Atlas Air
Safety Score
9.9/10Total Incidents
3
Total Fatalities
3
Recent Incidents
Boeing 767-300
On February 23, 2019, at 1239 central standard time, Atlas Air Inc. (Atlas) flight 3591, a Boeing 767-375BCF, N1217A, was destroyed after it rapidly descended from an altitude of about 6,000 ft mean sea level (msl) and crashed into a shallow, muddy marsh area of Trinity Bay, Texas, about 41 miles east-southeast of George Bush Intercontinental/Houston Airport (IAH), Houston, Texas. The captain, first officer (FO), and a nonrevenue pilot riding in the jumpseat died. Atlas operated the airplane as a Title 14 Code of Federal Regulations Part 121 domestic cargo flight for Amazon.com Services LLC, and an instrument flight rules flight plan was filed. The flight departed from Miami International Airport (MIA), Miami, Florida, about 1033 (1133 eastern standard time) and was destined for IAH. The accident flight’s departure from MIA, en route cruise, and initial descent toward IAH were uneventful. As the flight descended toward the airport, the flight crew extended the speedbrakes, lowered the slats, and began setting up the flight management computer for the approach. The FO was the pilot flying, the captain was the pilot monitoring, and the autopilot and autothrottle were engaged and remained engaged for the remainder of the flight. Analysis of the available weather information determined that, about 1238:25, the airplane was beginning to penetrate the leading edge of a cold front, within which associated windshear and instrument meteorological conditions (as the flight continued) were likely. Flight data recorder data indicated that, during the time, aircraft load factors consistent with the airplane encountering light turbulence were recorded and, at 1238:31, the airplane’s go-around mode was activated. At the time, the accident flight was about 40 miles from IAH and descending through about 6,300 ft msl toward the target altitude of 3,000 ft msl. This location and phase of flight were inconsistent with any scenario in which a pilot would intentionally select go-around mode, and neither pilot made a go-around callout to indicate intentional activation. Within seconds of go-around mode activation, manual elevator control inputs overrode the autopilot and eventually forced the airplane into a steep dive from which the crew did not recover. Only 32 seconds elapsed between the go-around mode activation and the airplane’s ground impact.
Boeing 747-200
Shortly after take off from Lomé international Airport, while on a cargo flight to Amsterdam, the crew declared an emergency and was cleared for an immediate return. The approach and landing were considered as normal and the aircraft returned safely to the apron. While all three crew members were uninjured, the aircraft was damaged beyond repair due to bulkhead destruction.
Boeing 747-200
The aircraft departed Dubai on a cargo flight to Düsseldorf with three crew members on board. Following an uneventful flight, the crew established radio contact with Düsseldorf Radar at 0543LT. The crew were told that runway 23L was in use. Two minutes later the radar controller contacted flight 8995: "I just talked to the tower and ah for the time being braking action on all parts of the runway is supposed to be good. They are measuring again right now because it started to snow again and I'll keep you advised." The flight was then cleared to descend to FL80. The flight crew decided to set the autobrakes for landing on Medium, to account for the snow. At 05:50 the radar controller again contacted the flight about the current weather circumstances: "...latest update on the weather situation ahm the friction tester has reported braking action to be good for the moment however as its continuing to snow they are ah afraid that it might worsen, so they are going to do another friction test right before you land." In the following minutes the flight was given descent instructions and vectors for an approach to runway 23L. At 05:54 the controller radioed: "weather update we now have a surface wind of three four zero degrees eleven knots, that's slight tail wind component by two knots. Visibility is down to one thousand five hundred meters, still in snow showers and ah cloud base is now five hundred feet only." The flight was subsequently cleared for the approach. At 05:57 the radar controller instructed the crew to contact Düsseldorf Tower. The Tower controller stated: "Good morning,... we are just waiting for the braking action values from the friction tester stand by a second. The surface wind is actually three three zero degrees one two knots." Two minutes later the controller radioed: "... the braking action was measured to be medium at all parts. And ah the visibility dropped right now due to the heavy snow showers at the field ah. The RVR value at the touchdown zone is presently nine hundred meters, at the mid-point one thousand one hundred meters and ah stop end one thousand one hundred meters." At that moment the flight was 3,5 nautical miles out. The flight was subsequently cleared to land. The airplane touched down about 1700 ft (518 m) past the runway threshold. Ground spoilers and thrust reversers deployed and the autobrakes activated. Still the airplane did not decelerate as expected and the pilot applied manual braking. The airplane failed to stop and overran the runway end. It collided with ILS equipments, which caused a fire in engines n°2 and 3. All three crew members evacuated safely and the aircraft was considered as damaged beyond repair.
Airline Information
Country of Origin
United States of America
Risk Level
Low Risk
