Dallas – Austin

Witnesses reported observing the airplane flying slowly toward the airport at a low altitude. The left engine was at a low rpm; "sputtering," "knocking," or making a "banging" noise; and trailing black smoke. One witness said that, as the airplane passed over his location, he saw the tail "kick" horizontally to the right and the airplane bank slightly left. The airplane subsequently collided with trees and impacted a field 1/2 mile north of the airport. Disassembly of the right engine revealed no anomalies, and signatures on the right propeller blades were consistent with power and rotation on impact. The left propeller was found feathered. Disassembly of the left engine revealed that the spark plugs were black and heavily carbonized, consistent with a rich fuel-air mixture; the exhaust tubing also exhibited dark sooting. The rubber boot that connected the intercooler to the fuel injector servo was found dislodged and partially sucked in toward the servo. The clamp used to secure the hose was loose but remained around the servo, the safety wire on the clamp was in place, and the clamp was not impact damaged or bent. The condition of the boot and the clamp were consistent with improper installation. The time since the last overhaul of the left engine was about 1,050 hours. The last 100-hour inspection occurred 3 months before the accident, and the airplane had been flown only 0.8 hour since then. It could not be determined when the rubber boot was improperly installed. Although the left engine had failed, the pilot should have been able to fly the airplane and maintain altitude on the operable right engine, particularly since he had appropriately feathered the left engine.

Flight / Schedule

Dallas – Austin

Registration

N711YM

MSN

61-0215-023

Year of Manufacture

1975

Operator

David Anderson

Date

September 10, 2014 at 01:26 PM

Type

CRASH

Flight Type

Private

Flight Phase

Landing (descent or approach)

Crash Site

Airport (less than 10 km from airport)

Crash Location

Austin-Bergstrom Texas

Region

North America • United States of America

Coordinates

30.1935°, -97.6650°

Crash Cause

Human factor

Narrative Report

On September 10, 2014 at 01:26 PM, Dallas – Austin experienced a crash involving Piper PA-61 Aerostar (Ted Smith 601), operated by David Anderson, with the event recorded near Austin-Bergstrom Texas.

The flight was categorized as private and the reported phase was landing (descent or approach) at a airport (less than 10 km from airport) crash site.

1 people were known to be on board, 1 fatalities were recorded, 0 survivors were identified or estimated. This corresponds to an estimated fatality rate of 100.0%.

Crew on board: 1, crew fatalities: 1, passengers on board: 0, passenger fatalities: 0, other fatalities: 0.

The listed crash cause is human factor. Witnesses reported observing the airplane flying slowly toward the airport at a low altitude. The left engine was at a low rpm; "sputtering," "knocking," or making a "banging" noise; and trailing black smoke. One witness said that, as the airplane passed over his location, he saw the tail "kick" horizontally to the right and the airplane bank slightly left. The airplane subsequently collided with trees and impacted a field 1/2 mile north of the airport. Disassembly of the right engine revealed no anomalies, and signatures on the right propeller blades were consistent with power and rotation on impact. The left propeller was found feathered. Disassembly of the left engine revealed that the spark plugs were black and heavily carbonized, consistent with a rich fuel-air mixture; the exhaust tubing also exhibited dark sooting. The rubber boot that connected the intercooler to the fuel injector servo was found dislodged and partially sucked in toward the servo. The clamp used to secure the hose was loose but remained around the servo, the safety wire on the clamp was in place, and the clamp was not impact damaged or bent. The condition of the boot and the clamp were consistent with improper installation. The time since the last overhaul of the left engine was about 1,050 hours. The last 100-hour inspection occurred 3 months before the accident, and the airplane had been flown only 0.8 hour since then. It could not be determined when the rubber boot was improperly installed. Although the left engine had failed, the pilot should have been able to fly the airplane and maintain altitude on the operable right engine, particularly since he had appropriately feathered the left engine.

Aircraft reference details include registration N711YM, MSN 61-0215-023, year of manufacture 1975.

Geospatial coordinates for this crash are approximately 30.1935°, -97.6650°.

Fatalities

Total

1

Crew

1

Passengers

0

Other

0

Crash Summary

Witnesses reported observing the airplane flying slowly toward the airport at a low altitude. The left engine was at a low rpm; "sputtering," "knocking," or making a "banging" noise; and trailing black smoke. One witness said that, as the airplane passed over his location, he saw the tail "kick" horizontally to the right and the airplane bank slightly left. The airplane subsequently collided with trees and impacted a field 1/2 mile north of the airport. Disassembly of the right engine revealed no anomalies, and signatures on the right propeller blades were consistent with power and rotation on impact. The left propeller was found feathered. Disassembly of the left engine revealed that the spark plugs were black and heavily carbonized, consistent with a rich fuel-air mixture; the exhaust tubing also exhibited dark sooting. The rubber boot that connected the intercooler to the fuel injector servo was found dislodged and partially sucked in toward the servo. The clamp used to secure the hose was loose but remained around the servo, the safety wire on the clamp was in place, and the clamp was not impact damaged or bent. The condition of the boot and the clamp were consistent with improper installation. The time since the last overhaul of the left engine was about 1,050 hours. The last 100-hour inspection occurred 3 months before the accident, and the airplane had been flown only 0.8 hour since then. It could not be determined when the rubber boot was improperly installed. Although the left engine had failed, the pilot should have been able to fly the airplane and maintain altitude on the operable right engine, particularly since he had appropriately feathered the left engine.

Cause: Human factor

Occupants & Outcome

Crew On Board

1

Passengers On Board

0

Estimated Survivors

0

Fatality Rate

100.0%

Known people on board: 1

Operational Details

Schedule / Flight

Dallas – Austin

Operator

David Anderson

Flight Type

Private

Flight Phase

Landing (descent or approach)

Crash Site

Airport (less than 10 km from airport)

Region / Country

North America • United States of America

Aircraft Details

Registration

N711YM

MSN

61-0215-023

Year of Manufacture

1975