Greco Air

Safety profile and incident history for Greco Air.

Safety Score

9.9/10

Total Incidents

1

Total Fatalities

1

Recent Incidents

January 6, 1990 1 Fatalities

Lockheed L-1329 JetStar

Miami-Intl Florida

Flight was a 3-engine ferry with the #4 engine shut down. During takeoff roll at V1 the #2 engine overheat light came on. According to the copilot the pilot reduced throttle slightly and continued the takeoff. After lift-off the pilot aborted the takeoff. The airplane could not be stopped on the remaining runway and collided with antennas, approach lights and a construction site 1,180 feet from the departure end of the runway. Postcrash exam of the 3 operating engines did not reveal any evidence of mechanical failure or malfunction. A failed resistor was found in the #2 engine electronic engine control (eec). This would cause the unit to over-schedule fuel to the engine resulting in hotter engine operating temperatures. Retarding the throttle would reduce fuel flow to within normal ranges for engine operation. Under conditions that existed at the time of the accident, the airplane would have a 3-engine rate-of-climb of 1,398 fpm, and a 2-engome rate-of-climb of 350 fpm. The captain was killed while the copilot was seriously injured.

Airline Information

Country of Origin

United States of America

Risk Level

Low Risk

Common Aircraft in Incidents

Lockheed L-1329 JetStar1