Dallas - Teterboro

Airplane crashed during a uncontrolled descent, following a turbulence upset at FL370. The upset occurred as a result of clear air turbulences associated with a vip level 6 thunderstorm located within 7 miles of the last position of the airplane. After the upset, the airplane penetrated and descended thru the cell which contained lightning, extreme turbulences and severe icing. During the upset/descent both engines flamed out and the crew's attempts to recover the airplane were unsuccessful due to conditions in the cell. Crew received an improper briefing from FSS and reported their radar was malfunctioning to the deputy controller. Sigmet and AWW info was not given during the briefing. As the airplane came out of the bottom of the cell at 4,000 feet, the crew overstressed the airplane causing the left main landing door to separate and hit the left horizontal stab which subsequently separated in overload. Impact was 82° nose down. Nature of the airplane radar malfunction could not be determined. All seven occupants were killed.

Flight / Schedule

Dallas - Teterboro

Registration

N50SK

MSN

309

Year of Manufacture

1980

Date

April 4, 1986 at 07:22 PM

Type

CRASH

Flight Type

Executive/Corporate/Business

Flight Phase

Flight

Crash Site

Plain, Valley

Crash Location

Redwater Texas

Region

North America • United States of America

Coordinates

33.3582°, -94.2544°

Crash Cause

Weather

Narrative Report

On April 4, 1986 at 07:22 PM, Dallas - Teterboro experienced a crash involving IAI 1124 Westwind, operated by Drayton Associates, with the event recorded near Redwater Texas.

The flight was categorized as executive/corporate/business and the reported phase was flight at a plain, valley crash site.

7 people were known to be on board, 7 fatalities were recorded, 0 survivors were identified or estimated. This corresponds to an estimated fatality rate of 100.0%.

Crew on board: 2, crew fatalities: 2, passengers on board: 5, passenger fatalities: 5, other fatalities: 0.

The listed crash cause is weather. Airplane crashed during a uncontrolled descent, following a turbulence upset at FL370. The upset occurred as a result of clear air turbulences associated with a vip level 6 thunderstorm located within 7 miles of the last position of the airplane. After the upset, the airplane penetrated and descended thru the cell which contained lightning, extreme turbulences and severe icing. During the upset/descent both engines flamed out and the crew's attempts to recover the airplane were unsuccessful due to conditions in the cell. Crew received an improper briefing from FSS and reported their radar was malfunctioning to the deputy controller. Sigmet and AWW info was not given during the briefing. As the airplane came out of the bottom of the cell at 4,000 feet, the crew overstressed the airplane causing the left main landing door to separate and hit the left horizontal stab which subsequently separated in overload. Impact was 82° nose down. Nature of the airplane radar malfunction could not be determined. All seven occupants were killed.

Aircraft reference details include registration N50SK, MSN 309, year of manufacture 1980.

Geospatial coordinates for this crash are approximately 33.3582°, -94.2544°.

Fatalities

Total

7

Crew

2

Passengers

5

Other

0

Crash Summary

Airplane crashed during a uncontrolled descent, following a turbulence upset at FL370. The upset occurred as a result of clear air turbulences associated with a vip level 6 thunderstorm located within 7 miles of the last position of the airplane. After the upset, the airplane penetrated and descended thru the cell which contained lightning, extreme turbulences and severe icing. During the upset/descent both engines flamed out and the crew's attempts to recover the airplane were unsuccessful due to conditions in the cell. Crew received an improper briefing from FSS and reported their radar was malfunctioning to the deputy controller. Sigmet and AWW info was not given during the briefing. As the airplane came out of the bottom of the cell at 4,000 feet, the crew overstressed the airplane causing the left main landing door to separate and hit the left horizontal stab which subsequently separated in overload. Impact was 82° nose down. Nature of the airplane radar malfunction could not be determined. All seven occupants were killed.

Cause: Weather

Occupants & Outcome

Crew On Board

2

Passengers On Board

5

Estimated Survivors

0

Fatality Rate

100.0%

Known people on board: 7

Operational Details

Schedule / Flight

Dallas - Teterboro

Flight Type

Executive/Corporate/Business

Flight Phase

Flight

Crash Site

Plain, Valley

Region / Country

North America • United States of America

Aircraft Details

Registration

N50SK

MSN

309

Year of Manufacture

1980