Stockholm - Zurich

The aircraft was originally planned to fly a non-scheduled international flight from Stockholm-Arlanda to Palma de Mallorca. During the take-off run No. 4 engine did not function properly; the take-off was aborted and the aircraft was taxiied back to the apron. Inspection of the engine revealed damage to the compressor. After consultation with the Spantax Operations Department in Madrid, it was decided to ferry the aircraft on three engines to Zurich, where No. 4 engine would be changed. The technical preparation of the aircraft for the ferry flight was supervised by a ground engineer from Spantax. Meanwhile, the flight crew planned the flight. As the ATS briefing office at Arlanda was closed after 2100 hours, the co-pilot phoned the ATS flight plan to Stockholm Control Centre (ACC) . Neither when phoning the flight plan nor at the weather briefing did the crew advise that the flight was a 3-engine ferry flight. However, the Air Traffic Controller (Tower) in some other way had been informed about the nature of the flight. At 2208 hours the crew received a taxi clearance to Runway 08, but as they considered that this runway was too short for a 3-engine take-off , they requested permission to use Runway 19 and this was granted. Another advantage of using Runway 19 was that it made it possible to join the outbound track with minor heading changes. During taxiing the aircraft and the engine anti-icing system were checked according to the checklist. (After checking the engine anti-icing was switched OFF.) At 2221 hours the flight was cleared to take-off, and at 2224 hours the crew reported "Rolling". According to the pilot-in-command,maximum EPR take-off power was set on engines Nos. 1, 2 and 3 with brakes on, then, after having checked the instruments, No. 1 engine was throttled back to 85 per cent and the brakes were released. When the aircraft had rolled for 5-10 seconds the nose wheel skidded to the right and to regain heading he had to retard throttle No. 1 to 80-60 per cent. When back on the centre line he slowly opened the throttle again. Maximum EPR take-off power was set when the aircraft reached a speed of 100 kt. He rotated the aircraft at the calculated speed Vr - 134 kt (27° of flaps) and it became airborne. He retracted the gear when positive climb was indicated. Just after lift off he was blinded by the aircraft landing lights illuminating unexpectedly low clouds over the runway. Initially he kept the speed at V2 (145 kt) and noticed a rate- of-climb of 800 ft/min. He had to apply extremely hard left rudder to centre the turn indicator (ball). He did not observe any bank or turn tendency, but noted that the indicated airspeed (IAS) was not increasing normally and shortly thereafter that the rate-of-climb and speed decreased. The pilot-in-command felt they urgently needed more power, but all happened very quickly and shortly after he had noticed the speed drop the aircraft collided with the terrain. From the time take-off power had been set on the runway the throttle positions were not changed. The co-pilot stated that they had to taxi down the runway to avoid ice patches on the first part of the runway. He could not say how far they taxiied and it was not possible to determine it in any other way. During preparation for take-off he asked the pilot-in-command if they should use 10° flaps, but the decision of the pilot- in-command to uae 27° was not changed. He completed the pre-take-off instrument check and did not notice any abnormal readings. The three gyro horizons indicated no differences. When rolling he kept the control column forward, to increase the friction on the nose wheel, and gave full left aileron. Gradually he decreased the pressure on the column and reduced left aileron deflection. At V1 the pilot-in-command took mr the controls. The co-pilot kept his left hand on the throttles and verified that no changes were made on throttles Nos. 2 and 3 after takeoff power was set, but he noticed that the pilot-in-command had to vary the No. 1 throttle setting several times during the roll. After lift-off when the gear was retracted the co-pilot received a message from the tower giving the take-off time and instruction to change over to STOCKHOLM RADAR on 124.1 MHz. He never acknowledged the message but when leaning forward to select the new frequency he noticed on his horizon a banking to the right of 4 to 60. He also observed the gyro horizon of the pilot-in-command indicating o bank to the right. Zhe speed had dropped to 10 kt belau V2 and he called: "The speed, the speed". Ifc felt no buffeting in the aircraft aud noted no tendency to Dutch roll. Be also stated that he observed a power drop of about 2 per cent below EPR take-off power. Shortly after the first contact with the treetops the banking to the right had increased to 10-lSO and the co-pilot retarded the throttles. The flight and the ground engineers sitting in the cockpit observed nothing abnormal until the crash. None of them observed any indications of power changes on the instruments. No buffeting was felt in the aircraft, neither were any warning signals heard. Whilst in a right bank of 4-6° the aircraft collided with tree-tops approximately 26 m above and 1 060 m from the far end of Runway 19, or about 1 800 m from the point of lift-off, having turned through about 25 degrees from the runway heading. The aircraft came to a final stop approximately 500 m after first contact with the trees on a heading of 240°. The aircraft was destroyed and five occupants were killed while five others were injured.

