Page - Page
Flight / Schedule
Page - Page
Aircraft
Cessna 207 Skywagon/StationairRegistration
N7311U
MSN
207A-0395
Year of Manufacture
1977
Operator
American AviationDate
May 10, 2014 at 03:45 PM
Type
CRASHFlight Type
Charter/Taxi (Non Scheduled Revenue Flight)
Flight Phase
Landing (descent or approach)
Crash Site
Airport (less than 10 km from airport)
Crash Location
Page Arizona
Region
North America • United States of America
Coordinates
36.9148°, -111.4573°
Crash Cause
Human factor
Narrative Report
On May 10, 2014 at 03:45 PM, Page - Page experienced a crash involving Cessna 207 Skywagon/Stationair, operated by American Aviation, with the event recorded near Page Arizona.
The flight was categorized as charter/taxi (non scheduled revenue flight) and the reported phase was landing (descent or approach) at a airport (less than 10 km from airport) crash site.
7 people were known to be on board, 1 fatalities were recorded, 6 survivors were identified or estimated. This corresponds to an estimated fatality rate of 14.3%.
Crew on board: 1, crew fatalities: 0, passengers on board: 6, passenger fatalities: 1, other fatalities: 0.
The listed crash cause is human factor. During a local sightseeing flight, the pilot noticed that the engine had lost partial power, and he initiated a turn back toward the airport while troubleshooting the loss of power. Despite the pilot's attempts, the engine would not regain full power and was surging and sputtering randomly. The pilot entered the airport's traffic pattern on the downwind leg, and, while on final approach to the runway, the airplane encountered multiple downdrafts and wind gusts. It is likely that, due to the downdrafts and the partial loss of engine power, the pilot was not able to maintain airplane control. The airplane subsequently landed hard short of the runway surface and nosed over, coming to rest inverted. The reported wind conditions around the time of the accident varied between 20 and 70 degrees right of the runway heading and were 14 knots gusting to greater than 20 knots. In addition, a company pilot who landed about 8 minutes before the accident reported that he encountered strong downdrafts and windshear while on final approach to the runway and that he would not have been able to reach the runway if he had a partial or total loss of engine power. Postaccident examination of the airframe and engine revealed no evidence of any preexisting mechanical malfunctions or failures that would have precluded normal operation. The engine was subsequently installed on a test stand and was successfully run through various power settings for several minutes. The reason for the partial loss of engine power could not be determined.
Aircraft reference details include registration N7311U, MSN 207A-0395, year of manufacture 1977.
Geospatial coordinates for this crash are approximately 36.9148°, -111.4573°.
Fatalities
Total
1
Crew
0
Passengers
1
Other
0
Crash Summary
During a local sightseeing flight, the pilot noticed that the engine had lost partial power, and he initiated a turn back toward the airport while troubleshooting the loss of power. Despite the pilot's attempts, the engine would not regain full power and was surging and sputtering randomly. The pilot entered the airport's traffic pattern on the downwind leg, and, while on final approach to the runway, the airplane encountered multiple downdrafts and wind gusts. It is likely that, due to the downdrafts and the partial loss of engine power, the pilot was not able to maintain airplane control. The airplane subsequently landed hard short of the runway surface and nosed over, coming to rest inverted. The reported wind conditions around the time of the accident varied between 20 and 70 degrees right of the runway heading and were 14 knots gusting to greater than 20 knots. In addition, a company pilot who landed about 8 minutes before the accident reported that he encountered strong downdrafts and windshear while on final approach to the runway and that he would not have been able to reach the runway if he had a partial or total loss of engine power. Postaccident examination of the airframe and engine revealed no evidence of any preexisting mechanical malfunctions or failures that would have precluded normal operation. The engine was subsequently installed on a test stand and was successfully run through various power settings for several minutes. The reason for the partial loss of engine power could not be determined.
Cause: Human factor
Occupants & Outcome
Crew On Board
1
Passengers On Board
6
Estimated Survivors
6
Fatality Rate
14.3%
Known people on board: 7
Operational Details
Schedule / Flight
Page - Page
Operator
American AviationFlight Type
Charter/Taxi (Non Scheduled Revenue Flight)
Flight Phase
Landing (descent or approach)
Crash Site
Airport (less than 10 km from airport)
Region / Country
North America • United States of America
