway 06 was carried out followed by a reduction to climb power at 1,200 feet amsl. At 2,200 feet amsl the aircraft anti-icing systems were selected on. Three seconds later the torque on each engine reduced rapidly to zero. A MAYDAY call was made by the crew advising that they had experienced a double engine failure. The aircraft was ditched in the Firth of Forth estuary some 100 meters from the shoreline near Granton Harbour. Both pilots were killed. Weather reported just before the accident with a temperature of +2°C, dewpoint of -3°C, visibility of more then 10 km, broken clouds at 4500 feet and cover at 8000 feet.

Flight / Schedule

Edinburgh – Belfast

Aircraft

Short 360

Registration

G-BNMT

MSN

3723

Year of Manufacture

1987

Operator

Loganair

Date

February 27, 2001 at 05:31 PM

Type

CRASH

Flight Type

Cargo

Flight Phase

Takeoff (climb)

Crash Site

Lake, Sea, Ocean, River

Crash Location

Edinburgh Midlothian (County of Edinburgh)

Region

Europe • United Kingdom

Crash Cause

Technical failure

Narrative Report

On February 27, 2001 at 05:31 PM, Edinburgh – Belfast experienced a crash involving Short 360, operated by Loganair, with the event recorded near Edinburgh Midlothian (County of Edinburgh).

The flight was categorized as cargo and the reported phase was takeoff (climb) at a lake, sea, ocean, river crash site.

2 people were known to be on board, 2 fatalities were recorded, 0 survivors were identified or estimated. This corresponds to an estimated fatality rate of 100.0%.

Crew on board: 2, crew fatalities: 2, passengers on board: 0, passenger fatalities: 0, other fatalities: 0.

The listed crash cause is technical failure. The aircraft landed at Edinburgh Airport, Scotland, at 00:03 and was parked there on Stand 31 in conditions including light and moderate snowfall. After preparation for a Royal Mail charter flight 670A to Belfast, start clearance was given at 15:03. At 15:12 hrs the crew advised ATC they were shutting down due to a technical problem. The crew then advised their company that a generator would not come on line. An avionics technician carried out diagnosis during which both engines were ground-run twice. No fault was found and the flight crew requested taxi clearance at 17:10. A normal take off from runway 06 was carried out followed by a reduction to climb power at 1,200 feet amsl. At 2,200 feet amsl the aircraft anti-icing systems were selected on. Three seconds later the torque on each engine reduced rapidly to zero. A MAYDAY call was made by the crew advising that they had experienced a double engine failure. The aircraft was ditched in the Firth of Forth estuary some 100 meters from the shoreline near Granton Harbour. Both pilots were killed. Weather reported just before the accident with a temperature of +2°C, dewpoint of -3°C, visibility of more then 10 km, broken clouds at 4500 feet and cover at 8000 feet.

Aircraft reference details include registration G-BNMT, MSN 3723, year of manufacture 1987.

Fatalities

Total

2

Crew

2

Passengers

0

Other

0

Crash Summary

The aircraft landed at Edinburgh Airport, Scotland, at 00:03 and was parked there on Stand 31 in conditions including light and moderate snowfall. After preparation for a Royal Mail charter flight 670A to Belfast, start clearance was given at 15:03. At 15:12 hrs the crew advised ATC they were shutting down due to a technical problem. The crew then advised their company that a generator would not come on line. An avionics technician carried out diagnosis during which both engines were ground-run twice. No fault was found and the flight crew requested taxi clearance at 17:10. A normal take off from runway 06 was carried out followed by a reduction to climb power at 1,200 feet amsl. At 2,200 feet amsl the aircraft anti-icing systems were selected on. Three seconds later the torque on each engine reduced rapidly to zero. A MAYDAY call was made by the crew advising that they had experienced a double engine failure. The aircraft was ditched in the Firth of Forth estuary some 100 meters from the shoreline near Granton Harbour. Both pilots were killed. Weather reported just before the accident with a temperature of +2°C, dewpoint of -3°C, visibility of more then 10 km, broken clouds at 4500 feet and cover at 8000 feet.

Cause: Technical failure

Occupants & Outcome

Crew On Board

2

Passengers On Board

0

Estimated Survivors

0

Fatality Rate

100.0%

Known people on board: 2

Operational Details

Schedule / Flight

Edinburgh – Belfast

Operator

Loganair

Flight Type

Cargo

Flight Phase

Takeoff (climb)

Crash Site

Lake, Sea, Ocean, River

Region / Country

Europe • United Kingdom

Aircraft Details

Aircraft

Short 360

Registration

G-BNMT

MSN

3723

Year of Manufacture

1987