Coldwater - Elkhart

The pilot obtained a preflight briefing and indicated that he would obtain an IFR clearance after becoming airborne; however, he took off and did not activate a flight plan. Witnesses observed the airplane flying north (away from the destination) about 200 to 300 feet above the ground below a low overcast sky condition. One witness said the airplane was flying very slow; he said he was almost able to keep up with it in his vehicle. The witnesses said they saw the airplane roll rapidly to the right and descend toward the ground. It collided with the ground in an approximate 50 degree pitch down attitude. An on-scene examination did not reveal any airframe or control anomaly that would have resulted in the accident. The engines and propellers were disassembled for inspection. Examination of the engines revealed they were capable of producing power. Examination of the propellers revealed both were operating at low pitch settings. About 25 miles north-northwest at Battle Creek, MI, the 1145 edt weather was, in part: 500 feet overcast, visibility 2 miles with fog, wind from 050 degrees at 10 knots.

Flight / Schedule

Coldwater - Elkhart

Registration

N14A

MSN

421B-0373

Year of Manufacture

1973

Operator

Hanseatic Air

Date

September 21, 1995 at 11:45 AM

Type

CRASH

Flight Type

Executive/Corporate/Business

Flight Phase

Takeoff (climb)

Crash Site

Airport (less than 10 km from airport)

Crash Location

Coldwater-Branch County Michigan

Region

North America • United States of America

Coordinates

41.9411°, -85.0031°

Crash Cause

Human factor

Narrative Report

On September 21, 1995 at 11:45 AM, Coldwater - Elkhart experienced a crash involving Cessna 421B Golden Eagle II, operated by Hanseatic Air, with the event recorded near Coldwater-Branch County Michigan.

The flight was categorized as executive/corporate/business and the reported phase was takeoff (climb) at a airport (less than 10 km from airport) crash site.

1 people were known to be on board, 1 fatalities were recorded, 0 survivors were identified or estimated. This corresponds to an estimated fatality rate of 100.0%.

Crew on board: 1, crew fatalities: 1, passengers on board: 0, passenger fatalities: 0, other fatalities: 0.

The listed crash cause is human factor. The pilot obtained a preflight briefing and indicated that he would obtain an IFR clearance after becoming airborne; however, he took off and did not activate a flight plan. Witnesses observed the airplane flying north (away from the destination) about 200 to 300 feet above the ground below a low overcast sky condition. One witness said the airplane was flying very slow; he said he was almost able to keep up with it in his vehicle. The witnesses said they saw the airplane roll rapidly to the right and descend toward the ground. It collided with the ground in an approximate 50 degree pitch down attitude. An on-scene examination did not reveal any airframe or control anomaly that would have resulted in the accident. The engines and propellers were disassembled for inspection. Examination of the engines revealed they were capable of producing power. Examination of the propellers revealed both were operating at low pitch settings. About 25 miles north-northwest at Battle Creek, MI, the 1145 edt weather was, in part: 500 feet overcast, visibility 2 miles with fog, wind from 050 degrees at 10 knots.

Aircraft reference details include registration N14A, MSN 421B-0373, year of manufacture 1973.

Geospatial coordinates for this crash are approximately 41.9411°, -85.0031°.

Fatalities

Total

1

Crew

1

Passengers

0

Other

0

Crash Summary

The pilot obtained a preflight briefing and indicated that he would obtain an IFR clearance after becoming airborne; however, he took off and did not activate a flight plan. Witnesses observed the airplane flying north (away from the destination) about 200 to 300 feet above the ground below a low overcast sky condition. One witness said the airplane was flying very slow; he said he was almost able to keep up with it in his vehicle. The witnesses said they saw the airplane roll rapidly to the right and descend toward the ground. It collided with the ground in an approximate 50 degree pitch down attitude. An on-scene examination did not reveal any airframe or control anomaly that would have resulted in the accident. The engines and propellers were disassembled for inspection. Examination of the engines revealed they were capable of producing power. Examination of the propellers revealed both were operating at low pitch settings. About 25 miles north-northwest at Battle Creek, MI, the 1145 edt weather was, in part: 500 feet overcast, visibility 2 miles with fog, wind from 050 degrees at 10 knots.

Cause: Human factor

Occupants & Outcome

Crew On Board

1

Passengers On Board

0

Estimated Survivors

0

Fatality Rate

100.0%

Known people on board: 1

Operational Details

Schedule / Flight

Coldwater - Elkhart

Operator

Hanseatic Air

Flight Type

Executive/Corporate/Business

Flight Phase

Takeoff (climb)

Crash Site

Airport (less than 10 km from airport)

Region / Country

North America • United States of America

Aircraft Details

Registration

N14A

MSN

421B-0373

Year of Manufacture

1973