Flight / Schedule

Stockholm - Zurich

Aircraft

Convair CV-990

Registration

EC-BNM

MSN

30-10-32

Year of Manufacture

1962

Operator

Spantax

Date

January 5, 1970 at 10:25 PM

Type

CRASH

Flight Type

Positioning

Flight Phase

Takeoff (climb)

Crash Site

Airport (less than 10 km from airport)

Crash Location

Stockholm-Arlanda Uppland

Region

Europe • Sweden

Crash Cause

Human factor

Narrative Report

On January 5, 1970 at 10:25 PM, Stockholm - Zurich experienced a crash involving Convair CV-990, operated by Spantax, with the event recorded near Stockholm-Arlanda Uppland.

The flight was categorized as positioning and the reported phase was takeoff (climb) at a airport (less than 10 km from airport) crash site.

10 people were known to be on board, 5 fatalities were recorded, 5 survivors were identified or estimated. This corresponds to an estimated fatality rate of 50.0%.

Crew on board: 3, crew fatalities: 0, passengers on board: 7, passenger fatalities: 5, other fatalities: 0.

The listed crash cause is human factor. The aircraft was originally planned to fly a non-scheduled international flight from Stockholm-Arlanda to Palma de Mallorca. During the take-off run No. 4 engine did not function properly; the take-off was aborted and the aircraft was taxiied back to the apron. Inspection of the engine revealed damage to the compressor. After consultation with the Spantax Operations Department in Madrid, it was decided to ferry the aircraft on three engines to Zurich, where No. 4 engine would be changed. The technical preparation of the aircraft for the ferry flight was supervised by a ground engineer from Spantax. Meanwhile, the flight crew planned the flight. As the ATS briefing office at Arlanda was closed after 2100 hours, the co-pilot phoned the ATS flight plan to Stockholm Control Centre (ACC) . Neither when phoning the flight plan nor at the weather briefing did the crew advise that the flight was a 3-engine ferry flight. However, the Air Traffic Controller (Tower) in some other way had been informed about the nature of the flight. At 2208 hours the crew received a taxi clearance to Runway 08, but as they considered that this runway was too short for a 3-engine take-off , they requested permission to use Runway 19 and this was granted. Another advantage of using Runway 19 was that it made it possible to join the outbound track with minor heading changes. During taxiing the aircraft and the engine anti-icing system were checked according to the checklist. (After checking the engine anti-icing was switched OFF.) At 2221 hours the flight was cleared to take-off, and at 2224 hours the crew reported "Rolling". According to the pilot-in-command,maximum EPR take-off power was set on engines Nos. 1, 2 and 3 with brakes on, then, after having checked the instruments, No. 1 engine was throttled back to 85 per cent and the brakes were released. When the aircraft had rolled for 5-10 seconds the nose wheel skidded to the right and to regain heading he had to retard throttle No. 1 to 80-60 per cent. When back on the centre line he slowly opened the throttle again. Maximum EPR take-off power was set when the aircraft reached a speed of 100 kt. He rotated the aircraft at the calculated speed Vr - 134 kt (27° of flaps) and it became airborne. He retracted the gear when positive climb was indicated. Just