Istanbul – Southampton
Flight / Schedule
Istanbul – Southampton
Aircraft
Lockheed L-1329 JetStarRegistration
N6NE
MSN
5006
Year of Manufacture
1961
Operator
Aerospace Finance LeasingDate
November 27, 1992 at 04:16 PM
Type
CRASHFlight Type
Executive/Corporate/Business
Flight Phase
Landing (descent or approach)
Crash Site
Airport (less than 10 km from airport)
Crash Location
Southampton Hampshire
Region
Europe • United Kingdom
Coordinates
50.8995°, -1.3275°
Crash Cause
Weather
Narrative Report
On November 27, 1992 at 04:16 PM, Istanbul – Southampton experienced a crash involving Lockheed L-1329 JetStar, operated by Aerospace Finance Leasing, with the event recorded near Southampton Hampshire.
The flight was categorized as executive/corporate/business and the reported phase was landing (descent or approach) at a airport (less than 10 km from airport) crash site.
7 people were known to be on board, 0 fatalities were recorded, 7 survivors were identified or estimated. This corresponds to an estimated fatality rate of 0.0%.
Crew on board: 2, crew fatalities: 0, passengers on board: 5, passenger fatalities: 0, other fatalities: 0.
The listed crash cause is weather. Completing a flight from Istanbul to Southampton, the aircraft flew a procedural ILS and landed on runway 20. The crew report that they encountered wind shear on the final approach and they increased power to compensate for a loss of 10 knot of airspeed. The aircraft landed some 500 feet into the runway and, after touchdown, maximum braking appeared to be ineffective. The crew suspected aquaplaning and activated reversed thrust but they report that correct deployment was not indicated on the flight deck and so they assumed that it was not operating. Despite weaving along the remaining 1,500 feet of runway they were unable to prevent the aircraft from over running the end. The aircraft came to rest some 75 metres into the grass area beyond. Debris, consisting of earth and stones was ingested by the engines and the right wing tank was punctured. An inspection of the runway 10 minutes previously showed that, although the runway was wet, there was no standing water. A runway friction test was carried out at 1646 hrs and this gave the friction on the first, second and third runway segments as 0.67 Mu, 0.66 Mu and 0.57 Mu respectively.
Aircraft reference details include registration N6NE, MSN 5006, year of manufacture 1961.
Geospatial coordinates for this crash are approximately 50.8995°, -1.3275°.
Fatalities
Total
0
Crew
0
Passengers
0
Other
0
Crash Summary
Completing a flight from Istanbul to Southampton, the aircraft flew a procedural ILS and landed on runway 20. The crew report that they encountered wind shear on the final approach and they increased power to compensate for a loss of 10 knot of airspeed. The aircraft landed some 500 feet into the runway and, after touchdown, maximum braking appeared to be ineffective. The crew suspected aquaplaning and activated reversed thrust but they report that correct deployment was not indicated on the flight deck and so they assumed that it was not operating. Despite weaving along the remaining 1,500 feet of runway they were unable to prevent the aircraft from over running the end. The aircraft came to rest some 75 metres into the grass area beyond. Debris, consisting of earth and stones was ingested by the engines and the right wing tank was punctured. An inspection of the runway 10 minutes previously showed that, although the runway was wet, there was no standing water. A runway friction test was carried out at 1646 hrs and this gave the friction on the first, second and third runway segments as 0.67 Mu, 0.66 Mu and 0.57 Mu respectively.
Cause: Weather
Occupants & Outcome
Crew On Board
2
Passengers On Board
5
Estimated Survivors
7
Fatality Rate
0.0%
Known people on board: 7
Operational Details
Schedule / Flight
Istanbul – Southampton
Operator
Aerospace Finance LeasingFlight Type
Executive/Corporate/Business
Flight Phase
Landing (descent or approach)
Crash Site
Airport (less than 10 km from airport)
Region / Country
Europe • United Kingdom
Aircraft Details
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