Newton - Salina
Flight / Schedule
Newton - Salina
Aircraft
Learjet 25Registration
N333CG
MSN
25-262
Year of Manufacture
1978
Operator
Avcon IndustriesDate
June 12, 2001 at 01:00 PM
Type
CRASHFlight Type
Test
Flight Phase
Landing (descent or approach)
Crash Site
Airport (less than 10 km from airport)
Crash Location
Salina Kansas
Region
North America • United States of America
Coordinates
38.8403°, -97.6114°
Crash Cause
Human factor
Narrative Report
On June 12, 2001 at 01:00 PM, Newton - Salina experienced a crash involving Learjet 25, operated by Avcon Industries, with the event recorded near Salina Kansas.
The flight was categorized as test and the reported phase was landing (descent or approach) at a airport (less than 10 km from airport) crash site.
2 people were known to be on board, 0 fatalities were recorded, 2 survivors were identified or estimated. This corresponds to an estimated fatality rate of 0.0%.
Crew on board: 2, crew fatalities: 0, passengers on board: 0, passenger fatalities: 0, other fatalities: 0.
The listed crash cause is human factor. During a test flight, the airplane encountered an elevator system oscillation while in a high speed dive outside the normal operating envelope. The 17 second oscillation was recorded on the cockpit voice recorder and had an average frequency of 28 Hz. The aft elevator sector clevis (p/n 2331510-32) fractured due to reverse bending fatigue caused by vibration, resulting in a complete loss of elevator control. The flight crew reported that pitch control was established by using horizontal stabilizer pitch trim. The flightcrew stated that during final approach to runway 17 (13,337 feet by 200 feet, dry/asphalt) the aircraft's nose began to drop and that the flying pilot was unable to raise the nose using a combination of horizontal stabilizer trim and engine power. The aircraft landed short of the runway, striking an airport perimeter fence and a berm. The surface winds were from the south at 23 knots, gusting to 32 knots.
Aircraft reference details include registration N333CG, MSN 25-262, year of manufacture 1978.
Geospatial coordinates for this crash are approximately 38.8403°, -97.6114°.
Fatalities
Total
0
Crew
0
Passengers
0
Other
0
Crash Summary
During a test flight, the airplane encountered an elevator system oscillation while in a high speed dive outside the normal operating envelope. The 17 second oscillation was recorded on the cockpit voice recorder and had an average frequency of 28 Hz. The aft elevator sector clevis (p/n 2331510-32) fractured due to reverse bending fatigue caused by vibration, resulting in a complete loss of elevator control. The flight crew reported that pitch control was established by using horizontal stabilizer pitch trim. The flightcrew stated that during final approach to runway 17 (13,337 feet by 200 feet, dry/asphalt) the aircraft's nose began to drop and that the flying pilot was unable to raise the nose using a combination of horizontal stabilizer trim and engine power. The aircraft landed short of the runway, striking an airport perimeter fence and a berm. The surface winds were from the south at 23 knots, gusting to 32 knots.
Cause: Human factor
Occupants & Outcome
Crew On Board
2
Passengers On Board
0
Estimated Survivors
2
Fatality Rate
0.0%
Known people on board: 2
Operational Details
Schedule / Flight
Newton - Salina
Operator
Avcon IndustriesFlight Type
Test
Flight Phase
Landing (descent or approach)
Crash Site
Airport (less than 10 km from airport)
Region / Country
North America • United States of America
