Anniston - Ray

The private pilot reported that, while on a left downwind in the airport traffic pattern after conducting a cross-country business flight, he extended the flaps 10 degrees. While on short final, he fully extended the flaps, and shortly after, the left wing dropped. The pilot attempted to correct the left wing drop by applying right aileron and rudder; however, the airplane did not respond. The pilot chose to conduct a go-around and increased engine power. The airplane subsequently pitched up, and the left turn steepened. The pilot subsequently reduced engine power, and the airplane began to descend. The airplane struck the ground short of the runway, and the left wing separated from the fuselage. The examination of the airframe, flight controls, and engine revealed no preimpact mechanical anomalies that would have precluded normal operation. Examination of the trim system revealed that the right aileron trim and the left rudder trim were in positions that would have resulted in a right turn and a left yaw. Further, a witness reported that the airplane appeared to be in a cross-controlled attitude while on final approach to the airport. It is likely that the pilot’s improper use of the trim led to a cross-controlled situation and resulted in the subsequent stall during the attempted go-around.

Flight / Schedule

Anniston - Ray

Aircraft

Comp Air CA-8

Registration

N224MS

MSN

0652843

Year of Manufacture

2006

Operator

Paul R. Boak

Date

October 15, 2015 at 06:10 PM

Type

CRASH

Flight Type

Executive/Corporate/Business

Flight Phase

Landing (descent or approach)

Crash Site

Airport (less than 10 km from airport)

Crash Location

Ray Michigan

Region

North America • United States of America

Coordinates

41.7599°, -84.8721°

Crash Cause

Human factor

Narrative Report

On October 15, 2015 at 06:10 PM, Anniston - Ray experienced a crash involving Comp Air CA-8, operated by Paul R. Boak, with the event recorded near Ray Michigan.

The flight was categorized as executive/corporate/business and the reported phase was landing (descent or approach) at a airport (less than 10 km from airport) crash site.

1 people were known to be on board, 0 fatalities were recorded, 1 survivors were identified or estimated. This corresponds to an estimated fatality rate of 0.0%.

Crew on board: 1, crew fatalities: 0, passengers on board: 0, passenger fatalities: 0, other fatalities: 0.

The listed crash cause is human factor. The private pilot reported that, while on a left downwind in the airport traffic pattern after conducting a cross-country business flight, he extended the flaps 10 degrees. While on short final, he fully extended the flaps, and shortly after, the left wing dropped. The pilot attempted to correct the left wing drop by applying right aileron and rudder; however, the airplane did not respond. The pilot chose to conduct a go-around and increased engine power. The airplane subsequently pitched up, and the left turn steepened. The pilot subsequently reduced engine power, and the airplane began to descend. The airplane struck the ground short of the runway, and the left wing separated from the fuselage. The examination of the airframe, flight controls, and engine revealed no preimpact mechanical anomalies that would have precluded normal operation. Examination of the trim system revealed that the right aileron trim and the left rudder trim were in positions that would have resulted in a right turn and a left yaw. Further, a witness reported that the airplane appeared to be in a cross-controlled attitude while on final approach to the airport. It is likely that the pilot’s improper use of the trim led to a cross-controlled situation and resulted in the subsequent stall during the attempted go-around.

Aircraft reference details include registration N224MS, MSN 0652843, year of manufacture 2006.

Geospatial coordinates for this crash are approximately 41.7599°, -84.8721°.

Fatalities

Total

0

Crew

0

Passengers

0

Other

0

Crash Summary

The private pilot reported that, while on a left downwind in the airport traffic pattern after conducting a cross-country business flight, he extended the flaps 10 degrees. While on short final, he fully extended the flaps, and shortly after, the left wing dropped. The pilot attempted to correct the left wing drop by applying right aileron and rudder; however, the airplane did not respond. The pilot chose to conduct a go-around and increased engine power. The airplane subsequently pitched up, and the left turn steepened. The pilot subsequently reduced engine power, and the airplane began to descend. The airplane struck the ground short of the runway, and the left wing separated from the fuselage. The examination of the airframe, flight controls, and engine revealed no preimpact mechanical anomalies that would have precluded normal operation. Examination of the trim system revealed that the right aileron trim and the left rudder trim were in positions that would have resulted in a right turn and a left yaw. Further, a witness reported that the airplane appeared to be in a cross-controlled attitude while on final approach to the airport. It is likely that the pilot’s improper use of the trim led to a cross-controlled situation and resulted in the subsequent stall during the attempted go-around.

Cause: Human factor

Occupants & Outcome

Crew On Board

1

Passengers On Board

0

Estimated Survivors

1

Fatality Rate

0.0%

Known people on board: 1

Operational Details

Schedule / Flight

Anniston - Ray

Operator

Paul R. Boak

Flight Type

Executive/Corporate/Business

Flight Phase

Landing (descent or approach)

Crash Site

Airport (less than 10 km from airport)

Region / Country

North America • United States of America

Aircraft Details

Aircraft

Comp Air CA-8

Registration

N224MS

MSN

0652843

Year of Manufacture

2006

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