Portland – Youngstown
Flight / Schedule
Portland – Youngstown
Aircraft
Cessna 303 CrusaderRegistration
N511AR
MSN
303-00192
Year of Manufacture
1982
Operator
Twin Cities Air ServiceDate
November 1, 1999 at 06:16 AM
Type
CRASHFlight Type
Charter/Taxi (Non Scheduled Revenue Flight)
Flight Phase
Landing (descent or approach)
Crash Site
Airport (less than 10 km from airport)
Crash Location
Binghamton New York
Region
North America • United States of America
Coordinates
42.0987°, -75.9125°
Crash Cause
Human factor
Narrative Report
On November 1, 1999 at 06:16 AM, Portland – Youngstown experienced a crash involving Cessna 303 Crusader, operated by Twin Cities Air Service, with the event recorded near Binghamton New York.
The flight was categorized as charter/taxi (non scheduled revenue flight) and the reported phase was landing (descent or approach) at a airport (less than 10 km from airport) crash site.
3 people were known to be on board, 0 fatalities were recorded, 3 survivors were identified or estimated. This corresponds to an estimated fatality rate of 0.0%.
Crew on board: 1, crew fatalities: 0, passengers on board: 2, passenger fatalities: 0, other fatalities: 0.
The listed crash cause is human factor. While in cruise flight, at 6,000 feet, the left engine lost power. The pilot attempted a restart of the engine, but only about one-half rotation of the left engine propeller was observed, and the engine was secured. The pilot stated that he was unable to maintain altitude and initiated a decent. He requested and was cleared for an instrument approach at an airport where the weather conditions were, 1/4 statute mile of visibility, fog, and a vertical visibility of 100 feet. On the approach, at the minimum descent altitude, the pilot executed a missed approach. As the airplane climbed, the pilot reported to the controller that the 'best altitude [he] could get was 2,200 feet.' A second approach was initiated to the reciprocal runway. While on the second approach, the pilot 'was going to fly the aircraft right to the runway, and told the controller so.' He put the gear down, reduced power, and decided there was 'no hope for a go-around.' He then 'flew down past the decision height,' and about 70-80 feet above the ground, 'added a little power to smooth the landing.' The pilot also stated, 'The last thing I remember was the aircraft nose contacting the runway.' A passenger stated that once the pilot could not see the runway, [the pilot] 'applied power, pitched the nose up,' and attempted a 'go-around' similar to the one that was executed on the first approach. Disassembly of the left engine revealed that the crankshaft was fatigue fractured between connecting rod journal number 2 and main journal number 2. Review of the pilot's operating handbook revealed that the single engine service ceiling, at a weight of 4,800 pounds, was 11,700 feet. The average single engine rate of climb, at a pressure altitude of 6,000 feet, was 295 feet per minute. The average single engine rate of climb, at a pressure altitude of 1,625 feet, was 314 feet per minute. Review of the ILS approach plate for Runway 34 revealed that the decision height was 200 feet above the ground.
Aircraft reference details include registration N511AR, MSN 303-00192, year of manufacture 1982.
Geospatial coordinates for this crash are approximately 42.0987°, -75.9125°.
Fatalities
Total
0
Crew
0
Passengers
0
Other
0
Crash Summary
While in cruise flight, at 6,000 feet, the left engine lost power. The pilot attempted a restart of the engine, but only about one-half rotation of the left engine propeller was observed, and the engine was secured. The pilot stated that he was unable to maintain altitude and initiated a decent. He requested and was cleared for an instrument approach at an airport where the weather conditions were, 1/4 statute mile of visibility, fog, and a vertical visibility of 100 feet. On the approach, at the minimum descent altitude, the pilot executed a missed approach. As the airplane climbed, the pilot reported to the controller that the 'best altitude [he] could get was 2,200 feet.' A second approach was initiated to the reciprocal runway. While on the second approach, the pilot 'was going to fly the aircraft right to the runway, and told the controller so.' He put the gear down, reduced power, and decided there was 'no hope for a go-around.' He then 'flew down past the decision height,' and about 70-80 feet above the ground, 'added a little power to smooth the landing.' The pilot also stated, 'The last thing I remember was the aircraft nose contacting the runway.' A passenger stated that once the pilot could not see the runway, [the pilot] 'applied power, pitched the nose up,' and attempted a 'go-around' similar to the one that was executed on the first approach. Disassembly of the left engine revealed that the crankshaft was fatigue fractured between connecting rod journal number 2 and main journal number 2. Review of the pilot's operating handbook revealed that the single engine service ceiling, at a weight of 4,800 pounds, was 11,700 feet. The average single engine rate of climb, at a pressure altitude of 6,000 feet, was 295 feet per minute. The average single engine rate of climb, at a pressure altitude of 1,625 feet, was 314 feet per minute. Review of the ILS approach plate for Runway 34 revealed that the decision height was 200 feet above the ground.
Cause: Human factor
Occupants & Outcome
Crew On Board
1
Passengers On Board
2
Estimated Survivors
3
Fatality Rate
0.0%
Known people on board: 3
Operational Details
Schedule / Flight
Portland – Youngstown
Operator
Twin Cities Air ServiceFlight Type
Charter/Taxi (Non Scheduled Revenue Flight)
Flight Phase
Landing (descent or approach)
Crash Site
Airport (less than 10 km from airport)
Region / Country
North America • United States of America
