Broomfield – Loveland

The commercial pilot was relocating the multiengine airplane following the completion of an extensive avionics upgrade, which also included the installation of new fuel flow transducers. As the pilot neared the destination airport, he reported over the common traffic advisory frequency that he had "an engine out [and] smoke in the cockpit." Witnesses observed and airport surveillance video showed fire emanating from the airplane's right wing. As the airplane turned towards the runway, it entered a rightrolling descent and impacted the ground near the airport's perimeter fence. The right propeller was found feathered. Examination of the right engine revealed evidence of a fire aft of the engine-driven fuel pump. The fuel pump was discolored by the fire. The fire sleeves on both the fuel pump inlet and outlet hoses were burned away. The fuel outlet hose from the fuel pump to the flow transducer was found loose. The reason the hose was loose was not determined. It is likely that pressurized fuel sprayed from the fuel pump outlet hose and was ignited by the hot turbocharger, which resulted in the inflight fire.

Flight / Schedule

Broomfield – Loveland

Registration

N60RK

MSN

P-79

Year of Manufacture

1969

Date

May 15, 2019 at 12:48 PM

Type

CRASH

Flight Type

Ferry

Flight Phase

Landing (descent or approach)

Crash Site

Airport (less than 10 km from airport)

Crash Location

Loveland Colorado

Region

North America • United States of America

Coordinates

40.3978°, -105.0750°

Crash Cause

Technical failure

Narrative Report

On May 15, 2019 at 12:48 PM, Broomfield – Loveland experienced a crash involving Beechcraft 60 Duke, operated by Private American, with the event recorded near Loveland Colorado.

The flight was categorized as ferry and the reported phase was landing (descent or approach) at a airport (less than 10 km from airport) crash site.

1 people were known to be on board, 1 fatalities were recorded, 0 survivors were identified or estimated. This corresponds to an estimated fatality rate of 100.0%.

Crew on board: 1, crew fatalities: 1, passengers on board: 0, passenger fatalities: 0, other fatalities: 0.

The listed crash cause is technical failure. The commercial pilot was relocating the multiengine airplane following the completion of an extensive avionics upgrade, which also included the installation of new fuel flow transducers. As the pilot neared the destination airport, he reported over the common traffic advisory frequency that he had "an engine out [and] smoke in the cockpit." Witnesses observed and airport surveillance video showed fire emanating from the airplane's right wing. As the airplane turned towards the runway, it entered a rightrolling descent and impacted the ground near the airport's perimeter fence. The right propeller was found feathered. Examination of the right engine revealed evidence of a fire aft of the engine-driven fuel pump. The fuel pump was discolored by the fire. The fire sleeves on both the fuel pump inlet and outlet hoses were burned away. The fuel outlet hose from the fuel pump to the flow transducer was found loose. The reason the hose was loose was not determined. It is likely that pressurized fuel sprayed from the fuel pump outlet hose and was ignited by the hot turbocharger, which resulted in the inflight fire.

Aircraft reference details include registration N60RK, MSN P-79, year of manufacture 1969.

Geospatial coordinates for this crash are approximately 40.3978°, -105.0750°.

Fatalities

Total

1

Crew

1

Passengers

0

Other

0

Crash Summary

The commercial pilot was relocating the multiengine airplane following the completion of an extensive avionics upgrade, which also included the installation of new fuel flow transducers. As the pilot neared the destination airport, he reported over the common traffic advisory frequency that he had "an engine out [and] smoke in the cockpit." Witnesses observed and airport surveillance video showed fire emanating from the airplane's right wing. As the airplane turned towards the runway, it entered a rightrolling descent and impacted the ground near the airport's perimeter fence. The right propeller was found feathered. Examination of the right engine revealed evidence of a fire aft of the engine-driven fuel pump. The fuel pump was discolored by the fire. The fire sleeves on both the fuel pump inlet and outlet hoses were burned away. The fuel outlet hose from the fuel pump to the flow transducer was found loose. The reason the hose was loose was not determined. It is likely that pressurized fuel sprayed from the fuel pump outlet hose and was ignited by the hot turbocharger, which resulted in the inflight fire.

Cause: Technical failure

Occupants & Outcome

Crew On Board

1

Passengers On Board

0

Estimated Survivors

0

Fatality Rate

100.0%

Known people on board: 1

Operational Details

Schedule / Flight

Broomfield – Loveland

Flight Type

Ferry

Flight Phase

Landing (descent or approach)

Crash Site

Airport (less than 10 km from airport)

Region / Country

North America • United States of America

Aircraft Details

Registration

N60RK

MSN

P-79

Year of Manufacture

1969