Linton-on-Ouse - Linton-on-Ouse

The aircraft left RAF Linton-on-Ouse at 1605LT on December 2nd on a bombing mission to Lorient, France. On the return trip, the crew lost his orientation and decided to divert to the RAF Cold Kirby airfield which is not suitable for this kind of aircraft. After touch down on a grassy runway, the aircraft went out of control and came to rest. All crew members were unhurt but the aircraft was damaged beyond repair. Crew (58th Squadron): Sgt Ronald Albert Gosling, pilot, P/O Jack Gordon Kerry, copilot, Sgt Reginald Denis Kirby, observer, Sgt Patrick William Kenealy Crisp, wireless operator, Sgt John Grange Uff, air gunner.

Flight / Schedule

Linton-on-Ouse - Linton-on-Ouse

Registration

T4207

Date

December 3, 1940 at 07:00 AM

Type

CRASH

Flight Type

Bombing

Flight Phase

Landing (descent or approach)

Crash Site

Airport (less than 10 km from airport)

Crash Location

Cold Kirby AFB North Yorkshire

Region

Europe • United Kingdom

Crash Cause

Human factor

Narrative Report

On December 3, 1940 at 07:00 AM, Linton-on-Ouse - Linton-on-Ouse experienced a crash involving Armstrong Whitworth AW.38 Whitley, operated by Royal Air Force - RAF, with the event recorded near Cold Kirby AFB North Yorkshire.

The flight was categorized as bombing and the reported phase was landing (descent or approach) at a airport (less than 10 km from airport) crash site.

5 people were known to be on board, 0 fatalities were recorded, 5 survivors were identified or estimated. This corresponds to an estimated fatality rate of 0.0%.

Crew on board: 5, crew fatalities: 0, passengers on board: 0, passenger fatalities: 0, other fatalities: 0.

The listed crash cause is human factor. The aircraft left RAF Linton-on-Ouse at 1605LT on December 2nd on a bombing mission to Lorient, France. On the return trip, the crew lost his orientation and decided to divert to the RAF Cold Kirby airfield which is not suitable for this kind of aircraft. After touch down on a grassy runway, the aircraft went out of control and came to rest. All crew members were unhurt but the aircraft was damaged beyond repair. Crew (58th Squadron): Sgt Ronald Albert Gosling, pilot, P/O Jack Gordon Kerry, copilot, Sgt Reginald Denis Kirby, observer, Sgt Patrick William Kenealy Crisp, wireless operator, Sgt John Grange Uff, air gunner.

Aircraft reference details include registration T4207.

Fatalities

Total

0

Crew

0

Passengers

0

Other

0

Crash Summary

The aircraft left RAF Linton-on-Ouse at 1605LT on December 2nd on a bombing mission to Lorient, France. On the return trip, the crew lost his orientation and decided to divert to the RAF Cold Kirby airfield which is not suitable for this kind of aircraft. After touch down on a grassy runway, the aircraft went out of control and came to rest. All crew members were unhurt but the aircraft was damaged beyond repair. Crew (58th Squadron): Sgt Ronald Albert Gosling, pilot, P/O Jack Gordon Kerry, copilot, Sgt Reginald Denis Kirby, observer, Sgt Patrick William Kenealy Crisp, wireless operator, Sgt John Grange Uff, air gunner.

Cause: Human factor

Occupants & Outcome

Crew On Board

5

Passengers On Board

0

Estimated Survivors

5

Fatality Rate

0.0%

Known people on board: 5

Operational Details

Schedule / Flight

Linton-on-Ouse - Linton-on-Ouse

Flight Type

Bombing

Flight Phase

Landing (descent or approach)

Crash Site

Airport (less than 10 km from airport)

Region / Country

Europe • United Kingdom

Aircraft Details

Registration

T4207

Similar Plane Crashes

June 8, 1918 at 12:00 AM5 Fatalities

Handley Page Aircraft Company Ltd

Handley Page V/1500

Assembled at Cricklewood Airfield in May 1918, the aircraft departed Cricklewood for its 13th test flight, carrying six crew members. Shortly after takeoff, while climbing to a height of about 700-800 feet, all four engines stopped. The pilot elected to return for an emergency landing when the aircraft stalled and crashed in a field located in front of 21 Garrick Avenue in Golders Green, bursting into flames. Colonel Ogilvie, who was seating in the tail gunner position at the back of the plane, survived, while all five other occupants were killed. Crew: Cpt Vernon Earl George Busby, pilot, † Mr. Bertram G. Cooper, † Mr. R. P. Cooper, † Mr. W. H. Hathaway, † Mr. J. W. Windebank, † Colonel Ogilvie.

June 11, 1918 at 12:00 AM1 Fatalities

Royal Air Force - RAF

Avro 504

The single engine aircraft was completing a local training flight when it stalled and crashed near Abukir. A crew member was killed and the second was injured. Crew: 2nd Lt G. E. Satterthwaite, † 2nd Lt J. Acheson.

July 14, 1918 at 12:00 AM1 Fatalities

Marine Aeroplane Depot

Fairey III

The pilot departed Isle of Grain on a delivery flight to Glasgow-Renfrew Airport. On approach to RAF Usworth (RAF Hylton), he elected to make a go-around when the aircraft lost height and crashed. The aircraft was destroyed and the pilot, Captain Arthur Leslie Simms, was killed.

July 18, 1918 at 12:00 AM2 Fatalities

Royal Air Force - RAF

De Havilland DH.6

The crew was completing a local training flight at RAF Seaton Carew when the aircraft entered a spin and crashed in a field, bursting into flames. Both occupants were killed. Crew: Cpt Charles David Danby, pilot, 1st Class E. A. Bannister, mechanic.

August 19, 1918 at 03:15 PM7 Fatalities

Royal Air Force - RAF

Handley Page H.P.12

The aircraft departed Castle Bromwich for a test flight, carrying five engineers and two crew members. En route, the twin engine aircraft suffered technical problems with a wing, lost height and crashed in a field located in Maxstoke. The aircraft was destroyed and all seven occupants were killed. Crew: Lt Robert Edward Macbeth, Lt Frederick James Bravery, 1st Air Mechanic James Benjamn May, 2nd Air Mechanic Albert J. Winrow, 2nd Air Mechanic H. Simmonds, 3rd Air Mechanic Charles William Offord, 3rd George Greenland.

August 26, 1918 at 12:00 AM

Royal Air Force - RAF

Blackburn R.T.1 Kangaroo

On final approach in bad visibility, aircraft was too low. It struck the ground short of runway and crashed. Both occupants were injured. Crew was performing a training flight on behalf of the 246th Squadron.