Hickam – Wake Island – Tokyo

While cruising by night, the crew informed ATC about technical issues with the number three and elected to feather the propeller. In the mean time, the captain decided to divert to Hickam Field. Thirteen minutes later, the crew reported he was unable to feather the propeller that was windmilling while the engine number three was losing oil. In such condition, the captain decided to divert to Johnston atoll closer from his position. Unfortunately, shortly later, a propeller detached from the engine number three and struck the ailerons, causing serious control difficulties. The crew reduced his altitude and attempted to ditch the airplane about 200 miles northeast of the Johnston atoll. Rescuers arrived twelve hours later and were able to evacuate three wounded crew members while the aircraft sank and six other occupants were killed.

Flight / Schedule

Hickam – Wake Island – Tokyo

Registration

50-0107

MSN

43245

Year of Manufacture

1950

Date

July 4, 1958 at 01:33 AM

Type

CRASH

Flight Type

Military

Flight Phase

Flight

Crash Site

Lake, Sea, Ocean, River

Crash Location

Pacific Ocean All World

Region

World • World

Crash Cause

Technical failure

Narrative Report

On July 4, 1958 at 01:33 AM, Hickam – Wake Island – Tokyo experienced a crash involving Douglas C-124 Globemaster II, operated by United States Air Force - USAF, with the event recorded near Pacific Ocean All World.

The flight was categorized as military and the reported phase was flight at a lake, sea, ocean, river crash site.

9 people were known to be on board, 6 fatalities were recorded, 3 survivors were identified or estimated. This corresponds to an estimated fatality rate of 66.7%.

Crew on board: 7, crew fatalities: 4, passengers on board: 2, passenger fatalities: 2, other fatalities: 0.

The listed crash cause is technical failure. While cruising by night, the crew informed ATC about technical issues with the number three and elected to feather the propeller. In the mean time, the captain decided to divert to Hickam Field. Thirteen minutes later, the crew reported he was unable to feather the propeller that was windmilling while the engine number three was losing oil. In such condition, the captain decided to divert to Johnston atoll closer from his position. Unfortunately, shortly later, a propeller detached from the engine number three and struck the ailerons, causing serious control difficulties. The crew reduced his altitude and attempted to ditch the airplane about 200 miles northeast of the Johnston atoll. Rescuers arrived twelve hours later and were able to evacuate three wounded crew members while the aircraft sank and six other occupants were killed.

Aircraft reference details include registration 50-0107, MSN 43245, year of manufacture 1950.

Fatalities

Total

6

Crew

4

Passengers

2

Other

0

Crash Summary

While cruising by night, the crew informed ATC about technical issues with the number three and elected to feather the propeller. In the mean time, the captain decided to divert to Hickam Field. Thirteen minutes later, the crew reported he was unable to feather the propeller that was windmilling while the engine number three was losing oil. In such condition, the captain decided to divert to Johnston atoll closer from his position. Unfortunately, shortly later, a propeller detached from the engine number three and struck the ailerons, causing serious control difficulties. The crew reduced his altitude and attempted to ditch the airplane about 200 miles northeast of the Johnston atoll. Rescuers arrived twelve hours later and were able to evacuate three wounded crew members while the aircraft sank and six other occupants were killed.

Cause: Technical failure

Occupants & Outcome

Crew On Board

7

Passengers On Board

2

Estimated Survivors

3

Fatality Rate

66.7%

Known people on board: 9

Operational Details

Schedule / Flight

Hickam – Wake Island – Tokyo

Flight Type

Military

Flight Phase

Flight

Crash Site

Lake, Sea, Ocean, River

Region / Country

World • World

Aircraft Details

Registration

50-0107

MSN

43245

Year of Manufacture

1950

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