East Midlands - East Midlands
Flight / Schedule
East Midlands - East Midlands
Aircraft
Fokker F27 FriendshipRegistration
G-BMAU
MSN
10241
Year of Manufacture
1963
Operator
British Midland Airways - BMADate
January 18, 1987 at 02:15 PM
Type
CRASHFlight Type
Training
Flight Phase
Landing (descent or approach)
Crash Site
Airport (less than 10 km from airport)
Crash Location
East Midlands Leicestershire
Region
Europe • United Kingdom
Coordinates
52.8281°, -1.3327°
Crash Cause
Human factor
Narrative Report
On January 18, 1987 at 02:15 PM, East Midlands - East Midlands experienced a crash involving Fokker F27 Friendship, operated by British Midland Airways - BMA, with the event recorded near East Midlands Leicestershire.
The flight was categorized as training and the reported phase was landing (descent or approach) at a airport (less than 10 km from airport) crash site.
3 people were known to be on board, 0 fatalities were recorded, 3 survivors were identified or estimated. This corresponds to an estimated fatality rate of 0.0%.
Crew on board: 3, crew fatalities: 0, passengers on board: 0, passenger fatalities: 0, other fatalities: 0.
The listed crash cause is human factor. The BMA Fokker F-27 aircraft was engaged on crew training at East Midlands Airport (EMA). The commander, who was an experienced training captain, occupied the right pilot's seat and a first officer undergoing training for conversion to captaincy occupied the left seat as handling pilot. Another captain refreshing on type sat on the jump seat behind the pilots' seats, the intention being that he should move into the left seat after the first officer's training period. The weather was: wind 150 degrees at 7 kts, visibility 4 km and cloud 7 oktas stratus, base 1000 feet. The surface temperature was 2 °C and the QNH 1030. The training session began with a practice abandoned takeoff after which the aircraft took off at 13:08 and flew three practice ILS approaches followed by touch-and-go landings on runway 09, climbing to 2000 feet above mean sea level (amsl) after each takeoff. The runway in use was then changed and the aircraft flew a simulated asymmetric ILS approach to runway 27 followed by a missed approach (go-around) with the left engine throttled back. The runway was then changed again and an ILS approach to runway 09 was flown with the left engine still throttled back. This approach was followed by a touch-and-go landing during which both engines were brought up to full power. Very soon after becoming airborne the training captain again simulated failure of the left engine and the aircraft was climbed to 2000 feet amsl. Soon after the aircraft levelled off, the handling pilot commented on the large amount of rudder required to counteract the simulated failure of the left engine after takeoff. The training captain then said that he was deliberately putting more drag on the left side than would have been the case if the propeller had auto-feathered so that the climb performance corresponded better with that of an aircraft with passengers on board. He went on to say that if the handling pilot could cope with that extra drag, he could expect to control the aircraft if the failed engine auto-feathered because the rudder pedal force would then not be quite so great. The crew then began a procedural NDB approach to runway 09, for which instrument screens were fitted in front of the handling pilot. It was intended that the aircraft should be landed after the NDB approach for the pilot in the jump seat to take over as handling pilot. Decision altitude for the approach was 740 feet and touchdown altitude was 305 feet. It was company practice for beacon passage to be identified by the movement of the radio compass needle and, as the aircraft passed about one third of a mile north of the marker beacon inbound, descending through approximately 1300 feet amsl, the handling pilot said "Over the beacon now". No audio signal from the marker beacon was heard on the cockpit voice recorder. The landing checklist was completed during the following 20 seconds, including confirmation that the undercarriage was down, fuel heaters were off, two blue propeller lights were illuminated and fuel was trimmed up. 48 seconds after passing the beacon the aircraft reached decision altitude, and the training captain asked the handling pilot "How long and where is it?", to which the handling pilot replied "Got about a minute and ten seconds to go - should be straight in front". 22 seconds later and some 36 seconds before impact the training captain said "Why are we at 650 feet?" and pointed out that the handling pilot had allowed the aircraft to descend below decision altitude when he was, for training purposes, still in IMC. The handling pilot responded by saying "Intend going around then", or words to that effect. The training captain then said "Yes, well I'll let you see it now. There it is". As the training captain was saying this, the sound of an engine power increase was heard on the CVR, and, about 25 seconds before impact, the rpm of one engine was increased to 14,800 rpm, a setting 200 rpm below maximum continuous power. 10 seconds later the training captain was heard to say "Hang on, that's the - that's the field there. See it?" The handling pilot then said "Hold tight", at which point, some 13 seconds before impact, the CVR recorded the sound of another engine increasing power to 14,800 rpm. A moment later the handling pilot said "Haven't got it", and the training captain said "I've got it". The F-27 yawed to the left before banking steeply to the right. The aircraft struck the ground on the northern side of the Castle Donington motor racing circuit in a nose-down attitude, banked to the left and with considerable left sideslip. After the accident an accumulation of mixed rime and glaze ice was found on the leading edges of the wings and tail surfaces which had formed rough-surfaced horns one inch high above and below the airflow stagnation point. No ice was found on the flaps or landing gear.