after lift off he was blinded by the aircraft landing lights illuminating unexpectedly low clouds over the runway. Initially he kept the speed at V2 (145 kt) and noticed a rate- of-climb of 800 ft/min. He had to apply extremely hard left rudder to centre the turn indicator (ball). He did not observe any bank or turn tendency, but noted that the indicated airspeed (IAS) was not increasing normally and shortly thereafter that the rate-of-climb and speed decreased. The pilot-in-command felt they urgently needed more power, but all happened very quickly and shortly after he had noticed the speed drop the aircraft collided with the terrain. From the time take-off power had been set on the runway the throttle positions were not changed. The co-pilot stated that they had to taxi down the runway to avoid ice patches on the first part of the runway. He could not say how far they taxiied and it was not possible to determine it in any other way. During preparation for take-off he asked the pilot-in-command if they should use 10° flaps, but the decision of the pilot- in-command to uae 27° was not changed. He completed the pre-take-off instrument check and did not notice any abnormal readings. The three gyro horizons indicated no differences. When rolling he kept the control column forward, to increase the friction on the nose wheel, and gave full left aileron. Gradually he decreased the pressure on the column and reduced left aileron deflection. At V1 the pilot-in-command took mr the controls. The co-pilot kept his left hand on the throttles and verified that no changes were made on throttles Nos. 2 and 3 after takeoff power was set, but he noticed that the pilot-in-command had to vary the No. 1 throttle setting several times during the roll. After lift-off when the gear was retracted the co-pilot received a message from the tower giving the take-off time and instruction to change over to STOCKHOLM RADAR on 124.1 MHz. He never acknowledged the message but when leaning forward to select the new frequency he noticed on his horizon a banking to the right of 4 to 60. He also observed the gyro horizon of the pilot-in-command indicating o bank to the right. Zhe speed had dropped to 10 kt belau V2 and he called: "The speed, the speed". Ifc felt no buffeting in the aircraft aud noted no tendency to Dutch roll. Be also stated that he observed a power drop of about 2 per cent below EPR take-off power. Shortly after the first contact with the treetops the banking to the right had increased to 10-lSO and the co-pilot retarded the throttles. The flight and the ground engineers sitting in the cockpit observed nothing abnormal until the crash. None of them observed any indications of power changes on the instruments. No buffeting was felt in the aircraft, neither were any warning signals heard. Whilst in a right bank of 4-6° the aircraft collided with tree-tops approximately 26 m above and 1 060 m from the far end of Runway 19, or about 1 800 m from the point of lift-off, having turned through about 25 degrees from the runway heading. The aircraft came to a final stop approximately 500 m after first contact with the trees on a heading of 240°. The aircraft was destroyed and five occupants were killed while five others were injured.

Aircraft reference details include registration EC-BNM, MSN 30-10-32, year of manufacture 1962.

