Hong Kong - Saigon - Bangkok

Flight CX033 was a scheduled flight from Hong Kong to Bangkok with an additional en-route stop at Saigon to transport a backlog of passengers. A Check captain joined the flight. The co-pilot was flying the aircraft from the left-hand seat whilst the pilot-in-command occupied the right-hand seat to assess his performance. The Check captain occupied the jump seat behind the co-pilot from where he could monitor the performance of both pilots. At 10:31 the aircraft commenced to taxi out for takeoff on runway 13. A wind check of 010/10 kt was passed by the tower and acknowledged by the aircraft when the takeoff clearance was given. At 10:34 a rolling takeoff was commenced. The co-pilot, who was piloting the aircraft, increased the power to 1.5 EPR after which the engineer set the engines at maximum power. The aircraft accelerated normally but at a speed of slightly under 120 kt (as reported by the co-pilot) heavy vibration was experienced. The vibration increased in severity and the co-pilot decided to discontinue the takeoff. He called "abort", closed the power levers, applied maximum symmetrical braking and selected the spoilers. The abort action was stated to have been taken promptly except that there was a delay of 4-5 sec in applying reverse thrust which was then used at full power throughout the remainder of the aircraft's travel. No significant decrease in the rate of acceleration occurred until after an indicated airspeed of 133 kt had been attained, there was then a slow build-up of speed to 137 kt over the next 2 sec after which deceleration commenced. Both pilots were applying full brakes but neither of them felt the antiskid cycling. The aircraft continued to run straight some distance after initial braking was applied but then a veer to the right commenced. Opposite rudder was used but failed to check this forcing the use of differential braking to the extent that eventually the right brake had been eased off completely, whilst maximum left braking, full left rudder, full lateral control to the left, and nose-wheel steering were being applied, These actions were only partly effective and the aircraft eventually left the runway and entered the grass strip. The turn to the right continued until finally the aircraft crossed the seawall. All four engines separated on impact with, the sea, the nose of the aircraft was smashed in and the fuselage above floor level between the flight deck and the leading edge of the wing was fractured in two places. The aircraft spun to the right and came to rest some 400 ft from the seawall. A passenger was killed while 33 other were injured.

Flight / Schedule

Hong Kong - Saigon - Bangkok

Aircraft

Convair CV-880

Registration

VR-HFX

MSN

22-00-37M

Year of Manufacture

1963

Date

November 5, 1967 at 10:35 AM

Type

CRASH

Flight Type

Scheduled Revenue Flight

Flight Phase

Takeoff (climb)

Crash Site

Airport (less than 10 km from airport)

Crash Location

Hong Kong-Kai Tak Hong Kong

Region

Asia • China

Coordinates

22.3316°, 114.2031°

Crash Cause

Technical failure

Narrative Report

On November 5, 1967 at 10:35 AM, Hong Kong - Saigon - Bangkok experienced a crash involving Convair CV-880, operated by Cathay Pacific Airways, with the event recorded near Hong Kong-Kai Tak Hong Kong.

The flight was categorized as scheduled revenue flight and the reported phase was takeoff (climb) at a airport (less than 10 km from airport) crash site.

127 people were known to be on board, 1 fatalities were recorded, 126 survivors were identified or estimated. This corresponds to an estimated fatality rate of 0.8%.

Crew on board: 11, crew fatalities: 0, passengers on board: 116, passenger fatalities: 1, other fatalities: 0.

