EPPS Air Service
Safety Score
9.8/10Total Incidents
3
Total Fatalities
7
Recent Incidents
Mitsubishi MU-2 Marquise
The pilot was finishing his third round-trip, Part 135 cargo flight. The first round trip began the previous evening, about 2150, and the approach back to the origination airport resulted in a landing on runway 15R at 2305. The second approach back to the origination airport resulted in a landing on runway 28 at 0230. Prior to the third approach back to the airport, the pilot was cleared for, and acknowledged a visual approach to runway 33R twice, at 0720, and at 0721. However, instead of proceeding to the runway, the airplane flew north of it, on a westerly track consistent with a modified downwind to runway 15L. During the westerly track, the airplane descended to 700 feet. Just prior to an abeam position for runway 15L, the airplane made a "sharp" left turn back toward the southeast, and descended into the ground. Witnesses reported the airplane's movements as "swaying motions as if it were going to bank left, then right, and back left again," and "the nose...pointing up more than anything...but doing a corkscrew motion." Other witnesses reported the "wings straight up and down," and "wings vertical." Tower controllers also noted the airplane to be "low and tight," and "in an unusually nose high attitude close to the ground. It then "banked left and appeared to stall and then crashed." A post-flight examination of the wreckage revealed no evidence of mechanical malfunction. The pilot, who reported 6,800 hours of flight time, had also flown multiple round trips the previous two evenings. He had checked into a hotel at 0745, the morning prior to the accident flight, checked out at 1956, the same day, and reported for work about 1 hour before the first flight began.
Canadair CL-604 Challenger
Following ATC clearance, engine start was at 1156 hrs and N90AG was cleared to taxi at 1201 hrs. All radio calls during the accident flight were made by the commander, seated in the right cockpit seat. During taxi, the crew completed their normal Before Takeoff Checks; these included confirmation that the control checks had been completed and that anti-ice might be required immediately after takeoff. Flap 20 had been selected for takeoff and the following speeds had been calculated and briefed by the pilots: V1 137 kt; VR 140 kt; V2 147 kt. By 1206 hrs, the aircraft was cleared to line up on Runway 15. At 1207 hrs, N90AG was cleared for takeoff with a surface wind of 140°/8 kt. The pilot in the left seat was handling the controls. Takeoff appeared normal up to lift-off. Rotation was started at about 146 kt with the elevator position being increased to 8°, in the aircraft nose up sense, resulting in an initial pitch rate of around 4°/second. Lift-off occurred 2 seconds later, at about 153 kt and with a pitch attitude of about 8° nose-up. Once airborne, the elevator position was reduced to 3° aircraft nose-up whilst the pitch rate increased to about 5°/second. Immediately after lift-off, the aircraft started to bank to the left. The rate of bank increased rapidly and 2 seconds after lift-off the bank angle had reached 50°. At that point, the aircraft heading had diverged about 10° to the left. Opposite aileron, followed closely by right rudder, was applied as the aircraft started banking; full right aileron and full right rudder had been applied within 1 second and were maintained until the end of the recording. As the bank angle continued to increase, progressively more aircraft nose-up elevator was applied. Stick-shaker operation initiated 3.5 seconds after lift-off and the recorders ceased 2 seconds later. The aircraft struck the ground, inverted, adjacent to the runway. The last recorded aircraft attitude was approximately 111° left bank and 13° nose-down pitch; the final recorded heading was about 114° (M). The aircraft was destroyed by impact forces and a post crash fire and all five occupants were killed, among them John Shumejda, President of the Massey-Ferguson Group and Ed Swingle, Vice President. The aircraft was leased by AGCO Massey-Ferguson.
Beechcraft 100 King Air
During arrival at night, Beechcraft A100 (King Air, N44UE) was cleared for an ILS runway 26R approach behind Continental flight 9687, then Eastern Airline (EA) flight 111 (Boeing 727, N8867E) was cleared for the same approach behind the King Air. After landing, flight 9687 had a radio problem and the tower controller had difficulty communicating with flight 9687. Meanwhile, the King Air landed and its crew had moved the aircraft to the right side of the runway near taxiway Delta (the primary taxiway for general aviation aircraft). The turnoff for taxiway Delta was about 3,800 feet from the approach end of runway 26R. Before the King Air was clear of the runway, EA111 landed and converged on the King Air. The crew of EA111 did not see the King Air until moments before the accident. The captain tried to avoid a collision, but the Boeing's right wing struck the King Air, shearing the top of its fuselage and cockpit. Some of the King Air's strobe/beacon lights were inoperative, though they most likely would have been extinguished for the IMC approach. The local controller did not issue a traffic advisory to EA111 with the landing clearance. One of the pilot on board the King Air was killed while the second was seriously injured.
Airline Information
Country of Origin
United States of America
Risk Level
Low Risk
