Philadelphia - Charlotte

During gear retraction after takeoff, the right main gear became jammed in a partially retracted position and the respective in-transit gear light would not extinguish. Attempts to recycle the gear were unsuccessful. The flight crew diverted to Atlanta, GA; then decided to land at Dobbins AFB, where there was a long, wide runway that could be foamed. Foam was applied to approximately 300 feet of runway 29. The aircraft was landed with the nose and left main gear extended and the right main gear partially retracted. Subsequently, the aircraft veered to the right and stopped with the nose gear approximately 70 feet off the runway. Fire erupted in the area of the right main gear; however, the fire was quickly extinguished by fire dept personnel. An investigation revealed the clearance between the main landing gear door hook, pn 803845-1, and the strut roller was excessive. The reason for the improper clearance was not determined. Lockheed service bulletin 88/sb-558 warned that excessive clearance combined with a drop in hydraulic pressure, gust or maneuver could result in the gear jamming. All three crew members were uninjured.

Flight / Schedule

Philadelphia - Charlotte

Registration

N854U

MSN

2009

Year of Manufacture

1959

Operator

Galaxy Airlines

Date

January 29, 1985 at 09:36 AM

Type

CRASH

Flight Type

Cargo

Flight Phase

Landing (descent or approach)

Crash Site

Airport (less than 10 km from airport)

Crash Location

Dobbins AFB Georgia

Region

North America • United States of America

Coordinates

33.9178°, -84.5091°

Crash Cause

Technical failure

Narrative Report

On January 29, 1985 at 09:36 AM, Philadelphia - Charlotte experienced a crash involving Lockheed L-188 Electra, operated by Galaxy Airlines, with the event recorded near Dobbins AFB Georgia.

The flight was categorized as cargo and the reported phase was landing (descent or approach) at a airport (less than 10 km from airport) crash site.

3 people were known to be on board, 0 fatalities were recorded, 3 survivors were identified or estimated. This corresponds to an estimated fatality rate of 0.0%.

Crew on board: 3, crew fatalities: 0, passengers on board: 0, passenger fatalities: 0, other fatalities: 0.

The listed crash cause is technical failure. During gear retraction after takeoff, the right main gear became jammed in a partially retracted position and the respective in-transit gear light would not extinguish. Attempts to recycle the gear were unsuccessful. The flight crew diverted to Atlanta, GA; then decided to land at Dobbins AFB, where there was a long, wide runway that could be foamed. Foam was applied to approximately 300 feet of runway 29. The aircraft was landed with the nose and left main gear extended and the right main gear partially retracted. Subsequently, the aircraft veered to the right and stopped with the nose gear approximately 70 feet off the runway. Fire erupted in the area of the right main gear; however, the fire was quickly extinguished by fire dept personnel. An investigation revealed the clearance between the main landing gear door hook, pn 803845-1, and the strut roller was excessive. The reason for the improper clearance was not determined. Lockheed service bulletin 88/sb-558 warned that excessive clearance combined with a drop in hydraulic pressure, gust or maneuver could result in the gear jamming. All three crew members were uninjured.

Aircraft reference details include registration N854U, MSN 2009, year of manufacture 1959.

Geospatial coordinates for this crash are approximately 33.9178°, -84.5091°.

Fatalities

Total

0

Crew

0

Passengers

0

Other

0

Crash Summary

During gear retraction after takeoff, the right main gear became jammed in a partially retracted position and the respective in-transit gear light would not extinguish. Attempts to recycle the gear were unsuccessful. The flight crew diverted to Atlanta, GA; then decided to land at Dobbins AFB, where there was a long, wide runway that could be foamed. Foam was applied to approximately 300 feet of runway 29. The aircraft was landed with the nose and left main gear extended and the right main gear partially retracted. Subsequently, the aircraft veered to the right and stopped with the nose gear approximately 70 feet off the runway. Fire erupted in the area of the right main gear; however, the fire was quickly extinguished by fire dept personnel. An investigation revealed the clearance between the main landing gear door hook, pn 803845-1, and the strut roller was excessive. The reason for the improper clearance was not determined. Lockheed service bulletin 88/sb-558 warned that excessive clearance combined with a drop in hydraulic pressure, gust or maneuver could result in the gear jamming. All three crew members were uninjured.

Cause: Technical failure

Occupants & Outcome

Crew On Board

3

Passengers On Board

0

Estimated Survivors

3

Fatality Rate

0.0%

Known people on board: 3

Operational Details

Schedule / Flight

Philadelphia - Charlotte

Operator

Galaxy Airlines

Flight Type

Cargo

Flight Phase

Landing (descent or approach)

Crash Site

Airport (less than 10 km from airport)

Region / Country

North America • United States of America

Aircraft Details

Registration

N854U

MSN

2009

Year of Manufacture

1959