The listed crash cause is technical failure. Flight CX033 was a scheduled flight from Hong Kong to Bangkok with an additional en-route stop at Saigon to transport a backlog of passengers. A Check captain joined the flight. The co-pilot was flying the aircraft from the left-hand seat whilst the pilot-in-command occupied the right-hand seat to assess his performance. The Check captain occupied the jump seat behind the co-pilot from where he could monitor the performance of both pilots. At 10:31 the aircraft commenced to taxi out for takeoff on runway 13. A wind check of 010/10 kt was passed by the tower and acknowledged by the aircraft when the takeoff clearance was given. At 10:34 a rolling takeoff was commenced. The co-pilot, who was piloting the aircraft, increased the power to 1.5 EPR after which the engineer set the engines at maximum power. The aircraft accelerated normally but at a speed of slightly under 120 kt (as reported by the co-pilot) heavy vibration was experienced. The vibration increased in severity and the co-pilot decided to discontinue the takeoff. He called "abort", closed the power levers, applied maximum symmetrical braking and selected the spoilers. The abort action was stated to have been taken promptly except that there was a delay of 4-5 sec in applying reverse thrust which was then used at full power throughout the remainder of the aircraft's travel. No significant decrease in the rate of acceleration occurred until after an indicated airspeed of 133 kt had been attained, there was then a slow build-up of speed to 137 kt over the next 2 sec after which deceleration commenced. Both pilots were applying full brakes but neither of them felt the antiskid cycling. The aircraft continued to run straight some distance after initial braking was applied but then a veer to the right commenced. Opposite rudder was used but failed to check this forcing the use of differential braking to the extent that eventually the right brake had been eased off completely, whilst maximum left braking, full left rudder, full lateral control to the left, and nose-wheel steering were being applied, These actions were only partly effective and the aircraft eventually left the runway and entered the grass strip. The turn to the right continued until finally the aircraft crossed the seawall. All four engines separated on impact with, the sea, the nose of the aircraft was smashed in and the fuselage above floor level between the flight deck and the leading edge of the wing was fractured in two places. The aircraft spun to the right and came to rest some 400 ft from the seawall. A passenger was killed while 33 other were injured.

Aircraft reference details include registration VR-HFX, MSN 22-00-37M, year of manufacture 1963.

Geospatial coordinates for this crash are approximately 22.3316°, 114.2031°.

Fatalities

Total

1

Crew

0

Passengers

1

Other

0

Crash Summary

Flight CX033 was a scheduled flight from Hong Kong to Bangkok with an additional en-route stop at Saigon to transport a backlog of passengers. A Check captain joined the flight. The co-pilot was flying the aircraft from the left-hand seat whilst the pilot-in-command occupied the right-hand seat to assess his performance. The Check captain occupied the jump seat behind the co-pilot from where he could monitor the performance of both pilots. At 10:31 the aircraft commenced to taxi out for takeoff on runway 13. A wind check of 010/10 kt was passed by the tower and acknowledged by the aircraft when the takeoff clearance was given. At 10:34 a rolling takeoff was commenced. The co-pilot, who was piloting the aircraft, increased the power to 1.5 EPR after which the engineer set the engines at maximum power. The aircraft accelerated normally but at a speed of slightly under 120 kt (as reported by the co-pilot) heavy vibration was experienced. The vibration increased in severity and the co-pilot decided to discontinue the takeoff. He called "abort", closed the power levers, applied maximum symmetrical braking and selected the spoilers. The abort action was stated to have been taken promptly except that there was a delay of 4-5 sec in applying reverse thrust which was then used at full power throughout the remainder of the aircraft's travel. No significant decrease in the rate of acceleration occurred until after an indicated airspeed of 133 kt had been attained, there was then a slow build-up of speed to 137 kt over the next 2 sec after which deceleration commenced. Both pilots were applying full brakes but neither of them felt the antiskid cycling. The aircraft continued to run straight some distance after initial braking was applied but then a veer to the right commenced. Opposite rudder was used but failed to check this forcing the use of differential braking to the extent that eventually the right brake had been eased off completely, whilst maximum left braking, full left rudder, full lateral control to the left, and nose-wheel steering were being applied, These actions were only partly effective and the aircraft eventually left the runway and entered the grass strip. The turn to the right continued until finally the aircraft crossed the seawall. All four engines separated on impact with, the sea, the nose of the aircraft was smashed in and the fuselage above floor level between the flight deck and the leading edge of the wing was fractured in two places. The aircraft spun to the right and came to rest some 400 ft from the seawall. A passenger was killed while 33 other were injured.

Cause: Technical failure

Occupants & Outcome

Crew On Board

11

Passengers On Board

116

Estimated Survivors

126

Fatality Rate

0.8%

Known people on board: 127

Operational Details

Schedule / Flight

Hong Kong - Saigon - Bangkok

Flight Type

Scheduled Revenue Flight

Flight Phase

Takeoff (climb)

Crash Site

Airport (less than 10 km from airport)

Region / Country

Asia • China

Aircraft Details

Aircraft

Convair CV-880

Registration

VR-HFX

MSN

22-00-37M

Year of Manufacture

1963