Perth - Esperance
Flight / Schedule
Perth - Esperance
Aircraft
Swearingen SA226 Metro IIRegistration
VH-SWO
MSN
TC-275
Year of Manufacture
1978
Operator
Skywest Airlines - AustraliaDate
May 13, 1980 at 07:45 AM
Type
CRASHFlight Type
Scheduled Revenue Flight
Flight Phase
Landing (descent or approach)
Crash Site
Airport (less than 10 km from airport)
Crash Location
Esperance Western Australia
Region
Oceania • Australia
Coordinates
-33.8615°, 121.8915°
Crash Cause
Technical failure
Narrative Report
On May 13, 1980 at 07:45 AM, Perth - Esperance experienced a crash involving Swearingen SA226 Metro II, operated by Skywest Airlines - Australia, with the event recorded near Esperance Western Australia.
The flight was categorized as scheduled revenue flight and the reported phase was landing (descent or approach) at a airport (less than 10 km from airport) crash site.
12 people were known to be on board, 0 fatalities were recorded, 12 survivors were identified or estimated. This corresponds to an estimated fatality rate of 0.0%.
Crew on board: 1, crew fatalities: 0, passengers on board: 11, passenger fatalities: 0, other fatalities: 0.
The listed crash cause is technical failure. Weather conditions at Esperance were fine; there was no cloud, visibility was in excess of 30 km and the surface wind was from the northwest at 5 to 10 knots. The aircraft entered the circuit on a left downwind leg for an approach to Runway 29. The flaps were lowered, firstly a quarter and then half-way, on the downwind leg and the landing gear was extended just before the aircraft turned onto a base leg. This configuration, and an airspeed of 133 knots (best single - engine rate of climb speed), was maintained until after the aircraft was straightened onto final approach. At an altitude of 1100 feet, the pilot considered he was at Decision Height and committed to land. He lowered full flaps and reduced the airspeed to 115 knots. At about this time, as he was retarding the power levers, the right engine flamed out. The pilot reported that he promptly sensed the engine failure and checked the engine instruments while re-opening both power levers. He noted both torque and fuel flow indication s for the right engine were zero. He briefly considered retracting the landing gear and flaps but decided to do neither. Left engine power was increased initially to the maximum available of 940°C ITT (Inter-turbine temperature) and then adjusted to the normal maximum limit of 923°C ITT. The right propeller was feathered. During this period the aircraft banked to the right and turned away from the runway. Its airspeed had reduced and the rate of descent increased. The turn had been opposed but the pilot found that the application of full left rudder and aileron would not enable him to maintain runway heading, although the airspeed was above the minimum control airspeed of 94 knots, specified in the aircraft flight manual. It was evident to the pilot that the aircraft would land short of the aerodrome, amongst trees to the right of the runway approach path. He therefore abandoned his efforts to regain the normal approach path and allowed the aircraft to turn further to the right, towards a large, clear paddock. Just before touchdown, he observed a power pole on his selected landing path and he again turned further right to avoid it. During this turn the right wing tip struck the ground. The nosegear then impacted heavily and collapsed . The aircraft slid and bounced across the ground for 188 metres before coming to rest. Fuel from ruptured line s ignite d under the left engine , but the fire was slow to develop and the occupants were able to make an orderly evacuation . By the time the fire brigade arrived from Esperance township, the fire had spread and most of the aircraft was consumed.
Aircraft reference details include registration VH-SWO, MSN TC-275, year of manufacture 1978.
Geospatial coordinates for this crash are approximately -33.8615°, 121.8915°.
Fatalities
Total
0
Crew
0
Passengers
0
Other
0
Crash Summary
Weather conditions at Esperance were fine; there was no cloud, visibility was in excess of 30 km and the surface wind was from the northwest at 5 to 10 knots. The aircraft entered the circuit on a left downwind leg for an approach to Runway 29. The flaps were lowered, firstly a quarter and then half-way, on the downwind leg and the landing gear was extended just before the aircraft turned onto a base leg. This configuration, and an airspeed of 133 knots (best single - engine rate of climb speed), was maintained until after the aircraft was straightened onto final approach. At an altitude of 1100 feet, the pilot considered he was at Decision Height and committed to land. He lowered full flaps and reduced the airspeed to 115 knots. At about this time, as he was retarding the power levers, the right engine flamed out. The pilot reported that he promptly sensed the engine failure and checked the engine instruments while re-opening both power levers. He noted both torque and fuel flow indication s for the right engine were zero. He briefly considered retracting the landing gear and flaps but decided to do neither. Left engine power was increased initially to the maximum available of 940°C ITT (Inter-turbine temperature) and then adjusted to the normal maximum limit of 923°C ITT. The right propeller was feathered. During this period the aircraft banked to the right and turned away from the runway. Its airspeed had reduced and the rate of descent increased. The turn had been opposed but the pilot found that the application of full left rudder and aileron would not enable him to maintain runway heading, although the airspeed was above the minimum control airspeed of 94 knots, specified in the aircraft flight manual. It was evident to the pilot that the aircraft would land short of the aerodrome, amongst trees to the right of the runway approach path. He therefore abandoned his efforts to regain the normal approach path and allowed the aircraft to turn further to the right, towards a large, clear paddock. Just before touchdown, he observed a power pole on his selected landing path and he again turned further right to avoid it. During this turn the right wing tip struck the ground. The nosegear then impacted heavily and collapsed . The aircraft slid and bounced across the ground for 188 metres before coming to rest. Fuel from ruptured line s ignite d under the left engine , but the fire was slow to develop and the occupants were able to make an orderly evacuation . By the time the fire brigade arrived from Esperance township, the fire had spread and most of the aircraft was consumed.
Cause: Technical failure
Occupants & Outcome
Crew On Board
1
Passengers On Board
11
Estimated Survivors
12
Fatality Rate
0.0%
Known people on board: 12
Operational Details
Schedule / Flight
Perth - Esperance
Operator
Skywest Airlines - AustraliaFlight Type
Scheduled Revenue Flight
Flight Phase
Landing (descent or approach)
Crash Site
Airport (less than 10 km from airport)
Region / Country
Oceania • Australia
Aircraft Details
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