Wichita – Grand Rapids
Flight / Schedule
Wichita – Grand Rapids
Aircraft
Beechcraft 60 DukeRegistration
N7277R
MSN
P-318
Year of Manufacture
1975
Operator
Scott M. BrunkeDate
September 29, 1983 at 05:20 PM
Type
CRASHFlight Type
Executive/Corporate/Business
Flight Phase
Landing (descent or approach)
Crash Site
Airport (less than 10 km from airport)
Crash Location
Wichita-Beechcraft Field Kansas
Region
North America • United States of America
Crash Cause
Technical failure
Narrative Report
On September 29, 1983 at 05:20 PM, Wichita – Grand Rapids experienced a crash involving Beechcraft 60 Duke, operated by Scott M. Brunke, with the event recorded near Wichita-Beechcraft Field Kansas.
The flight was categorized as executive/corporate/business and the reported phase was landing (descent or approach) at a airport (less than 10 km from airport) crash site.
2 people were known to be on board, 0 fatalities were recorded, 2 survivors were identified or estimated. This corresponds to an estimated fatality rate of 0.0%.
Crew on board: 2, crew fatalities: 0, passengers on board: 0, passenger fatalities: 0, other fatalities: 0.
The listed crash cause is technical failure. Shortly after takeoff, the left engine began to progressively lose power and was shut down. The aircrew notified Beech Tower of the problem and reported they would like to return and land. The aircraft was observed on final approach to runway 18 with the gear extended and the left prop stopped. Before landing, the aircraft began veering to the left. It crossed over the end of the airport at about 40 feet agl and 300 feet left (east) of the runway. The left wing and nose dropped and the aircraft impacted the ramp, left wing first. The aircraft then skidded across the ramp on a heading of 160° and collided with and damaged three other aircraft; a Beechcraft F33A registered N1833S; another Beechcraft 60 Duke registered N6747D and a Beechcraft 58 registered N5800B. An investigation revealed that the #2 exhaust valve lifter had become flat and the #2 exhaust valve had failed from fatigue. Both pilots escaped uninjured.
Aircraft reference details include registration N7277R, MSN P-318, year of manufacture 1975.
Fatalities
Total
0
Crew
0
Passengers
0
Other
0
Crash Summary
Shortly after takeoff, the left engine began to progressively lose power and was shut down. The aircrew notified Beech Tower of the problem and reported they would like to return and land. The aircraft was observed on final approach to runway 18 with the gear extended and the left prop stopped. Before landing, the aircraft began veering to the left. It crossed over the end of the airport at about 40 feet agl and 300 feet left (east) of the runway. The left wing and nose dropped and the aircraft impacted the ramp, left wing first. The aircraft then skidded across the ramp on a heading of 160° and collided with and damaged three other aircraft; a Beechcraft F33A registered N1833S; another Beechcraft 60 Duke registered N6747D and a Beechcraft 58 registered N5800B. An investigation revealed that the #2 exhaust valve lifter had become flat and the #2 exhaust valve had failed from fatigue. Both pilots escaped uninjured.
Cause: Technical failure
Occupants & Outcome
Crew On Board
2
Passengers On Board
0
Estimated Survivors
2
Fatality Rate
0.0%
Known people on board: 2
Operational Details
Schedule / Flight
Wichita – Grand Rapids
Operator
Scott M. BrunkeFlight Type
Executive/Corporate/Business
Flight Phase
Landing (descent or approach)
Crash Site
Airport (less than 10 km from airport)
Region / Country
North America • United States of America
