Washington - Louisburg

The airline transport pilot was conducting a cross-country aerial observation flight in the multiengine airplane. The pilot reported that the airplane was on the final leg of the traffic pattern when he reduced the power levers for landing and noticed that the right engine sounded like the propeller was moving toward the beta position. The pilot increased the engine power, and the sound stopped. As the airplane got closer to the runway, he decreased the engine power, and the sound returned. In addition, the airplane began to yaw right. The pilot applied left aileron and rudder inputs to remain above the runway centerline without success. While over the runway, the pilot reduced the engine power to idle, and the airplane continued to yaw right. The pilot applied full power in an attempt to perform a go-around; however, the airplane yawed about 30 degrees off the runway centerline, touched down in the grass, and impacted trees before coming to rest. The right wing, right engine, and right propeller assembly were impact-separated. The right engine propeller came to rest about 50 ft forward of the main wreckage, and it was found in the feathered position. A review of maintenance records revealed that the right propeller had been overhauled and reinstalled on the airplane 2 days before the accident and had operated 9 hours since that time. Subsequent testing of the right propeller governor revealed that it functioned without anomaly; however, the speed settings were improperly configured. Further, the testing revealed that the beta valve travel from the neutral position was out of tolerance. Although this could have let oil pressure port to one side of the spool or the other and, thus, changed the propeller blade angle, it could not be determined whether this occurred during the accident landing. Impact damage precluded examination of the right propeller governor control linkage; therefore, it could not be determined if it was inadequately installed or rigged, which could have resulted in the propeller moving into the beta position. The investigation could not determine why the right propeller moved toward the beta position as engine power was reduced, as reported the pilot.

Flight / Schedule

Washington - Louisburg

Registration

N181CS

MSN

181

Year of Manufacture

1968

Date

September 6, 2015 at 03:40 PM

Type

CRASH

Flight Type

Survey / Patrol / Reconnaissance

Flight Phase

Landing (descent or approach)

Crash Site

Airport (less than 10 km from airport)

Crash Location

Louisburg-North Raleigh North Carolina

Region

North America • United States of America

Coordinates

35.8032°, -78.6220°

Crash Cause

Technical failure

Narrative Report

On September 6, 2015 at 03:40 PM, Washington - Louisburg experienced a crash involving De Havilland DHC-6 Twin Otter, operated by Rampart Aviation, with the event recorded near Louisburg-North Raleigh North Carolina.

The flight was categorized as survey / patrol / reconnaissance and the reported phase was landing (descent or approach) at a airport (less than 10 km from airport) crash site.

3 people were known to be on board, 0 fatalities were recorded, 3 survivors were identified or estimated. This corresponds to an estimated fatality rate of 0.0%.

Crew on board: 2, crew fatalities: 0, passengers on board: 1, passenger fatalities: 0, other fatalities: 0.

The listed crash cause is technical failure. The airline transport pilot was conducting a cross-country aerial observation flight in the multiengine airplane. The pilot reported that the airplane was on the final leg of the traffic pattern when he reduced the power levers for landing and noticed that the right engine sounded like the propeller was moving toward the beta position. The pilot increased the engine power, and the sound stopped. As the airplane got closer to the runway, he decreased the engine power, and the sound returned. In addition, the airplane began to yaw right. The pilot applied left aileron and rudder inputs to remain above the runway centerline without success. While over the runway, the pilot reduced the engine power to idle, and the airplane continued to yaw right. The pilot applied full power in an attempt to perform a go-around; however, the airplane yawed about 30 degrees off the runway centerline, touched down in the grass, and impacted trees before coming to rest. The right wing, right engine, and right propeller assembly were impact-separated. The right engine propeller came to rest about 50 ft forward of the main wreckage, and it was found in the feathered position. A review of maintenance records revealed that the right propeller had been overhauled and reinstalled on the airplane 2 days before the accident and had operated 9 hours since that time. Subsequent testing of the right propeller governor revealed that it functioned without anomaly; however, the speed settings were improperly configured. Further, the testing revealed that the beta valve travel from the neutral position was out of tolerance. Although this could have let oil pressure port to one side of the spool or the other and, thus, changed the propeller blade angle, it could not be determined whether this occurred during the accident landing. Impact damage precluded examination of the right propeller governor control linkage; therefore, it could not be determined if it was inadequately installed or rigged, which could have resulted in the propeller moving into the beta position. The investigation could not determine why the right propeller moved toward the beta position as engine power was reduced, as reported the pilot.

Aircraft reference details include registration N181CS, MSN 181, year of manufacture 1968.

Geospatial coordinates for this crash are approximately 35.8032°, -78.6220°.

Fatalities

Total

0

Crew

0

Passengers

0

Other

0

Crash Summary

The airline transport pilot was conducting a cross-country aerial observation flight in the multiengine airplane. The pilot reported that the airplane was on the final leg of the traffic pattern when he reduced the power levers for landing and noticed that the right engine sounded like the propeller was moving toward the beta position. The pilot increased the engine power, and the sound stopped. As the airplane got closer to the runway, he decreased the engine power, and the sound returned. In addition, the airplane began to yaw right. The pilot applied left aileron and rudder inputs to remain above the runway centerline without success. While over the runway, the pilot reduced the engine power to idle, and the airplane continued to yaw right. The pilot applied full power in an attempt to perform a go-around; however, the airplane yawed about 30 degrees off the runway centerline, touched down in the grass, and impacted trees before coming to rest. The right wing, right engine, and right propeller assembly were impact-separated. The right engine propeller came to rest about 50 ft forward of the main wreckage, and it was found in the feathered position. A review of maintenance records revealed that the right propeller had been overhauled and reinstalled on the airplane 2 days before the accident and had operated 9 hours since that time. Subsequent testing of the right propeller governor revealed that it functioned without anomaly; however, the speed settings were improperly configured. Further, the testing revealed that the beta valve travel from the neutral position was out of tolerance. Although this could have let oil pressure port to one side of the spool or the other and, thus, changed the propeller blade angle, it could not be determined whether this occurred during the accident landing. Impact damage precluded examination of the right propeller governor control linkage; therefore, it could not be determined if it was inadequately installed or rigged, which could have resulted in the propeller moving into the beta position. The investigation could not determine why the right propeller moved toward the beta position as engine power was reduced, as reported the pilot.

Cause: Technical failure

Occupants & Outcome

Crew On Board

2

Passengers On Board

1

Estimated Survivors

3

Fatality Rate

0.0%

Known people on board: 3

Operational Details

Schedule / Flight

Washington - Louisburg

Flight Type

Survey / Patrol / Reconnaissance

Flight Phase

Landing (descent or approach)

Crash Site

Airport (less than 10 km from airport)

Region / Country

North America • United States of America

Aircraft Details

Registration

N181CS

MSN

181

Year of Manufacture

1968

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