Waukegan – Winnipeg

The commercial pilot of the multi-engine airplane was conducting an instrument flight rules cross-country flight at night. The pilot checked in with air traffic control at a cruise altitude about 10,000 ft mean sea level (msl). About 31 minutes later, the pilot reported that he saw lightning off the airplane's left wing. The controller advised the pilot that the weather appeared to be about 35 to 40 miles away and that the airplane should be well clear of it. The pilot responded to the controller that he had onboard weather radar and agreed that they would fly clear of the weather. There were no further communications from the pilot. About 4 minutes later, radar information showed the airplane at 10,400 ft msl. About 1 minute later, radar showed the airplane in a descending right turn at 9,400 ft. Radar contact was lost shortly thereafter. The distribution of the wreckage, which was scattered in an area with about a 1/4-mile radius, was consistent with an in-flight breakup. The left horizontal stabilizer and significant portions of both left and right elevators and their respective trim tabs were not found. Of the available components for examination, no pre-impact airframe structural anomalies were found. Examination of the engines and turbochargers did not reveal any pre-impact anomalies. Examination of the propellers showed evidence of rotation at impact and no pre-impact anomalies. Review of weather information indicated that no convection or thunderstorms were coincident with or near the airplane's route of flight, and the nearest convective activity was located about 25 miles west of the accident site. Autopsy and toxicology testing revealed no evidence of pilot impairment or incapacitation. Given the lack of radar information after the airplane passed through 9,400 ft, it is likely that it entered a rapid descent during which it exceeded its design stress limitations, which resulted in the in-flight breakup; however, based on the available information, the event that precipitated the descent and loss of control could not be determined.

Flight / Schedule

Waukegan – Winnipeg

Registration

N2655B

MSN

421C-0698

Year of Manufacture

1979

Date

July 1, 2017 at 01:53 AM

Type

CRASH

Flight Type

Private

Flight Phase

Flight

Crash Site

Plain, Valley

Crash Location

Catawba Wisconsin

Region

North America • United States of America

Coordinates

45.5364°, -90.5299°

Narrative Report

On July 1, 2017 at 01:53 AM, Waukegan – Winnipeg experienced a crash involving Cessna 421C Golden Eagle III, operated by Sky King Flying Service, with the event recorded near Catawba Wisconsin.

The flight was categorized as private and the reported phase was flight at a plain, valley crash site.

6 people were known to be on board, 6 fatalities were recorded, 0 survivors were identified or estimated. This corresponds to an estimated fatality rate of 100.0%.

Crew on board: 1, crew fatalities: 1, passengers on board: 5, passenger fatalities: 5, other fatalities: 0.

The commercial pilot of the multi-engine airplane was conducting an instrument flight rules cross-country flight at night. The pilot checked in with air traffic control at a cruise altitude about 10,000 ft mean sea level (msl). About 31 minutes later, the pilot reported that he saw lightning off the airplane's left wing. The controller advised the pilot that the weather appeared to be about 35 to 40 miles away and that the airplane should be well clear of it. The pilot responded to the controller that he had onboard weather radar and agreed that they would fly clear of the weather. There were no further communications from the pilot. About 4 minutes later, radar information showed the airplane at 10,400 ft msl. About 1 minute later, radar showed the airplane in a descending right turn at 9,400 ft. Radar contact was lost shortly thereafter. The distribution of the wreckage, which was scattered in an area with about a 1/4-mile radius, was consistent with an in-flight breakup. The left horizontal stabilizer and significant portions of both left and right elevators and their respective trim tabs were not found. Of the available components for examination, no pre-impact airframe structural anomalies were found. Examination of the engines and turbochargers did not reveal any pre-impact anomalies. Examination of the propellers showed evidence of rotation at impact and no pre-impact anomalies. Review of weather information indicated that no convection or thunderstorms were coincident with or near the airplane's route of flight, and the nearest convective activity was located about 25 miles west of the accident site. Autopsy and toxicology testing revealed no evidence of pilot impairment or incapacitation. Given the lack of radar information after the airplane passed through 9,400 ft, it is likely that it entered a rapid descent during which it exceeded its design stress limitations, which resulted in the in-flight breakup; however, based on the available information, the event that precipitated the descent and loss of control could not be determined.

Aircraft reference details include registration N2655B, MSN 421C-0698, year of manufacture 1979.

Geospatial coordinates for this crash are approximately 45.5364°, -90.5299°.

Fatalities

Total

6

Crew

1

Passengers

5

Other

0

Crash Summary

The commercial pilot of the multi-engine airplane was conducting an instrument flight rules cross-country flight at night. The pilot checked in with air traffic control at a cruise altitude about 10,000 ft mean sea level (msl). About 31 minutes later, the pilot reported that he saw lightning off the airplane's left wing. The controller advised the pilot that the weather appeared to be about 35 to 40 miles away and that the airplane should be well clear of it. The pilot responded to the controller that he had onboard weather radar and agreed that they would fly clear of the weather. There were no further communications from the pilot. About 4 minutes later, radar information showed the airplane at 10,400 ft msl. About 1 minute later, radar showed the airplane in a descending right turn at 9,400 ft. Radar contact was lost shortly thereafter. The distribution of the wreckage, which was scattered in an area with about a 1/4-mile radius, was consistent with an in-flight breakup. The left horizontal stabilizer and significant portions of both left and right elevators and their respective trim tabs were not found. Of the available components for examination, no pre-impact airframe structural anomalies were found. Examination of the engines and turbochargers did not reveal any pre-impact anomalies. Examination of the propellers showed evidence of rotation at impact and no pre-impact anomalies. Review of weather information indicated that no convection or thunderstorms were coincident with or near the airplane's route of flight, and the nearest convective activity was located about 25 miles west of the accident site. Autopsy and toxicology testing revealed no evidence of pilot impairment or incapacitation. Given the lack of radar information after the airplane passed through 9,400 ft, it is likely that it entered a rapid descent during which it exceeded its design stress limitations, which resulted in the in-flight breakup; however, based on the available information, the event that precipitated the descent and loss of control could not be determined.

Occupants & Outcome

Crew On Board

1

Passengers On Board

5

Estimated Survivors

0

Fatality Rate

100.0%

Known people on board: 6

Operational Details

Schedule / Flight

Waukegan – Winnipeg

Flight Type

Private

Flight Phase

Flight

Crash Site

Plain, Valley

Region / Country

North America • United States of America

Aircraft Details

Registration

N2655B

MSN

421C-0698

Year of Manufacture

1979