Hatfield - Hatfield
Flight / Schedule
Hatfield - Hatfield
Aircraft
Hawker Siddeley HS.121 TridentRegistration
G-ARPY
MSN
2126
Year of Manufacture
1965
Operator
Hawker Siddeley AircraftDate
June 3, 1966 at 06:35 PM
Type
CRASHFlight Type
Test
Flight Phase
Flight
Crash Site
Plain, Valley
Crash Location
Felthorpe Norfolk
Region
Europe • United Kingdom
Coordinates
52.7162°, 1.2061°
Crash Cause
Human factor
Narrative Report
On June 3, 1966 at 06:35 PM, Hatfield - Hatfield experienced a crash involving Hawker Siddeley HS.121 Trident, operated by Hawker Siddeley Aircraft, with the event recorded near Felthorpe Norfolk.
The flight was categorized as test and the reported phase was flight at a plain, valley crash site.
4 people were known to be on board, 4 fatalities were recorded, 0 survivors were identified or estimated. This corresponds to an estimated fatality rate of 100.0%.
Crew on board: 4, crew fatalities: 4, passengers on board: 0, passenger fatalities: 0, other fatalities: 0.
The listed crash cause is human factor. The aircraft took-off from Hatfield at 1652 hours to carry out the first of a series of production test flights for the purpose of qualifying for a Series Certificate of Airworthiness. The schedule for the flight called for stalling tests should the aircraft and the flight conditions be suitable. After take-off the aircraft climbed towards the north-east and at about 1830 hours, after completing the greater part of the flight test schedule, the stalling tests were begun. Three approaches to the stall were made in order to check the aircraft's stall warning and stall recovery systems and the flight engineer's log shows that with the aircraft in the landing configuration the stick shaker operated at 102 kt and the stall recovery system at 93 kt. The fourth stalling run was made at a height of 11 600 ft with the aircraft still in the landing configuration but, in accordance with the requirements of the test schedule, the stall warning and stall recovery systems had been made inoperative. Radio telephony communication with the aircraft consisted only of routine 11 messages until at 1834 hours when the pilot-in-command reported We are in a superstall at the moment". This was the last radiocommunication received. At about this time the aircraft was seen over Felthorpe flying very slowly heading south-west at about 10 000 ft. The nose was seen to go up 30 to 40 degrees and the aircraft began to turn to port; the starboard wing then dropped sharply and, following a short burst of engine power, the aircraft went into a flat spin to starboard. The spin continued, the aircraft turning once every 6 to 8 seconds until it reached the ground about a minute and a half later. All four crew members were killed.
Aircraft reference details include registration G-ARPY, MSN 2126, year of manufacture 1965.
Geospatial coordinates for this crash are approximately 52.7162°, 1.2061°.
Fatalities
Total
4
Crew
4
Passengers
0
Other
0
Crash Summary
The aircraft took-off from Hatfield at 1652 hours to carry out the first of a series of production test flights for the purpose of qualifying for a Series Certificate of Airworthiness. The schedule for the flight called for stalling tests should the aircraft and the flight conditions be suitable. After take-off the aircraft climbed towards the north-east and at about 1830 hours, after completing the greater part of the flight test schedule, the stalling tests were begun. Three approaches to the stall were made in order to check the aircraft's stall warning and stall recovery systems and the flight engineer's log shows that with the aircraft in the landing configuration the stick shaker operated at 102 kt and the stall recovery system at 93 kt. The fourth stalling run was made at a height of 11 600 ft with the aircraft still in the landing configuration but, in accordance with the requirements of the test schedule, the stall warning and stall recovery systems had been made inoperative. Radio telephony communication with the aircraft consisted only of routine 11 messages until at 1834 hours when the pilot-in-command reported We are in a superstall at the moment". This was the last radiocommunication received. At about this time the aircraft was seen over Felthorpe flying very slowly heading south-west at about 10 000 ft. The nose was seen to go up 30 to 40 degrees and the aircraft began to turn to port; the starboard wing then dropped sharply and, following a short burst of engine power, the aircraft went into a flat spin to starboard. The spin continued, the aircraft turning once every 6 to 8 seconds until it reached the ground about a minute and a half later. All four crew members were killed.
Cause: Human factor
Occupants & Outcome
Crew On Board
4
Passengers On Board
0
Estimated Survivors
0
Fatality Rate
100.0%
Known people on board: 4
Operational Details
Schedule / Flight
Hatfield - Hatfield
Operator
Hawker Siddeley AircraftFlight Type
Test
Flight Phase
Flight
Crash Site
Plain, Valley
Region / Country
Europe • United Kingdom
Aircraft Details
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