Fatalities

Total

5

Crew

0

Passengers

5

Other

0

Crash Summary

The aircraft was originally planned to fly a non-scheduled international flight from Stockholm-Arlanda to Palma de Mallorca. During the take-off run No. 4 engine did not function properly; the take-off was aborted and the aircraft was taxiied back to the apron. Inspection of the engine revealed damage to the compressor. After consultation with the Spantax Operations Department in Madrid, it was decided to ferry the aircraft on three engines to Zurich, where No. 4 engine would be changed. The technical preparation of the aircraft for the ferry flight was supervised by a ground engineer from Spantax. Meanwhile, the flight crew planned the flight. As the ATS briefing office at Arlanda was closed after 2100 hours, the co-pilot phoned the ATS flight plan to Stockholm Control Centre (ACC) . Neither when phoning the flight plan nor at the weather briefing did the crew advise that the flight was a 3-engine ferry flight. However, the Air Traffic Controller (Tower) in some other way had been informed about the nature of the flight. At 2208 hours the crew received a taxi clearance to Runway 08, but as they considered that this runway was too short for a 3-engine take-off , they requested permission to use Runway 19 and this was granted. Another advantage of using Runway 19 was that it made it possible to join the outbound track with minor heading changes. During taxiing the aircraft and the engine anti-icing system were checked according to the checklist. (After checking the engine anti-icing was switched OFF.) At 2221 hours the flight was cleared to take-off, and at 2224 hours the crew reported "Rolling". According to the pilot-in-command,maximum EPR take-off power was set on engines Nos. 1, 2 and 3 with brakes on, then, after having checked the instruments, No. 1 engine was throttled back to 85 per cent and the brakes were released. When the aircraft had rolled for 5-10 seconds the nose wheel skidded to the right and to regain heading he had to retard throttle No. 1 to 80-60 per cent. When back on the centre line he slowly opened the throttle again. Maximum EPR take-off power was set when the aircraft reached a speed of 100 kt. He rotated the aircraft at the calculated speed Vr - 134 kt (27° of flaps) and it became airborne. He retracted the gear when positive climb was indicated. Just after lift off he was blinded by the aircraft landing lights illuminating unexpectedly low clouds over the runway. Initially he kept the speed at V2 (145 kt) and noticed a rate- of-climb of 800 ft/min. He had to apply extremely hard left rudder to centre the turn indicator (ball). He did not observe any bank or turn tendency, but noted that the indicated airspeed (IAS) was not increasing normally and shortly thereafter that the rate-of-climb and speed decreased. The pilot-in-command felt they urgently needed more power, but all happened very quickly and shortly after he had noticed the speed drop the aircraft collided with the terrain. From the time take-off power had been set on the runway the throttle positions were not changed. The co-pilot stated that they had to taxi down the runway to avoid ice patches on the first part of the runway. He could not say how far they taxiied and it was not possible to determine it in any other way. During preparation for take-off he asked the pilot-in-command if they should use 10° flaps, but the decision of the pilot- in-command to uae 27° was not changed. He completed the pre-take-off instrument check and did not notice any abnormal readings. The three gyro horizons indicated no differences. When rolling he kept the control column forward, to increase the friction on the nose wheel, and gave full left aileron. Gradually he decreased the pressure on the column and reduced left aileron deflection. At V1 the pilot-in-command took mr the controls. The co-pilot kept his left hand on the throttles and verified that no changes were made on throttles Nos. 2 and 3 after takeoff power was set, but he noticed that the pilot-in-command had to vary the No. 1 throttle setting several times during the roll. After lift-off when the gear was retracted the co-pilot received a message from the tower giving the take-off time and instruction to change over to STOCKHOLM RADAR on 124.1 MHz. He never acknowledged the message but when leaning forward to select the new frequency he noticed on his horizon a banking to the right of 4 to 60. He also observed the gyro horizon of the pilot-in-command indicating o bank to the right. Zhe speed had dropped to 10 kt belau V2 and he called: "The speed, the speed". Ifc felt no buffeting in the aircraft aud noted no tendency to Dutch roll. Be also stated that he observed a power drop of about 2 per cent below EPR take-off power. Shortly after the first contact with the treetops the banking to the right had increased to 10-lSO and the co-pilot retarded the throttles. The flight and the ground engineers sitting in the cockpit observed nothing abnormal until the crash. None of them observed any indications of power changes on the instruments. No buffeting was felt in the aircraft, neither were any warning signals heard. Whilst in a right bank of 4-6° the aircraft collided with tree-tops approximately 26 m above and 1 060 m from the far end of Runway 19, or about 1 800 m from the point of lift-off, having turned through about 25 degrees from the runway heading. The aircraft came to a final stop approximately 500 m after first contact with the trees on a heading of 240°. The aircraft was destroyed and five occupants were killed while five others were injured.

Cause: Human factor

Occupants & Outcome

Crew On Board

3

Passengers On Board

7

Estimated Survivors

5

Fatality Rate

50.0%

Known people on board: 10

Operational Details

Schedule / Flight

Stockholm - Zurich

Operator

Spantax

Flight Type

Positioning

Flight Phase

Takeoff (climb)

Crash Site

Airport (less than 10 km from airport)

Region / Country

Europe • Sweden

Aircraft Details

Aircraft

Convair CV-990

Registration

EC-BNM

MSN

30-10-32

Year of Manufacture

1962

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