Charlevoix - Tiffin
Flight / Schedule
Charlevoix - Tiffin
Aircraft
Piper PA-31 CheyenneRegistration
N85EM
MSN
31-8166055
Year of Manufacture
1981
Operator
Cheyenne Sales %26 LeasingDate
December 4, 2009 at 06:45 PM
Type
CRASHFlight Type
Ferry
Flight Phase
Flight
Crash Site
Plain, Valley
Crash Location
Harrison Michigan
Region
North America • United States of America
Coordinates
44.0192°, -84.7998°
Crash Cause
Technical failure
Narrative Report
On December 4, 2009 at 06:45 PM, Charlevoix - Tiffin experienced a crash involving Piper PA-31 Cheyenne, operated by Cheyenne Sales %26 Leasing, with the event recorded near Harrison Michigan.
The flight was categorized as ferry and the reported phase was flight at a plain, valley crash site.
1 people were known to be on board, 1 fatalities were recorded, 0 survivors were identified or estimated. This corresponds to an estimated fatality rate of 100.0%.
Crew on board: 1, crew fatalities: 1, passengers on board: 0, passenger fatalities: 0, other fatalities: 0.
The listed crash cause is technical failure. Shortly after takeoff in the pressurized twin-engine airplane, the pilot was cleared to climb and maintain 16,000 feet. The pilot reported passing through instrument conditions with heavy snow and that he cleared the tops of the clouds at 7,000 feet. The pilot was then cleared to climb and maintain flight level (FL) 230. Radar data showed the airplane's altitude and course varied throughout the flight after having reached FL 230. Several times during the flight the air traffic controller questioned the pilot regarding his altitude and/or course. Each time the pilot responded that he was at the correct altitude and/or course. The radar data showed that after each of these conversations, the airplane would return to the assigned altitude and/or course. The controller then informed the pilot that, because radar showed the airplane’s altitude fluctuating between FL 224 and FL 237, he was going to have to descend out of positive controller airspace. The pilot acknowledged this transmission. The controller instructed the pilot to descend to 17,000 feet. The last transmission from the pilot was when he acknowledged the descent. Radar data showed that one minute later the airplane was at FL 234. During the last minute and 12 seconds of radar data, the airplane reversed its course and descended from FL 233 to FL 214, at which time radar data was lost. Witnesses reported hearing loud engine sounds and seeing the airplane in a spiraling descent until ground impact. Post accident inspection of the engines did not identify any anomalies that would have precluded normal operation. Most of the fuselage was consumed by fire; however, flight control continuity was established. Given the pilot’s experience and the flight’s altitude and course variations the investigation considered that the pilot may have suffered from hypoxia; however, due to the post impact fire the functionality of the airplane’s pressurization system could not be observed and no conclusive determination could be made that the pilot as impaired.
Aircraft reference details include registration N85EM, MSN 31-8166055, year of manufacture 1981.
Geospatial coordinates for this crash are approximately 44.0192°, -84.7998°.
Fatalities
Total
1
Crew
1
Passengers
0
Other
0
Crash Summary
Shortly after takeoff in the pressurized twin-engine airplane, the pilot was cleared to climb and maintain 16,000 feet. The pilot reported passing through instrument conditions with heavy snow and that he cleared the tops of the clouds at 7,000 feet. The pilot was then cleared to climb and maintain flight level (FL) 230. Radar data showed the airplane's altitude and course varied throughout the flight after having reached FL 230. Several times during the flight the air traffic controller questioned the pilot regarding his altitude and/or course. Each time the pilot responded that he was at the correct altitude and/or course. The radar data showed that after each of these conversations, the airplane would return to the assigned altitude and/or course. The controller then informed the pilot that, because radar showed the airplane’s altitude fluctuating between FL 224 and FL 237, he was going to have to descend out of positive controller airspace. The pilot acknowledged this transmission. The controller instructed the pilot to descend to 17,000 feet. The last transmission from the pilot was when he acknowledged the descent. Radar data showed that one minute later the airplane was at FL 234. During the last minute and 12 seconds of radar data, the airplane reversed its course and descended from FL 233 to FL 214, at which time radar data was lost. Witnesses reported hearing loud engine sounds and seeing the airplane in a spiraling descent until ground impact. Post accident inspection of the engines did not identify any anomalies that would have precluded normal operation. Most of the fuselage was consumed by fire; however, flight control continuity was established. Given the pilot’s experience and the flight’s altitude and course variations the investigation considered that the pilot may have suffered from hypoxia; however, due to the post impact fire the functionality of the airplane’s pressurization system could not be observed and no conclusive determination could be made that the pilot as impaired.
Cause: Technical failure
Occupants & Outcome
Crew On Board
1
Passengers On Board
0
Estimated Survivors
0
Fatality Rate
100.0%
Known people on board: 1
Operational Details
Schedule / Flight
Charlevoix - Tiffin
Operator
Cheyenne Sales %26 LeasingFlight Type
Ferry
Flight Phase
Flight
Crash Site
Plain, Valley
Region / Country
North America • United States of America