Aircraft reference details include registration G-BMAU, MSN 10241, year of manufacture 1963.
Geospatial coordinates for this crash are approximately 52.8281°, -1.3327°.
Fatalities
Total
0
Crew
0
Passengers
0
Other
0
Crash Summary
The BMA Fokker F-27 aircraft was engaged on crew training at East Midlands Airport (EMA). The commander, who was an experienced training captain, occupied the right pilot's seat and a first officer undergoing training for conversion to captaincy occupied the left seat as handling pilot. Another captain refreshing on type sat on the jump seat behind the pilots' seats, the intention being that he should move into the left seat after the first officer's training period. The weather was: wind 150 degrees at 7 kts, visibility 4 km and cloud 7 oktas stratus, base 1000 feet. The surface temperature was 2 °C and the QNH 1030. The training session began with a practice abandoned takeoff after which the aircraft took off at 13:08 and flew three practice ILS approaches followed by touch-and-go landings on runway 09, climbing to 2000 feet above mean sea level (amsl) after each takeoff. The runway in use was then changed and the aircraft flew a simulated asymmetric ILS approach to runway 27 followed by a missed approach (go-around) with the left engine throttled back. The runway was then changed again and an ILS approach to runway 09 was flown with the left engine still throttled back. This approach was followed by a touch-and-go landing during which both engines were brought up to full power. Very soon after becoming airborne the training captain again simulated failure of the left engine and the aircraft was climbed to 2000 feet amsl. Soon after the aircraft levelled off, the handling pilot commented on the large amount of rudder required to counteract the simulated failure of the left engine after takeoff. The training captain then said that he was deliberately putting more drag on the left side than would have been the case if the propeller had auto-feathered so that the climb performance corresponded better with that of an aircraft with passengers on board. He went on to say that if the handling pilot could cope with that extra drag, he could expect to control the aircraft if the failed engine auto-feathered because the rudder pedal force would then not be quite so great. The crew then began a procedural NDB approach to runway 09, for which instrument screens were fitted in front of the handling pilot. It was intended that the aircraft should be landed after the NDB approach for the pilot in the jump seat to take over as handling pilot. Decision altitude for the approach was 740 feet and touchdown altitude was 305 feet. It was company practice for beacon passage to be identified by the movement of the radio compass needle and, as the aircraft passed about one third of a mile north of the marker beacon inbound, descending through approximately 1300 feet amsl, the handling pilot said "Over the beacon now". No audio signal from the marker beacon was heard on the cockpit voice recorder. The landing checklist was completed during the following 20 seconds, including confirmation that the undercarriage was down, fuel heaters were off, two blue propeller lights were illuminated and fuel was trimmed up. 48 seconds after passing the beacon the aircraft reached decision altitude, and the training captain asked the handling pilot "How long and where is it?", to which the handling pilot replied "Got about a minute and ten seconds to go - should be straight in front". 22 seconds later and some 36 seconds before impact the training captain said "Why are we at 650 feet?" and pointed out that the handling pilot had allowed the aircraft to descend below decision altitude when he was, for training purposes, still in IMC. The handling pilot responded by saying "Intend going around then", or words to that effect. The training captain then said "Yes, well I'll let you see it now. There it is". As the training captain was saying this, the sound of an engine power increase was heard on the CVR, and, about 25 seconds before impact, the rpm of one engine was increased to 14,800 rpm, a setting 200 rpm below maximum continuous power. 10 seconds later the training captain was heard to say "Hang on, that's the - that's the field there. See it?" The handling pilot then said "Hold tight", at which point, some 13 seconds before impact, the CVR recorded the sound of another engine increasing power to 14,800 rpm. A moment later the handling pilot said "Haven't got it", and the training captain said "I've got it". The F-27 yawed to the left before banking steeply to the right. The aircraft struck the ground on the northern side of the Castle Donington motor racing circuit in a nose-down attitude, banked to the left and with considerable left sideslip. After the accident an accumulation of mixed rime and glaze ice was found on the leading edges of the wings and tail surfaces which had formed rough-surfaced horns one inch high above and below the airflow stagnation point. No ice was found on the flaps or landing gear.
