Asheville – Greensboro

At about the 3,000-foot marker on the 8,000-foot long runway witnesses saw the airplane at about 100 to 150-feet above the ground with the landing gear retracted when they heard a loud "bang". They said the airplane made no attempt to land on the remaining 5,000 feet of runway after the noise. The airplane continued climbing and seemed to gain a little altitude before passing the end of the runway. At that point the airplane began a right descending turn and was in a 60 to 80 degree right bank, nose low attitude when they lost sight of it. The airplane collided with the ground about 8/10 of a mile from the departure end of runway 34 in a residential area. Examination of the critical left engine found no pre-impact mechanical malfunction. Examination of the right engine found galling on all of the connecting rods. Dirt and particular contaminants were found embedded on all of the bearings, and spalling was observed on all of the cam followers. The oil suction screen was found clean, The oil filter was found contaminated with ferrous and non-ferrous small particles. The number 3 cylinder connecting rod yoke was broken on one side of the rod cap and separated into two pieces. Heavy secondary damage was noted with no signs of heat distress. Examination of the engine logbooks revealed that both engine's had been overhauled in 1986. In 1992, the airplane was registered in the Dominican Republic and the last maintenance entry indicated that the left and right engines underwent an inspection 754.3 hours since major overhaul. There were no other maintenance entries in the logbooks until the airplane was sold and moved to the United States in 2002. All three blades of the right propeller were found in the low pitch position, confirming that the pilot did not feather the right propeller as outlined in the pilot's operating handbook, under emergency procedures following a loss of engine power during takeoff.

Flight / Schedule

Asheville – Greensboro

Registration

N611JC

MSN

P-496

Year of Manufacture

1979

Operator

Jorge Campillo

Date

October 27, 2004 at 10:50 AM

Type

CRASH

Flight Type

Executive/Corporate/Business

Flight Phase

Takeoff (climb)

Crash Site

City

Crash Location

Asheville North Carolina

Region

North America • United States of America

Coordinates

35.5954°, -82.5508°

Crash Cause

Technical failure

Narrative Report

On October 27, 2004 at 10:50 AM, Asheville – Greensboro experienced a crash involving Beechcraft 60 Duke, operated by Jorge Campillo, with the event recorded near Asheville North Carolina.

The flight was categorized as executive/corporate/business and the reported phase was takeoff (climb) at a city crash site.

4 people were known to be on board, 4 fatalities were recorded, 0 survivors were identified or estimated. This corresponds to an estimated fatality rate of 100.0%.

Crew on board: 1, crew fatalities: 1, passengers on board: 3, passenger fatalities: 3, other fatalities: 0.

The listed crash cause is technical failure. At about the 3,000-foot marker on the 8,000-foot long runway witnesses saw the airplane at about 100 to 150-feet above the ground with the landing gear retracted when they heard a loud "bang". They said the airplane made no attempt to land on the remaining 5,000 feet of runway after the noise. The airplane continued climbing and seemed to gain a little altitude before passing the end of the runway. At that point the airplane began a right descending turn and was in a 60 to 80 degree right bank, nose low attitude when they lost sight of it. The airplane collided with the ground about 8/10 of a mile from the departure end of runway 34 in a residential area. Examination of the critical left engine found no pre-impact mechanical malfunction. Examination of the right engine found galling on all of the connecting rods. Dirt and particular contaminants were found embedded on all of the bearings, and spalling was observed on all of the cam followers. The oil suction screen was found clean, The oil filter was found contaminated with ferrous and non-ferrous small particles. The number 3 cylinder connecting rod yoke was broken on one side of the rod cap and separated into two pieces. Heavy secondary damage was noted with no signs of heat distress. Examination of the engine logbooks revealed that both engine's had been overhauled in 1986. In 1992, the airplane was registered in the Dominican Republic and the last maintenance entry indicated that the left and right engines underwent an inspection 754.3 hours since major overhaul. There were no other maintenance entries in the logbooks until the airplane was sold and moved to the United States in 2002. All three blades of the right propeller were found in the low pitch position, confirming that the pilot did not feather the right propeller as outlined in the pilot's operating handbook, under emergency procedures following a loss of engine power during takeoff.

Aircraft reference details include registration N611JC, MSN P-496, year of manufacture 1979.

Geospatial coordinates for this crash are approximately 35.5954°, -82.5508°.

Fatalities

Total

4

Crew

1

Passengers

3

Other

0

Crash Summary

At about the 3,000-foot marker on the 8,000-foot long runway witnesses saw the airplane at about 100 to 150-feet above the ground with the landing gear retracted when they heard a loud "bang". They said the airplane made no attempt to land on the remaining 5,000 feet of runway after the noise. The airplane continued climbing and seemed to gain a little altitude before passing the end of the runway. At that point the airplane began a right descending turn and was in a 60 to 80 degree right bank, nose low attitude when they lost sight of it. The airplane collided with the ground about 8/10 of a mile from the departure end of runway 34 in a residential area. Examination of the critical left engine found no pre-impact mechanical malfunction. Examination of the right engine found galling on all of the connecting rods. Dirt and particular contaminants were found embedded on all of the bearings, and spalling was observed on all of the cam followers. The oil suction screen was found clean, The oil filter was found contaminated with ferrous and non-ferrous small particles. The number 3 cylinder connecting rod yoke was broken on one side of the rod cap and separated into two pieces. Heavy secondary damage was noted with no signs of heat distress. Examination of the engine logbooks revealed that both engine's had been overhauled in 1986. In 1992, the airplane was registered in the Dominican Republic and the last maintenance entry indicated that the left and right engines underwent an inspection 754.3 hours since major overhaul. There were no other maintenance entries in the logbooks until the airplane was sold and moved to the United States in 2002. All three blades of the right propeller were found in the low pitch position, confirming that the pilot did not feather the right propeller as outlined in the pilot's operating handbook, under emergency procedures following a loss of engine power during takeoff.

Cause: Technical failure

Occupants & Outcome

Crew On Board

1

Passengers On Board

3

Estimated Survivors

0

Fatality Rate

100.0%

Known people on board: 4

Operational Details

Schedule / Flight

Asheville – Greensboro

Operator

Jorge Campillo

Flight Type

Executive/Corporate/Business

Flight Phase

Takeoff (climb)

Crash Site

City

Region / Country

North America • United States of America

Aircraft Details

Registration

N611JC

MSN

P-496

Year of Manufacture

1979