Wheeling - Waukegan
Flight / Schedule
Wheeling - Waukegan
Aircraft
BAe 125Registration
N900CD
MSN
25111
Year of Manufacture
1966
Operator
DB AviationDate
May 30, 1994 at 06:42 PM
Type
CRASHFlight Type
Positioning
Flight Phase
Landing (descent or approach)
Crash Site
Airport (less than 10 km from airport)
Crash Location
Waukegan Illinois
Region
North America • United States of America
Coordinates
42.3602°, -87.8318°
Crash Cause
Human factor
Narrative Report
On May 30, 1994 at 06:42 PM, Wheeling - Waukegan experienced a crash involving BAe 125, operated by DB Aviation, with the event recorded near Waukegan Illinois.
The flight was categorized as positioning and the reported phase was landing (descent or approach) at a airport (less than 10 km from airport) crash site.
2 people were known to be on board, 0 fatalities were recorded, 2 survivors were identified or estimated. This corresponds to an estimated fatality rate of 0.0%.
Crew on board: 2, crew fatalities: 0, passengers on board: 0, passenger fatalities: 0, other fatalities: 0.
The listed crash cause is human factor. The corporate jet's sink rate increased during short final approach. The copilot applied elevator back pressure and nose up trim. The sink rate continued to increase. The captain observed the copilot's efforts and began applying back pressure on his control yoke. Through combined efforts of both pilots they were able to increase the pitch enough that the airplane touched down on the main gear first. However, the touchdown was hard. The on-scene investigation revealed that a trip manifest container was lodged between the copilot's control yoke column and seat frame. The pilots stated the container is required to be carried in the cockpit during lights. Both pilots said there is no designated space in the cockpit to retain the container.
Aircraft reference details include registration N900CD, MSN 25111, year of manufacture 1966.
Geospatial coordinates for this crash are approximately 42.3602°, -87.8318°.
Fatalities
Total
0
Crew
0
Passengers
0
Other
0
Crash Summary
The corporate jet's sink rate increased during short final approach. The copilot applied elevator back pressure and nose up trim. The sink rate continued to increase. The captain observed the copilot's efforts and began applying back pressure on his control yoke. Through combined efforts of both pilots they were able to increase the pitch enough that the airplane touched down on the main gear first. However, the touchdown was hard. The on-scene investigation revealed that a trip manifest container was lodged between the copilot's control yoke column and seat frame. The pilots stated the container is required to be carried in the cockpit during lights. Both pilots said there is no designated space in the cockpit to retain the container.
Cause: Human factor
Occupants & Outcome
Crew On Board
2
Passengers On Board
0
Estimated Survivors
2
Fatality Rate
0.0%
Known people on board: 2
Operational Details
Schedule / Flight
Wheeling - Waukegan
Operator
DB AviationFlight Type
Positioning
Flight Phase
Landing (descent or approach)
Crash Site
Airport (less than 10 km from airport)
Region / Country
North America • United States of America