Cause: Human factor
Occupants & Outcome
Crew On Board
3
Passengers On Board
0
Estimated Survivors
3
Fatality Rate
0.0%
Known people on board: 3
Operational Details
Schedule / Flight
East Midlands - East Midlands
Operator
British Midland Airways - BMAFlight Type
Training
Flight Phase
Landing (descent or approach)
Crash Site
Airport (less than 10 km from airport)
Region / Country
Europe • United Kingdom
Aircraft Details
Similar Plane Crashes
Handley Page Aircraft Company Ltd
Handley Page V/1500
Assembled at Cricklewood Airfield in May 1918, the aircraft departed Cricklewood for its 13th test flight, carrying six crew members. Shortly after takeoff, while climbing to a height of about 700-800 feet, all four engines stopped. The pilot elected to return for an emergency landing when the aircraft stalled and crashed in a field located in front of 21 Garrick Avenue in Golders Green, bursting into flames. Colonel Ogilvie, who was seating in the tail gunner position at the back of the plane, survived, while all five other occupants were killed. Crew: Cpt Vernon Earl George Busby, pilot, † Mr. Bertram G. Cooper, † Mr. R. P. Cooper, † Mr. W. H. Hathaway, † Mr. J. W. Windebank, † Colonel Ogilvie.
Marine Aeroplane Depot
Fairey III
The pilot departed Isle of Grain on a delivery flight to Glasgow-Renfrew Airport. On approach to RAF Usworth (RAF Hylton), he elected to make a go-around when the aircraft lost height and crashed. The aircraft was destroyed and the pilot, Captain Arthur Leslie Simms, was killed.
Royal Air Force - RAF
De Havilland DH.6
The crew was completing a local training flight at RAF Seaton Carew when the aircraft entered a spin and crashed in a field, bursting into flames. Both occupants were killed. Crew: Cpt Charles David Danby, pilot, 1st Class E. A. Bannister, mechanic.
Royal Air Force - RAF
Handley Page H.P.12
The aircraft departed Castle Bromwich for a test flight, carrying five engineers and two crew members. En route, the twin engine aircraft suffered technical problems with a wing, lost height and crashed in a field located in Maxstoke. The aircraft was destroyed and all seven occupants were killed. Crew: Lt Robert Edward Macbeth, Lt Frederick James Bravery, 1st Air Mechanic James Benjamn May, 2nd Air Mechanic Albert J. Winrow, 2nd Air Mechanic H. Simmonds, 3rd Air Mechanic Charles William Offord, 3rd George Greenland.
Royal Air Force - RAF
Blackburn R.T.1 Kangaroo
On final approach in bad visibility, aircraft was too low. It struck the ground short of runway and crashed. Both occupants were injured. Crew was performing a training flight on behalf of the 246th Squadron.
Royal Air Force - RAF
De Havilland DH.9
The pilot tried to return to his base but due to low visibility by night, he lost his orientation. He elected to make an emergency landing in an open field but the aircraft hit a tree and crashed. The pilot was injured.
